ML020950889

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IR 05000266/2001-017 (Drs), 05000301/2001-017 (Drs), on 12/03/2001-02/28/2002, Nuclear Management Company, LLC, Point Beach Nuclear Plant. Special Inspection. Violations Identified
ML020950889
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 04/03/2002
From: Dyer J
NRC/RGN-III
To: Warner M
Nuclear Management Co
References
EA-02-031 IR-01-017
Download: ML020950889 (25)


See also: IR 05000266/2001017

Text

April 3, 2002

EA-02-031

Mr. M. Warner

Site Vice President

Kewaunee and Point Beach Nuclear Plants

Nuclear Management Company, LLC

6610 Nuclear Road

Two Rivers, WI 54241

SUBJECT:

POINT BEACH SPECIAL INSPECTION - NRC INSPECTION

REPORT 50-266/01-17(DRS); 50-301/01-17(DRS), PRELIMINARY

RED FINDING

Dear Mr. Warner:

Your staff notified the NRC of a potential common mode failure, discovered by the Nuclear

Management Company, of auxiliary feedwater pumps at the Point Beach Nuclear Plant. In

response to the notification, the NRC conducted a Special Inspection at the facility. The

reported potential common mode failure met the NRC Management Directive 8.3, NRC

Incident Investigation Program, threshold for a Special Inspection in that the potential common

mode failure could have led to a loss of safety function. The Special Inspection was conducted

December 3, 2001, through February 28, 2002, in accordance with Inspection Procedure 93812, Special Inspection. On February 28, 2002, the NRC discussed with you and members

of your staff, by telephone, the results of the Special Inspection. The enclosed report presents

the results of that inspection.

This report discusses an issue that appears to have high safety significance. As described in

Section 4OA3.1 of this report, your staff identified a potential common mode failure of the

auxiliary feedwater pumps due to inadequate operator actions in response to a loss of

instrument air. Although your staff identified this issue in November 2001, the inspection

identified that inadequate procedure guidance had existed for many years and that there were

seven prior opportunities to identify the issue. The failures to provide adequate procedural

guidance and to take appropriate corrective actions were both apparent violations of 10 CFR Part 50, Appendix B, Criteria V and XVI. This issue was assessed using the applicable

Significance Determination Process and was preliminarily determined to be Red, an issue with

high safety significance that may result in additional NRC inspection. This issue is of high

safety significance because a common mode failure of auxiliary feedwater pumps would result

in substantially reduced mitigation capability for safely shutting down the plant in response to

certain transients. Your staff took prompt corrective actions to revise procedures and train

operators to address the immediate safety concerns associated with the issue. Additionally,

you recently installed backup pneumatic supplies for the recirculation valves to improve the

safety of the auxiliary feedwater system design.

M. Warner

-2-

Two apparent violations of NRC requirements were identified during the inspection and are

being considered for escalated enforcement action in accordance with the "General Statement

of Policy and Procedure for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600.

The current Enforcement Policy is included on the NRCs website at www.nrc.gov.

Before the NRC makes a final decision on these matters, we are providing you an opportunity

to request a Regulatory Conference where you would be able to provide your perspectives on

the significance of the findings, the bases for your position, and whether you agree with the

apparent violations. If you choose to request a conference, we encourage you to submit your

evaluation and any differences with the NRC evaluations at least one week prior to the

conference in an effort to make the conference more efficient and effective. If a conference is

held, it will be open for public observation. The NRC will also issue a press release to

announce the conference.

Please contact Mr. John M. Jacobson at (630) 829-9736 within seven days of the date of this

letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we will

continue with our significance determination and enforcement decision and you will be advised

by separate correspondence of the results of our deliberations on these matters.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for these inspection findings at this time. In addition, please be advised that the number

and characterization of apparent violations described in the enclosed inspection report may

change as a result of further NRC review.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure, and your responses will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

J. E. Dyer

Regional Administrator

Docket Nos. 50-266; 50-301

License Nos. DPR-24; DPR-27

Enclosure:

Special Inspection Report 50-266/01-17(DRS);

50-301/01-17 (DRS)

See Attached Distribution

M. Warner

-3-

Distribution

cc w/encl:

R. Grigg, President and Chief

Operating Officer, WEPCo

R. Anderson, Executive Vice President

and Chief Nuclear Officer

T. Webb, Licensing Manager

D. Weaver, Nuclear Asset Manager

T. Taylor, Plant Manager

A. Cayia, Site Director

J. ONeill, Jr., Shaw, Pittman,

Potts & Trowbridge

K. Duveneck, Town Chairman

Town of Two Creeks

D. Graham, Director

Bureau of Field Operations

A. Bie, Chairperson, Wisconsin

Public Service Commission

S. Jenkins, Electric Division

Wisconsin Public Service Commission

State Liaison Officer

M. Warner

-2-

Two apparent violations of NRC requirements were identified during the inspection and are

being considered for escalated enforcement action in accordance with the "General Statement

of Policy and Procedure for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600.

The current Enforcement Policy is included on the NRCs website at www.nrc.gov.

Before the NRC makes a final decision on these matters, we are providing you an opportunity

to request a Regulatory Conference where you would be able to provide your perspectives on

the significance of the findings, the bases for your position, and whether you agree with the

apparent violations. If you choose to request a conference, we encourage you to submit your

evaluation and any differences with the NRC evaluations at least one week prior to the

conference in an effort to make the conference more efficient and effective. If a conference is

held, it will be open for public observation. The NRC will also issue a press release to

announce the conference.

Please contact Mr. John M. Jacobson at (630) 829-9736 within seven days of the date of this

letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we will

continue with our significance determination and enforcement decision and you will be advised

by separate correspondence of the results of our deliberations on these matters.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for these inspection findings at this time. In addition, please be advised that the number

and characterization of apparent violations described in the enclosed inspection report may

change as a result of further NRC review.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure, and your responses will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

J. E. Dyer

Regional Administrator

Docket Nos. 50-266; 50-301

License Nos. DPR-24; DPR-27

Enclosure:

Special Inspection Report 50-266/01-17(DRS);

50-301/01-17 (DRS)

See Attached Distribution

DOCUMENT NAME: G:DRS\\ML020950889.wpd / *See Previous Concurrence

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE

RIII *

RIII *

E RIII *

RIII

NAME

RLangstaff:sd

KOBrien for

JJacobson

MKunowski for

RLanksbury

BClayton

DATE

03/29/02

03/29/02

03/28/02

4/2/02

OFFICE

RIII

RIII

NAME

JGrobe

JDyer

DATE

4/2/02

4/3/02

OFFICIAL RECORD COPY

M. Warner

-3-

Distribution

cc w/encl:

R. Grigg, President and Chief

Operating Officer, WEPCo

R. Anderson, Executive Vice President

and Chief Nuclear Officer

T. Webb, Licensing Manager

D. Weaver, Nuclear Asset Manager

T. Taylor, Plant Manager

A. Cayia, Site Director

J. ONeill, Jr., Shaw, Pittman,

Potts & Trowbridge

K. Duveneck, Town Chairman

Town of Two Creeks

D. Graham, Director

Bureau of Field Operations

A. Bie, Chairperson, Wisconsin

Public Service Commission

S. Jenkins, Electric Division

Wisconsin Public Service Commission

State Liaison Officer

ADAMS Distribution:

SECY

OCA

W. Kane, DEDRP

F. Congel, OE

J. Luehman, OE

C. Nolan, OE

J. Dyer, RIII:RA

D. Dambly, OGC

S. Collins, NRR

R. Borchardt, NRR

M. Johnson, NRR

Enforcement Coordinators

RI, RII, RIII, RIV

T. Frye, NRR

Resident Inspector

S. Gagner, OPA

H. Bell, OIG

F. Combs, OSTP

D. Dandois, OCFO/DAF/LFARB

WDR

DFT

BAW

RidsNrrDipmIipb

GEG

HBC

PGK1

C. Ariano (hard copy)

DRPIII

DRSIII

PLB1

JRK1

J. Strasma, RIII:PA

R. Lickus, RIII

J. Lynch, RIII

OEMAIL

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

License Nos:

50-266; 50-301

DPR-24; DPR-27

Report No:

50-266/01-17(DRS); 50-301/01-17(DRS)

Licensee:

Nuclear Management Company, LLC

Facility:

Point Beach Nuclear Plant, Units 1 & 2

Location:

6610 Nuclear Road

Two Rivers, WI 54241

Dates:

December 3, 2001, through February 28, 2002

Lead Inspector:

R. Langstaff, Senior Reactor Inspector

Mechanical Engineering Branch

Inspectors:

S. Burgess, Senior Reactor Analyst

Division of Reactor Safety

A. Dunlop, Senior Reactor Inspector

Mechanical Engineering Branch

G. ODwyer, Reactor Inspector

Mechanical Engineering Branch

R. Powell, Resident Inspector

Point Beach Nuclear Plant

Approved By:

J. Jacobson, Chief

Mechanical Engineering Branch

Division of Reactor Safety

2

SUMMARY OF FINDINGS

IR 05000266-01-17(DRS), 05000301-01-17(DRS), on 12/03/2001-02/28/2002, Nuclear

Management Company, LLC, Point Beach Nuclear Plant. Special Inspection.

This Special Inspection was conducted by a team of three Region III inspectors, a

Region III senior reactor analyst, and a resident inspector. The inspection identified one

finding preliminarily of high safety significance (Red) with two associated apparent

violations. The significance of this finding is indicated by the color Red using Inspection

Manual Chapter 0609, Significance Determination Process (SDP). The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described at its

Reactor Oversight Process website at http://www.nrc.gov/NRR/OVERSIGHT/index.html.

A.

Findings

Cornerstone: Mitigating Systems

TBD. Units 1 and 2. The licensee identified a potential common mode failure of

the auxiliary feedwater pumps due to operator actions specified in plant

procedures. The team identified that procedural guidance provided to operators

was inadequate to prevent such a common mode failure. In addition, the team

identified that the licensee had seven opportunities, from 1981 through 1997, to

identify the problem and take appropriate corrective actions. The failures to

provide adequate procedural guidance and to take appropriate corrective actions

are both apparent violations of 10 CFR Part 50, Appendix B, Criteria V and XVI.

This issue has been preliminarily determined to have high safety significance

(Red). A common mode failure of the auxiliary feedwater pumps would result in

substantially reduced mitigation capability for safely shutting down the plant in

response to certain transients. The significance was determined to be high

largely due to the relatively high initiating event frequencies associated with the

involved transients and the high likelihood of improper operator actions due to

the procedural inadequacies. (Section 4OA3.1)

3

Report Details

Summary of Plant Status:

At the beginning of the inspection period, Unit 1 was being operated at approximately

98 percent power for work associated with the plant process computer system (PPCS). Unit 1

continued to be operated at 98 percent power until December 18, when power was reduced to

30 percent to reduce the potential dose to workers for a containment entry to isolate a small

leak on the sensing line for 1PT-420, reactor coolant system (RCS) wide range pressure

detector. Unit 1 was returned to 98 percent power on December 19 and to 100 percent power

on December 24 after the PPCS modification was accepted for Rated Thermal Power

calculation purposes. Unit 1 continued to be operated at or near full power throughout the

remainder of inspection period.

At the beginning of the inspection period, Unit 2 was being operated at approximately

98 percent power for work associated with the PPCS. Unit 2 continued to be operated at 98

percent power until December 7, when power was reduced to 92 percent for condenser steam

dump testing. Unit 2 was returned to 98 percent power on December 19 and to 100 percent

power on December 24 after the PPCS modification was accepted for Rated Thermal Power

calculation purposes. Unit 2 was shutdown on February 22, 2002, to meet a Technical

Specification action statement regarding a safety injection pump. A rotating assembly for a

safety injection pump was replaced and Unit 2 was returned to criticality on February 25, 2002.

Unit 2 continued to be operated at or near full power throughout the remainder of inspection

period.

4.

OTHER ACTIVITIES (OA)

4OA3 Event Follow-Up (93812)

.1

Potential Common Mode Failure of Auxiliary Feedwater Pumps Due To Operator

Actions

.a

Inspection Scope

The potential common mode failure of auxiliary feedwater pumps, reported by the

licensee on November 29, 2001, met the NRC Management Directive 8.3, NRC

Incident Investigation Program, threshold for a Special Inspection in that the potential

common mode failure could have led to a loss of safety function. The team performed

inspection activities as specified by the charter for the Special Inspection. The charter

was outlined in NRC memorandum from John M. Jacobson to Ronald A. Langstaff,

dated November 30, 2001. The charter directed review of the following areas:

Timeline development relating to contributors and discovery of the potential

common mode failure of the auxiliary feedwater (AFW) system due to the loss of

instrument air.

4

Adequacy of licensees operability evaluation and immediate corrective actions

for addressing impact of the loss of instrument air on AFW.

Preliminary determination of risk significance.

Apparent cause of condition resulting in potential loss of AFW upon loss of

instrument air.

Evaluation of pressurizer power operated relief valve (PORV) modifications

impact on operational capability in response to loss of feedwater.

Extent of condition of the adequacy of engineering review of instrument air

system, other air operated valves, and failure modes.

Failure of the original individual plant examination (IPE) to consider AFW

recirculation valve function.

.b

Findings

One finding involving two apparent violations was identified regarding the potential

common mode failure of the AFW pumps due to operator actions. An apparent

violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, was identified for failure to have adequate guidance in emergency operating

procedures to prevent damage to AFW pumps. The second apparent violation was of

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, and was identified for

failure to promptly identify and correct the significant condition adverse to quality relating

to potential common mode failure of AFW pumps. The finding associated with the

violations was preliminarily determined to be of high safety significance (Red).

(1)

Event Description

The licensee probabilistic risk analysis (PRA) staff identified a vulnerability associated

with AFW recirculation valves. The recirculation valves were air operated valves which

failed closed upon a loss of instrument air. Consequently, in certain transients, such as

a loss of instrument air, a loss of off-site power, a loss of service water, or a seismic

event, the flow path via the recirculation lines would be lost due to the recirculation

valves failing closed upon a loss of instrument air. Closure of the recirculation valves

could result in pump failure under low flow conditions such as when AFW flow was

throttled back to control steam generator level or mitigate RCS overcooling.

The PRA staff identified the vulnerability while updating the Point Beach PRA model for

internal events. The PRA staff originally considered the vulnerability to be a procedural

weakness associated with abnormal operating procedure (AOP) 5B, Loss of Instrument

Air. The original concern was that the steps to restore AFW pump recirculation flow did

not occur sufficiently early in the procedure. Condition Report (CR) 01-2278 was

initiated on July 6, 2001, to document the concern. The PRA staff continued

discussions with operations personnel over the next several months with regards to the

vulnerability. In November 2001, the PRA staff completed their internal events modeling

and determined that the vulnerability resulted in a substantial increase in risk. On

5

November 28, 2001, the PRA staff, engineering personnel, and operations personnel

met to discuss the significance of the vulnerability and potential courses of action. On

November 29, 2001, operations personnel concluded that temporary information tags

and operator briefings were necessary to address the vulnerability. CR 01-3595 was

initiated to document the increased risk and to address the vulnerability. The NRC was

also formally notified (Event Notification 38525) on November 29, 2001. The issue was

subsequently reported by Licensee Event Report (LER) 266/2001-005-00, submitted on

January 28, 2002.

(2)

System Description

Point Beach Nuclear Plant is a two unit site. Each unit has a turbine driven AFW pump

(pumps 1P29 and 2P29) which can supply water to both steam generators. Additionally,

the plant has two motor driven AFW pumps (pumps P39A and P39B) each of which can

be aligned to a steam generator in each unit. The recirculation valves for both the

turbine driven and motor driven pumps would open for the initial 45 seconds after pump

start and would open on low flow conditions. However, the recirculation valves were air

operated valves which failed closed upon a loss of instrument air. The control room had

valve position indication for the recirculation valves, flow indication to individual steam

generators, and flow indication to the steam generators from each pump. However, the

flow element for providing flow indication for each pump was downstream of where the

recirculation line branched off from the discharge line. Consequently, the flow indication

for each pump would not indicate recirculation line flow.

The AFW recirculation lines were installed, as part of original construction, to ensure the

pump would have a flow path to prevent dead-heading the pump, which would damage

the pump. Discussions with licensee engineering staff indicated that a pump could be

damaged within minutes under insufficient flow conditions due to lack of cooling. The

initial lines installed included an orifice that allowed a 30 gallons per minute (gpm) flow

rate. This flow rate was determined by the pump vendor, Byron Jackson, to be sufficient

to prevent pump damage based on pump heat-up when on recirculation flow. The

recirculation lines were subsequently modified in 1988, in response to Bulletin 88-04,

Potential Safety-Related Pump Loss, to accommodate a greater recirculation flow rate

and protect the pump from low flow instabilities.

(3)

Procedural Guidance

Emergency Operating Procedure (EOP)-0.1, Reactor Trip Response, directed

operators to control feedwater flow early in the procedure. Procedure EOP-0.1 was the

procedure which operators would use for most transients. Response not obtained

(RNO) column step 1.c of the procedure directed operators to reduce feed flow if reactor

coolant system (RCS) temperatures were less than 547 degrees () Fahrenheit (F) and

trending lower. Step 4.b directed operators to control feed flow to maintain steam

generator levels between 29 percent and 69 percent. RNO step 4.b directed operators

to stop feed flow to intact steam generators if level continued to rise. If instrument air

had been lost, damage would occur to the AFW pumps by these operator actions to

control feedflow due to the low flow conditions created. The team noted that procedure

OM 4.3.1, AOP and EOP Writers Guide, step 5.4.2 stated, A caution is used to

present information regarding potential hazards to personnel or equipment associated

6

with the subsequent step(s). The emergency operating procedures steps did not

provide any such cautions prior to November 30, 2001.

Portions of the EOP-0.1 steps one and four are illustrated below:

STEP

ACTION/EXPECTED RESPONSE

RESPONSE NOT OBTAINED

1

Verify RCS Temperature Control:

Perform the following:

a. Check RCS wide range cold leg

temperatures:

LESS THAN OR EQUAL TO

547 F

AND

STABLE

1. IF RCS cold leg temperature less

than 547 F AND RCS

temperatures are trending lower,

THEN stabilize RCS temperature

as follows:

a) Stop dumping steam.

b) Ensure S/G blowdown

isolations - SHUT

c) IF cooldown continues, THEN

control feed flow:

1) Reduce total feed flow.

2) Maintain total feed flow

greater than or equal to

200 gpm until level greater

than 29 percent in at least

one S/G.

STEP

ACTION/EXPECTED RESPONSE

RESPONSE NOT OBTAINED

4

Stabilize S/G Levels:

a. Check S/G/ levels - GREATER

THAN 29 percent

a. Maintain total feedflow greater

than 200 gpm until level greater

than 29 percent in at least one

S/G

b. Control feed flow to maintain

S/G levels between 29 percent

and 65 percent

b. IF level in intact S/G continues to

rise, THEN stop feed flow to that

S/G.

Based on discussions with licensee engineering staff, the team determined that the time

that the AFW recirculation valves would fail closed due to loss of instrument air could

vary. The engineering staff had determined that the recirculation valves would begin to

drift shut when instrument air header pressure was reduced to 40 pounds per square

inch gauge (psig) and would be fully closed at 25 psig. The instrument air header

pressure was nominally maintained at 100 psig with some variation due to cycling of air

compressors. Based on observations of instrument air header pressure drop between

cycling of air compressors, the engineering staff determined that the instrument air head

pressure would drop approximately 13.5 pounds per square inch in one minute under

normal loads. The engineering staff estimated that the AFW recirculation valves would

7

begin to drift shut approximately six to eight minutes after loss of all air compressors with

complete valve closure one to two minutes thereafter. A loss of instrument air due to a

leak in an airline versus a loss of air compressors would result in different bleed down

rates, depending on the size of the break. Additionally, the instrument air bleed down

rate could be faster due to greater demands on the instrument air system in response to

the transient.

Based on discussions with operating licensee personnel, the preferred method for

controlling AFW flow was by throttling or closing the AFW flow control valves (for the

motor driven AFW pumps) or discharge valves (for the turbine driven AFW pumps)

rather than securing the pumps. The team noted that Section 14.1.12, Loss of All AC

Power to the Station Auxiliaries, of the original Final Facility Description and Safety

Analysis Report (FFDSAR), stated, The reactor operator in the control room can

monitor the steam generator water level and control the feedwater flow with remote

operated AFW control valves. The FFDSAR did not discuss securing AFW pumps as a

means to control steam generator levels. Additionally, the team noted that in some loss

of instrument air scenarios (e.g., those involving RCS overcooling), the recirculation

valves could remain open at the time that operators throttle or close flow control and

discharge valves due to remaining air header pressure. However, the recirculation

valves would subsequently close due to decreasing air pressure. Consequently, the

valves could reposition at a time when an operators attention would not be directly

focused on the AFW pumps.

Operating experience demonstrated that operators would drastically reduce AFW flow

within several minutes of pump start due to RCS overcooling under some transient

conditions. For example, on June 27, 2001, the Unit 2 reactor was manually tripped due

to low and decreasing water level in the Unit 2 circulating water pump bay (reported in

LER 05000301/2001-002-00). Due to subsequent low steam generator water levels, the

Unit 2 turbine driven AFW pump and both motor driven AFW pumps initiated and began

feeding the Unit 2 steam generators. One steam generator in a unit nominally requires

200 gpm feedwater flow for decay heat removal. However, with three AFW pumps

running, approximately 800 gpm of feedwater flow - approximately four times the

required flow, was provided to the Unit 2 steam generators. Consequently, the reactor

coolant system was cooled down at an excessive rate. Approximately three minutes

after the reactor was tripped, operators closed either the flow control valves or the

discharge valves to stop flow from the motor driven AFW pumps. Approximately four

minutes after the reactor was tripped, operators closed the discharge valves from the

Unit 2 turbine driven AFW pump stopping all AFW flow to the steam generators. The

AFW pumps were not secured until approximately eight minutes after the reactor was

tripped when feed flow using main feedwater was partially restored. In this particular

event, the AFW recirculation valves were functional because instrument air had not been

lost. However, had instrument air not been available, as would happen in transients

such as loss of instrument air, loss of off-site power, and loss of service water events, all

AFW pumps could have been damaged.

Procedure AOP-5B, Loss of Instrument Air, provided operators guidance for loss of

instrument air. However, the team noted that, during these transients, operators would

typically be using emergency operating procedures, such as EOP-0.1, in their initial

response to a transient. After plant conditions stabilized, abnormal operating

8

procedures, such as AOP-5B, would be used to restore equipment. The team reviewed

procedure AOP-5B and determined that procedural steps were provided to secure open

the AFW pump recirculation valves. However, guidance to secure open the valves did

not appear until step 1 of Attachment R, Auxiliary Feed, located on page 36 of the

procedure. Operators were directed to Attachment R by step 26 (located on page 14) of

the procedure. Step 26 simply directed operators to check plant systems status per

attachments A through Z. Consequently, although procedure AOP-5B had steps which

addressed the recirculation valves, the team determined that operators would likely

damage all AFW pumps by following the emergency operating procedures given the

transient timelines described above.

(4)

Regulatory Issue Associated With Procedure Guidance

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

requires, in part, that activities affecting quality be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances. As of

November 29, 2001, procedures EOP-0.1 Unit 1, Reactor Trip Response, Revision 24,

and EOP-0.1 Unit 2, Reactor Trip Response, Revision 23, addressing activities

affecting quality, were not of a type appropriate to the circumstances. Specifically, the

procedures did not provide adequate guidance to operators regarding the potential to

damage AFW pumps while controlling AFW flow upon low instrument air header

pressure, which would cause the recirculation valves to fail closed. Because the

procedures did not include instructions to ensure the recirculation valves were open, the

AFW pumps could be damaged under low flow conditions such as when the flow is

throttled back to control steam generator level or to mitigate RCS overcooling. This

issue is considered an apparent violation (AV 50-266/01-17-01; 50-301/01-17-01).

(5)

Operator Training

The team reviewed licensed operator training lesson plans and simulator scenarios for

training conducted prior to November 29, 2001, and interviewed licensed reactor

operators and senior reactor operators to evaluate the emphasis placed on the effect of

loss of instrument air on AFW operability prior to November 29, 2001. The team

determined:

Operators were trained on and knowledgeable of the fail-safe position of air

operated valves including the AFW recirculation valves. No emphasis, however,

was placed on the consequence of the fail-closed AFW recirculation valves.

Lesson Plan 2672, Instrument Air and Service Water Review, outlined training

on the loss of instrument air PRA initiating event. The outline addressed the loss

of instrument air effect on secondary cooling. The lesson plan stated that the

turbine-driven AFW pump would be available for feeding the steam generator -

loss of instrument air had no effect and that the pressure control valves for the

motor-driven AFW pumps fail open upon a loss of pneumatic supply providing a

flow path from the motor-driven AFW pumps to the steam generators. The team

noted that the training only addressed the forward flow aspect of AFW to feed

the steam generators. The training did not address the consequences of the

fail-closed recirculation valves causing pump damage.

9

No simulator training scenario, including loss of offsite power and loss of

instrument air, had included the failure of an AFW pump due to loss of

recirculation flow. The licensee's training staff informed the team that the

simulator, as modeled, would not fail an AFW pump due to low flow conditions

as would likely occur in the plant.

(6)

Operability Evaluation

The team reviewed the licensee's initial operability determination screen completed by a

senior reactor operator on November 29, 2001. The documented basis for system

operability was satisfactory completion of required surveillance testing. The team noted

that the operability determination screen did not address the potential simultaneous

failure of all AFW pumps due to loss of instrument air and procedurally directed operator

actions (the specific issue identified by the CR). The site resident inspectors engaged

licensee management (duty shift supervisor and operations manager) on the adequacy

of the operability determination screen. Licensee management assured the resident

inspectors that extensive discussions of system operability were conducted involving

both operations and engineering and the operability determination was adequate. After

questions by the resident inspectors, the licensee initiated a formal engineering

operability determination on November 30, 2001. The team reviewed Revision 1 of the

formal engineering operability determination. The operability determination concluded

that the AFW system was operable but nonconforming and specified necessary

procedural revisions.

(7)

Licensee Corrective Actions

The licensee revised procedures EOP 0, Reactor Trip or Safety Injection, and

EOP 0.1, Reactor Trip Response, on November 30, 2001, to provide additional

guidance to operators. The foldout pages for both procedures were revised to state:

IF any AFW pump mini-recirc valve fails shut, THEN maintain minimum

flow or stop the affected AFW pump as necessary to control S/G levels.

 P-38A minimum flow - GREATER THAN 50 GPM

 P-38B minimum flow - GREATER THAN 50 GPM

 P-29 minimum flow - GREATER THAN 75 GPM

The above guidance addressed overfilling of steam generators which would, generally,

take longer than 10 minutes after the transient initiated. Consequently, under such

circumstances, had instrument air failed, it would have likely bled down to the point of

failing the recirculation valves shut before operators would have taken actions to

drastically control AFW flow. As such, the operators would have had the opportunity,

when controlling AFW flow, to observe that the recirculation valves had failed shut.

The licensee PRA staff subsequently identified that operator action to control AFW flow

could be required much earlier in a transient due to RCS overcooling before the

10

recirculation valves would shut due to a loss of instrument air. In response to this issue,

the licensee revised the foldout page for procedures ECA-0.0, Loss of all AC Power,

EOP 0, and EOP 0.1, on December 20, 2001, to state:

IF any AFW pump mini-recirc valve fails shut OR annunciator C01 A 1-9,

INSTRUMENT AIR HEADER PRESSURE LOW in alarm, THEN monitor

and maintain minimum AFW flow or stop the affected AFW pump as

necessary to control S/G levels.

 P-38A minimum flow - GREATER THAN 50 GPM

 P-38B minimum flow - GREATER THAN 50 GPM

 P-29 minimum flow - GREATER THAN 75 GPM

The team reviewed an operations notebook entry, dated December 27, 2001, and

determined that operations staff had also changed the annunciator for low instrument air

header pressure to a green color. The change was made to make the annunciator tile

stand out if a large number of alarms are received at one time. The majority of

annunciator tiles were the color white.

(8)

Failures to Identify Significant Condition Adverse to Quality

The team identified a number of opportunities which the licensee had prior to 2001 to

identify that the failure mode of the AFW recirculation valves conflicted with operating

practice. The specific instances were as follows:

1981

In Generic Letter (GL) 81-14, Seismic Qualifications for Auxiliary Feedwater

Systems, the NRC requested that the licensee perform a walk-down of the non-

seismically qualified portions of their AFW systems to identify apparent and

practically correctable deficiencies that may exist. The GL specifically identified

instrument air for AFW control valves as a potential issue. In Attachment 1,

Section IV, of their response, dated May 4, 1982, the licensee documented that

the AFW recirculation valves are now normally open and fail close. The

licensee did not address the impact that the valves failing closed could have on

the system.

1988

GL 88-14, Instrument Air Supply System Problems Affecting Safety-Related

Equipment, requested that licensees perform a design verification of the entire

instrument air system including an analysis of current air operated component

failure positions to verify that they were correct for assuring required safety

functions. The licensees response, dated February 20, 1989, stated under

action item 2 that Abnormal Operating Procedure AOP-5B, Loss of Instrument

Air, provided operators with a listing of component failure positions due to loss

of instrument air and the actions that might be necessary for various systems

and/or components. The licensee failed to recognize that the emergency

operating procedures did not include appropriate guidance.

1989

In their April 17, 1989, submittal to the NRC in response to 10 CFR 50.63, Loss

of All Alternating Current, (i.e., the station blackout rule), the licensee stated that

no air-operated valves are required to operate to cope with a station blackout for

one hour.

11

1991

The original PRA performed in response to GL 88-20, Individual Plant

Examination for Severe Accident Vulnerabilities, did not model the recirculation

valves failing closed upon loss of instrument air. Consequently, the interaction

between the instrument air system and the AFW system was not fully evaluated.

1994

The design basis document (DBD) for the AFW system, DBD-01 dated April

1994, stated that recirculation valves had a safety function to open and remain

open. However, the identified safety function for the valves to open was not

reconciled with the valves failure mode to fail closed upon a loss of instrument

air.

1997

In March 1997, the licensee identified an AFW system failure mode due to

instrument air (reported by LER 97-014-00). Specifically, the flow control valves

for the motor driven AFW pumps were air operated valves which failed open. In

certain scenarios, such as a main steam line break coincident with a loss of

instrument air, the motor driven AFW pumps could be in a run-out condition and

trip the circuit breakers for the pumps. As a result of identifying this vulnerability,

the licensee installed nitrogen back-up for the motor driven pump flow control

valves. However, the licensee did not adequately review the function of other air

operated valves in the AFW system such as the recirculation valves.

1997

In October 1997, a contractor working on the revision of the licensees inservice

testing (IST) program identified the discrepancy between the IST background

document and the AFW system DBD for the safety function of the valves in the

recirculation line. The IST background document stated the check valves did not

have a safety function to open since there was always adequate flow to the

steam generator such that the recirculation flow path was not needed to protect

the pump. The AFW system DBD stated that the recirculation valves, and,

hence, the recirculation lines, did have a safety function to open to protect the

pumps. The issue was documented on CR 97-3363 and investigated. In their

investigation, the licensee focused on ensuring that the AFW system would

provide adequate flow to the steam generators. For the turbine-driven pumps,

the valve lineup was such that there was normally a flow path to the generator.

The only power-operated valves in the line were motor-operated valves (MOVs)

to each steam generator that were normally in the throttled position. For the

motor-driven pumps, although there were normally closed valves (one control

valve and an MOV to each steam generator) in the discharge path, these valves

received an open signal on pump start to provide an adequate flow path. The

dead-heading of the motor-driven pump could occur if the control valve or MOV

failed to open. Based on single failure criteria, this type of failure would only

affect one of the two motor-driven pumps. Based on this evaluation, the licensee

deleted the open safety-function of the recirculation valves from DBD-1.

However, the licensee failed to address operator actions which could be taken to

control AFW flow to prevent overcooling of the RCS or overfilling the steam

generators. As such, the licensee failed to identify that multiple AFW pumps

(both turbine driven and motor driven) could be damaged by the failure mode of

the AFW recirculation valves.

12

(9)

Regulatory Issue Associated With Failures to Identify Significant Condition Adverse to

Quality

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that

measures be established to assure that conditions adverse to quality are promptly

identified and corrected. In the case of significant conditions adverse to quality, the

measures shall assure that the cause of the condition is determined and corrective

actions taken to preclude repetition. As of November 2001, the licensee failed to identify

that the AFW system was not capable of performing its safety function under certain

conditions. Specifically, all AFW pumps would be subject to a common mode failure

involving dead-heading of AFW pumps following a loss of instrument air, loss of offsite

power, loss of service water, or a seismic event due to the closure of the recirculation

valves upon loss of the non-safety grade, non-seismically qualified instrument air system

and prescribed operation actions to control feedwater flow in response to transient

conditions. On seven occasions between 1981 and 1997, the licensee was made aware

of the susceptibility of the AFW system to this type of vulnerability, but the licensee failed

to identify this significant condition adverse to quality. This issue is considered an

apparent violation (AV 50-266/01-17-02; 50-301/01-17-02).

(10) Pressurizer PORV Impact on Operational Capability

The pressurizer PORVs were air operated valves which were provided with a backup

nitrogen supply. However, since 1979, the back-up nitrogen supply has been isolated,

by procedure, during power operation. A containment entry was required to restore the

back-up nitrogen supply. Consequently, upon a loss of instrument air, the PORVs would

not be available. The safety injection pumps do not provide sufficient discharge

pressure to lift the reactor coolant system safety relief valves. Although the positive

displacement charging pumps provide sufficient discharge pressure to lift and pass

coolant through the code safety relief valves, the charging pumps do not provide

sufficient flow for adequate decay heat removal. Consequently, a loss of instrument air

would result in the loss of effective feed and bleed capability. A loss of auxiliary

feedwater combined with a loss of instrument air, which would also involve a loss of

main feedwater, would result in a loss of decay heat removal capability.

(11) Extent of Condition

The team reviewed the configuration of other significant systems, such as safety

injection, to verify that the recirculation lines did not have air-operated valves which

failed closed upon of loss of instrument air. The team did not identify any other systems

in which a similar vulnerability existed.

(12) Safety Significance

The team evaluated the finding using the Phase 2 process described in Inspection

Manual Chapter 609, Appendix A, Significance Determination of Reactor Inspection

Findings for At-Power Situations. The site specific worksheets for the Point Beach

Nuclear Plant were used. These site specific worksheets had been benchmarked

against the licensees current PRA model for the plant. Based on this review, the team

determined that the most limiting scenario was loss of instrument air. The following

assumptions were made:

13

The exposure time was greater than 30 days.

The initiating event frequency was 1 x 10-3 for loss of instrument air.

No credit for any AFW was applied. The emergency operating procedures used

by operators did not provide adequate guidance to address recirculation valve

closure. Additionally, operators were not trained to specifically recognize the

potential for AFW recirculation valve closure and the consequences. The

licensees PRA staff performed informal calculations which showed overall

human error probabilities in the range of 0.3 to 0.5 (depending on the

calculational method used) for operator actions in response to steam generator

overfill. For operator response to RCS overcooling, the licensees PRA staff

assumed that operator actions would result in failure of the AFW pumps.

For loss of instrument air, feed and bleed capability using the pressurizer PORVs

was not credited because of the reliance upon instrument air.

Based on use of the Point Beach Nuclear Plant site specific worksheets for loss of

instrument air, the finding was preliminarily determined to be of high safety significance

(Red). The dominate sequences involved the loss of instrument air and the loss of

feedwater.

The team also evaluated the finding using the loss of off-site power site specific

worksheets. The assumptions used were similar to those above with the following

exceptions:

The initiating event frequency was 1 x 10-2 for loss of off-site power.

Instrument air would be initially lost upon loss of off-site power because the air

compressors would be automatically stripped from the safeguards power buses.

The initial loss of instrument air would result in damage to the AFW pumps due

to operator actions.

Credit for feed and bleed capability was applied because instrument air could be

restored by manual operators actions. The necessary operator actions were

proceduralized.

Credit for high pressure recirculation was applied because neither safety

injection nor residual heat removal was affected by the finding.

Based on use of the Point Beach Nuclear Plant site specific worksheets for loss of off-

site power, the finding was preliminarily determined to be of high safety significance

(Red). The dominate sequences involve the loss of off-site power and AFW with either

feed and bleed capability or high pressure recirculation being available.

In addition, the finding was evaluated using the loss of service water worksheets.

However, the significance due to loss of service water was not as great as the loss of

instrument air and loss of off-site power transients as described above.

14

.2

Licensee Event Reports

LER 50-266/2001-05; 50-301/2001-05 (Open): PRA assessment of AFW system

reveals procedural vulnerability related to loss of instrument air. The subject of this LER

is discussed in Section 4OA3.1 and two apparent violations were identified. This LER

will remain open pending future inspection review.

4OA6 Meeting(s)

Exit Meeting

On December 13, 2001, at the conclusion of the on-site inspection activities, the lead

inspector presented the initial findings to Mr. Reddemann and other members of

licensee management at Point Beach Nuclear Plant. On February 28, 2002, the team

presented the findings to Mr. Warner and other members of licensee management. The

licensee representatives acknowledged the findings presented. The team identified the

proprietary information reviewed during the inspection and noted that the information

would be handled accordingly. The licensee did not identify any other material reviewed

during the inspection as being proprietary.

15

KEY POINTS OF CONTACT

Licensee

J. Anderson, Manager, Production Planning

F. Cayia, Director, Kewaunee - Point Beach Site

R. Mende, Director, Kewaunee - Point Beach Engineering

M. Reddemann, Vice President - Engineering, Nuclear Management Company

J. Strharsky, Assistant Manager, Operations

M. Warner, Vice President, Kewaunee - Point Beach Site

T. Webb, Manager, Kewaunee - Point Beach Regulatory Affairs

NRC

J. Grobe, Director, Division of Reactor Safety, Region III

J. Jacobson, Chief, Mechanical Engineering Branch, Region III

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-266/01-05

LER

PRA Assessment of Auxiliary Feedwater System Reveals

50-302/01-05

Procedural Vulnerability Related to Loss of Instrument Air

50-266/01-17-01

AV

Potential Common Mode Failure of Auxiliary Feedwater Pumps

50-301/01-17-01

Due to Inadequate Procedural Guidance

50-266/01-17-02

AV

Failure to Identify and Correct Problem Associated With

50-301/01-17-02

Potential Common Mode Failure of Auxiliary Feedwater Pumps

16

LIST OF ACRONYMS USED



Degrees

AFW

Auxiliary Feedwater

AOP

Abnormal Operating Procedure

AV

Apparent Violation

CFR

Code of Federal Regulations

CR

Condition Report

DBD

Design Basis Document

DRP

Division of Reactor Projects

DRS

Division of Reactor Safety

EA

Enforcement Action

EOP

Emergency Operating Procedure

F

Fahrenheit

FFDSAR

Final Facility Description and Safety Analysis Report

GL

Generic Letter

GPM

Gallons Per Minute

IPE

Individual Plant Examination

IR

Inspection Report

IST

In Service Testing

LER

Licensee Event Report

LLC

Limited Liability Company

MOV

Motor Operated Valve

NMC

Nuclear Management Company, LLC

NRC

U.S. Nuclear Regulatory Commission

PORV

Power Operated Relief Valve

PPCS

Plant Process Computer System

PRA

Probabilistic Risk Analysis

PSIG

Pounds per Square Inch Gauge

RCS

Reactor Coolant System

RNO

Response Not Obtained

SDP

Significance Determination Process

S/G

Steam Generator

17

LIST OF DOCUMENTS REVIEWED

The following is a list of licensee documents reviewed during the inspection, including

documents prepared by others for the licensee. Inclusion on this list does not imply that NRC

team reviewed the documents in their entirety, but, rather that selected sections or portions of

the documents were evaluated as part of the overall inspection effort.

Number

Title

Revision/Date

Procedures

AOP-5B

Loss of Instrument Air

Revision 18

AOP-10A Unit 1

Safe Shutdown - Local Control

Revision 32

CSP-H.1 Unit 1

Red

Response to Loss of Secondary Heat Sink

Revision 21

ECA-0.0 Unit 1

Loss of All AC Power

Revision 29

ECA-0.0 Unit 2

Loss of All AC Power

Revision 30

EOP-0 Unit 1

Reactor Trip or Safety Injection

Revision 35

EOP-0 Unit 2

Reactor Trip or Safety Injection

Revision 36

EOP-0.1 Unit 1

Reactor Trip Response

Revision 24

EOP-0.1 Unit 2

Reactor Trip Response

Revision 23

IT 10

Test of Electrically-Driven Auxiliary Feed Pumps

and Valves (Quarterly)

July 5, 2001

OM 4.3.1

AOP and EOP Writers Guide

Revision 3

Temporary Changes

2001-0871

EOP-0 Unit 1, Reactor Trip or Safety Injection

November 30,

2001

2001-0872

EOP-0 Unit 2, Reactor Trip or Safety Injection

November 30,

2001

2001-0873

EOP-0.1 Unit 1, Reactor Trip Response

November 30,

2001

2001-0874

EOP-0.1 Unit 2, Reactor Trip Response

November 30,

2001

2001-0911

ARP C01 A 1-9, Instrument Air Header Pressure

Low

December 20,

2001

18

2001-0912

ECA-0.0 Unit 1, Loss of All AC Power

December 20,

2001

2001-0913

EOP-0.1 Unit 2, Reactor Trip Response

December 20,

2001

2001-0914

EOP-0 Unit 2, Reactor Trip or Safety Injection

December 20,

2001

2001-0915

EOP-0 Unit 1, Reactor Trip or Safety Injection

December 20,

2001

2001-0916

EOP-0.1 Unit 1, Reactor Trip Response

December 20,

2001

2001-0917

ECA-0.0 Unit 1, Loss of All AC Power

December 20,

2001

Design Basis Documents

DBD-01

Auxiliary Feedwater System

Revision 0

DBD-01

Auxiliary Feedwater System

Revision 1

DBD-06

Instrument & Service Air

Revision 2

DBD-T-46

Station Blackout

Revision 0

Updated Final Safety Analysis Report Sections

4.2

RCS System Design and Operation

June 2000

8.8

Diesel Generator (DG) System

June 2000

9.7

Instrument Air (IA) / Service Air (SA)

June 2000

10.2

Auxiliary Feedwater System (AF)

June 2000

Calculations

N-91-007

Steam Generator Inventories 5 Minutes After an

Earthquake

November 7, 1991

N-91-031

1 & 2 P29 Mini-Recirc Line System

Characteristics

March 19, 1991

N-91-032

Comparison of Nominal Flow Rates from 2P-29

to 2HX-1A and 2HX-1B with the Recirc Line

Open

March 19, 1991

19

Correspondence

NRC Generic Letter No. 81-14, Point Beach

Nuclear Plant, Units 1 and 2

July 16, 1981

Additional Response to NRC Generic Letter 81-14, Point Beach Nuclear Plant, Units 1 and 2

May 4, 1982

Seismic Qualification of the Auxiliary Feedwater

System, Point Beach Nuclear Plant, Units 1 and

2

December 15,

1982

Final Resolution of Generic Letter 81-14,

Seismic Qualification of Auxiliary Feedwater

System, Point Beach Nuclear Plant, Units 1 and

2

April 26, 1985

VPNPD-88-335

Response to NRC Bulletin 88-04

June 28, 1988

VPNPD-88-090

NRC-89-021

Response to Generic Letter No. 88-14,

Instrument Air System Problems Affecting

Safety-Related Equipment, Point Beach Nuclear

Plant, Units 1 and 2

February 20, 1989

VPNPD-89-216

NRC-89-043

Response to 10 CFR 50.63, Tac. Nos. 68586

and 68587, Loss of All Alternating Current

Power, Point Beach Nuclear Plant, Units 1 and 2

April 17, 1989

Response to NRC Bulletin 88-04

May 26, 1989

Minimum Flow Analysis

August 7, 1989

VPNPD-95-056

Generic Letter 88-20, Supplement 4, Summary

Report on Individual Plant Examination of

External Events for Severe Accident

Vulnerabilities

June 30, 1995

NPL 97-0186

Licensee Event Report 97-014-00, Auxiliary

Feedwater System Inoperability Due to Loss of

Instrument Air

April 18, 1997

NRC 2001-057

Licensee Event Report 301/2001-002-00,

Manual Reactor Trip Due to Decreasing Water

Level in Circulating Water System

August 17, 2001

NRC Memorandum From John M. Jacobson to

Ronald A. Langstaff, Special Inspection Charter

for Point Beach Potential Common Mode Failure

of Auxiliary Feedwater

November 30,

2001

20

NRC 2002-0012

Licensee Event Report 266/2001-005-00,

PRA Assessment of Auxiliary Feedwater System

Reveals Procedural Vulnerability Related to Loss

of Instrument Air

January 28, 2002

Condition Reports

97-0930

Questions and Concerns About the use of

Operator Action to Control AFW Flow

March 20, 1997

97-3363

IST Program Design Basis for AFW Minimum

Flow Recirculation Valves

October 15, 1997

98-2575

P-38A AFW Pump Recirc Valve Found Failed

Shut

June 29, 1998

QCR 99-0115

Code Testing Conflict with the Aux Feedwater

Mini-Flow Recirc Check Valves

May 24, 1999

99-3091

Aux Pump Recirc Line Leakage Acceptance

Criteria Questioned

December 3, 1999

01-2278

Auxiliary Feedwater Probabilistic Risk

Assessment (PRA) Model for Loss of Instrument

Air

July 6, 2001

01-3595

Potential common mode failure for all auxiliary

feed pumps under certain initiating events.

November 29,

2001

01-3641

Modifications that had potential to identify

concern

December 4, 2001

01-3654

The development and revision of DBD-01

appears to have been a missed opportunity to

identify a design weakness in the AFW system.

December 6, 2001

Evaluations

RCE 98-148

P-38A AFW Pump Recirc Valve Found Failed

Shut

January 29, 1999

Drawings

M-201, sheet 1

Main & Reheat Steam System

January 20, 2001

M-209, sheet 1

Service Air

May 12, 2001

M-209, sheet 2

Service Air

November 18,

2000

M-209, sheet 3

Instrument Air

November 18,

2000

21

M-209, sheet 4

Instrument Air

October 25, 2001

M-209, sheet 11

Instrument Air

January 19, 1998

M-217, sheet 1

Auxiliary Feedwater System

September 29,

2001

M-217, sheet 2

Auxiliary Feedwater System

February 3, 2001

M-2201, sheet 1

Main & Reheat Steam System

January 20, 2001

Modifications

97-038*A

AFW Motor Driven Pump Discharge Control

Valve Modification

March 24, 1998

97-038*B

AFW Discharge Valve AF-04012 & AF-04019

Modification

June 26, 1998

88-099, Common

AFW Recirc Line Modification

March 27, 1991

88-099*A,

Common

AFW Recirc Line Modification

February 14, 1992

88-099*C,

Common

AFW Recirc Line Modification

February 14, 1992

88-099*D,

Common

AFW Recirc Line Modification

July 1, 1992

Miscellaneous Documents

LP3178

Auxiliary Feedwater System

June 15, 2001

Mod Request IC-

274

Making AFW Recirc Valves Normally Open

Procedure Change

OP-1A,Major

Cold Shutdown to Low Power Operation

December 26,

1978

Procedure Change

OP-1A,Major

Cold Shutdown to Low Power Operation

July 26, 1979

IST Background

Valve Data Sheet

Auxiliary Feedwater

May 17, 2000

97-201

Setpoint Change to the Auxiliary Feedwater By-

pass Control Valves Time Delay Relay Setpoints

(1/2-NC005, 62-P38A and 62-P38B)

December 4, 1997

Action Items Associated with GL 88-14

September 17,

1991

Final Facility Description and Safety Analysis

Report

Original