IR 05000457/1988012

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Safety Insp Rept 50-457/88-12 on 880314-25.Violation Noted. Major Areas Inspected:Event in Which 2B Safety Injection Pump Found Incapable of Performing Intended Function When Pump Manual Discharge Valve Found Locked Shut
ML20151N459
Person / Time
Site: Braidwood Constellation icon.png
Issue date: 04/12/1988
From: Hinds J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20151N415 List:
References
50-457-88-12, NUDOCS 8804250305
Download: ML20151N459 (4)


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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Report No. 50-457/88012(DRP)

Docket No. 50-457 License No. NPF-75 Licensee: Commonwealth Edison ~ Company Post Office Box 767 Chicago, IL 60690 Facility Name: Braidwood Station, Unit 2 Inspection At: Braidwood Site, Braidwood, Illinois Inspection Conducted: March 14 through March 25, 1988 Inspectors: T. M. Tongue

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T. E. Taylor

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Approved B : M. Hinds, ief 4.52 BB eactor Projects Section 1A Date Inspection Summary Inspection from March 14 through March 25, 1988 (Report No. 50-457/88012(ORP))

Areas Inspected: Special safety inspection conducted by the resident inspectors concerning an event in which the 28 Safety Injection pump was found incapable o; performing its intended function when its manual discharge valve (25189218) was found locked shu Results: One violation (failure to meet a Technical Specification requirement)

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I 8804250305 880415 PDR l

ADOCK 05000457 i O DCD j

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DETAILS

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1. Persons Contacted CommonwealthEdisonCompany(CECM

  • R. E. Querio, Station Manager K. Kofron, Production Superintendent D.- E. O'Brien, Administrative Superintendent
  • G. Masters, Operations Assistant Superintendent
  • P. Barnes, Regulatory Assurance Supervisor
  • T. Simpkin, Regulatory Assurance
  • P. Holland, Regulatory Assurance J. Kuchenbecker, Shif t Control Room Engineer M. Hess, Nuclear Station Operator L. Ganci, Equipment Attendant B. Kempen, Equipment Attendant
  • Denotes those attending the exit interview conducted on March 25, 198 . Purpose This inspection was conducted to review the circumstances related to the event in which the Unit 2 "B" Safety Ir.jection (SI) pump manual discharge valve (2SI89218) was found locked shut, thus rendering the 28 SI pump inoperable from 7:47 p.m. on March 5 to 5:00 p.m. on March 13, 198 . Event Description and Chronology On March 13, 1988, it 4:50 p.m., the licensee identified that the 2B Safety Injection (SI) pump manual discharge valve (2518921B) was locked shut, thus rendering the 28 SI pump incapable of performing its intended function. The valve was promptly unlocked, opened, and relocked as required. The counterpart valve on the 2A SI pump was verified to be in its proper locked open positio The mispositioned valve was identified by a "B" equipment attendant (EA)

who was in the 28 SI pump room for routine rounds. There is no position indication for that valve on the main control board in the main control room; however, there is a position microswitch that provides a signal to the main compute An immediate review of the Sequence of Events Recorder log showed that the valve was shut prior to 7:30 a.m. on March 9, 198 In addition, an initial review of records showert that the 2B SI pump had been run for five minutes on February 8, 1988, starting at 10:27 Further investigation by the licensee revealed that the key for the lock on that valve had been checked out on March 5, 198 Follow-up interviws with the nuclear station operators (NS0s) and EAs involved found that the valve was unlocked and left open for maintenance

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personnel on March 5, 198 The maintenance personnel were attempting to tighten a leaky pipe flange very close to the valve, and the locking chain interfered with access to the flange studs and nut The center desk NSO stated that he requested the "B" EA to make an entry in the Locked Equipment Log; however, this log had been deleted several months previous to the event. In addition, there was no entry made in the Abnormal Position Log by control room personne Upon completion of the repair on March 5, 1988, maintenance personnel were contacted by the Shift Control Room Engineer (SCRE) to verify that the work was complete. The SCRE then directed the center desk NSO to have the valve relocked. A different "B" EA (who had about two months of experience on the job) was assigned to relock the valve by the center desk NSO. The "B" EA interpreted his instructions to mean that he should shut and relock the valve, and he did s In addition, he did not question the ordei' that was having him make an ECCS component inoperable by shutting the valve.

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Later interviews showed that the "B" EA was instructed to "lock the valve tight," or "lock it snug," which he interpreted to mean "shut the valve tight and lock it." The "B" EA told the Senior Resident Inspector (SRI)

that he wasn't sure if he confused the oroer or whether the NSO gave him erroneous direction The shut valve isolated the discharge flow path for the 2B SI pump for a period of over seven day . , Evaluation of the Event The result of this event was having the 28 SI pump inoperable or incapable of performing its intended safety function (mitigating the i,

consequences of an intermediate size loss of coolant accident) for a period of about eight days. The 28 SI pump is part of the "B" Emergency

, Core Cooling System (ECCS) train (subsystem). The other components (Charging pump, Residual Heat Removal pump, Residual Heat Removal heat

exchanger, and the flow path) of the "B" ECCS train and the entire "A" ECCS train were available (operable).

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I While the pump was inoperable, the Unit 2 reactor was at normal pressure

] (2235 psig) and temperature (Tavg=557'F) and in either Mode 2 or Mode The unit had attained initial criticality on March 8, 1988, and was involved in low power physics testing (nominally several orders of magnitude less than 1% power); therefore, the source term was extremely low as compared to that of the design basis accident analysi This event is considered a viglation of Technical Specification 3.5.2,

"ECCS SUBSYSTEMS - Tavg > 350 F," which requires that two independent ECCS subsystems (including the SI pump) be operable in Modes 1, 2, and 3, with an action statement requiring restoration within seven days or proceeding to hot standby (Mode 3) within six hours and hot shutdown (Mode 4) within the following six hour (50-457/88012-01(ORP))

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This appears to be the first event of this type at Braidwood and is not an example of a multiple occurrenc . Licensee Corrective Actions The licensee's immediate action was to unlock, open, and relock the valve and to verify that the opposite train did not have a similar proble This action was appropriat The licensee immediately commenced an investigation to determine the cause and took steps for long term corrective action to prevent recurrence. These actions included reaffirming and improving the communication skills of all operations personne Additional actions takel or planned are to re-emphasize the use of the Abnormal Positior. Log with shift personnel and to make use of the INPO

"Human Performance Evaluation System" for additional improvemen I Each of these completed and planned actions were reviewed and confirmed to be appropriate by the inspecto . Conclusion In summary, this is a violation of Technical Specification 3.5.2 for failure to have the required ECCS equipment (2B SI pump) operable for over seven days. Other ECCS equipment, including the opposite train,

was available during that time. The reactor power history was signi- i ficantly low such that decay heat for accident considerations was negligible, and this appears to be the first event of this type at '

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Braidwood.

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The cause is attributed to the lack of formality and quality of

communications, and a contributing cause was the improper use of logs (Abnormal Position Log). Training for prevention of recurrence and implementation of corrections is a concer , Exit Interview (30703) j i' The inspector met with the licensee representatives denoted in Paragraph 1 at the conclusion of the inspection on March 25, 1988. The inspector summarized the scope and results of the inspection and l'

discussed the likely content of this inspection repor The licensee acknowledged the information and did not indicate that any of the information disclosed during the inspection could be considered proprietary in natur .

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