IR 05000346/2006006

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IR 05000346-06-006(DRS); 01/23/2006 - 02/10/2006 and 03/02/2006; Davis-Besse Nuclear Power Station; Evaluation of Changes, Tests, or Experiments (10 CFR 50.59) and Permanent Plant Modifications
ML060810332
Person / Time
Site: Davis Besse 
Issue date: 03/17/2006
From: Dave Hills
NRC/RGN-III/DRS/EB1
To: Bezilla M
FirstEnergy Nuclear Operating Co
References
+kBR1SISP20060509 IR-06-006
Download: ML060810332 (25)


Text

March 17, 2006

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION, NRC EVALUATION OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000346/2006006(DRS)

Dear Mr. Bezilla:

On February 10, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed a combined baseline inspection of the Evaluation of Changes, Tests, or Experiments and Permanent Plant Modifications at the Davis-Besse Nuclear Power Station. The enclosed report documents the results of the inspection, which were discussed and others of your staff at the completion of the inspection on February 10, 2006 and March 2, 2006.

The inspectors examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of the inspection, three NRC identified findings of very low safety significance were identified, which involved violations of NRC requirements.

However, because these violations were of very low safety significance and because they were entered into your corrective action program, the NRC is treating the issues as Non-Cited Violations in accordance with Section VI.A.1 of the NRCs Enforcement Policy.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Davis-Besse Nuclear Power Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely, David E. Hills, Chief Engineering Branch 1 Division of Reactor Safety

Enclosure:

Inspection Report 05000346/2006006(DRS)

Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is a

REGION III==

Docket No:

50-346 License No:

Report No:

05000346/2006006(DRS)

Licensee:

Facility:

Davis-Besse Nuclear Power Plant Location:

Dates:

January 23, 2006, through February 10, 2006, and March 2, 2006 Inspectors:

R. Daley, Senior Reactor Inspector, Team Leader A. Dahbur, Reactor Inspector Approved by:

D. Hills, Chief Engineering Branch 1 Division of Reactor Safety (DRS)

Enclosure

SUMMARY OF FINDINGS

IR 05000346/2006006(DRS); 01/23/2006 - 02/10/2006 and 03/02/2006; Davis-Besse Nuclear

Power Station; Evaluation of Changes, Tests, or Experiments (10 CFR 50.59) and Permanent Plant Modifications.

The inspection covered a two week announced baseline inspection on evaluations of changes, tests, or experiments and permanent plant modifications. The inspection was conducted by two regional based engineering inspectors. Three Green Non-Cited Violations (NCV) and one Unresolved Item were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red), using Inspection Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply, may be Green, or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, that was of very low safety significance. Specifically, the flow acceptance curves used for two safety-related pumps, the number 2 High Pressure Injection (HPI) pump and the number 2 Low Pressure Injection (LPI) pump, were incorrect and non-conservative. This issue was entered into the licensees corrective action system and the licensee verified that other safety-related pumps were not similarity affected.

The issue was more than minor because it was associated with the Mitigating System cornerstone attribute of Design Control, and affected the cornerstone objective of ensuring the capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, performing required flow testing of safety related pumps with non-conservative acceptance criteria could allow the pumps to operate during an accident with less than acceptable flows. The finding screened as having very low significance (Green) using IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for the At-Power Situations, because the inspectors answered no to all five questions under the Mitigating Systems Cornerstone column of the Phase 1 worksheet. While the failure to apply conservative test acceptance criteria during flow tests for the HPI and LPI pumps could have eventually caused the pumps to be outside of their acceptable flow rates without it being detected, the licensee verified that the most recent test data for these pumps would have still been acceptable if the correct pump curves had been used. (Section 1R02.1.b.1)

Green.

The inspections identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, that was of very low safety significance, where the licensee had not evaluated and updated the plant cable ampacity calculation to determine the potential consequences of adverse effects to cabling due to higher temperatures in the Diesel Fire Pump Room and other areas in the plant. The issue was entered into the licensees corrective action program.

The finding was more than minor because it affected the mitigating system cornerstone attribute of Design Control and affected the cornerstone objective of ensuring reliability of systems that respond to initialing events to prevent undesirable consequences.

Specifically, the licensee did not account for high temperature conditions that adversely affected the ampacity of cabling supplying power to equipment important to safety. This finding was of very low safety significance, because the inspectors answered no to all five questions under the Mitigating Systems Cornerstone column of the Phase 1 worksheet. Specifically, the licensee was able to demonstrate that even though the higher temperatures decreased the ampacity margins for the effected cabling, it did not decrease the margins to the limit where the cabling would fail if called upon to provide power to equipment important to safety. (Section 1R17.1.b.1)

Green.

The inspectors identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion XI, Test Control, that was of very low safety significance. Specifically, after performing modifications to implement a new Boron Precipitation Control method for post-LOCA (Loss of Coolant Accident) operations, the licensee failed to both identify and establish testing for the flow instrumentation that the operators would use post-LOCA to ensure minimum flow for proper boron dilution. This issue was entered into the licensees corrective action system.

The issue was more than minor because if it was left uncorrected, the finding would become a more significant safety concern. Had this issue not been detected, the instrument could have fallen well out of tolerance in the future leading to inaccurate readings. During post-LOCA operations, these inaccurate readings could have caused operators to establish insufficient Boron Precipitation Control (BPC) flows. The finding screened as having very low significance (Green) using IMC 0609, Appendix A,

Significance Determination of Reactor Inspection Findings for the At-Power Situations, because the inspectors answered no to all five questions under the Mitigating Systems Cornerstone column of the Phase 1 worksheet. While the lack of calibration procedures for the flow instrumentation would have eventually caused the instrument to read inaccurately, the inspection team identified the problem early enough so that the instrument drift (as provided in the vendor instructions) would not be large enough to cause inaccuracies that would adversely affect BPC flows. (Section 1R17.1.b.2)

Licensee-Identified Violations

No findings of significance were identified.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R02 Evaluations of Changes, Tests, or Experiments

.1 Review of 10 CFR 50.59 Evaluations and Screenings

a. Inspection Scope

From January 23 through February 10, 2006, the inspectors reviewed four evaluations performed pursuant to 10 CFR 50.59. The inspectors confirmed that the evaluations were thorough and that prior NRC approval was obtained as appropriate. The team could not review the minimum sample size of five evaluations, because the licensee only performed four evaluations during the biennial sample period. The inspectors also reviewed 13 screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. In regard to the changes reviewed where no 10 CFR 50.59 evaluation was performed, the inspectors verified that the changes did not meet the threshold to require a 10 CFR 50.59 evaluation. The evaluations and screenings were chosen based on risk significance, safety significance, and complexity. The list of documents reviewed by the inspectors is included as an attachment to this report.

The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, 10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments.

b. Findings

b.1 Non-Conservative Flow Testing Acceptance Criteria for the Number 2 HPI and Number 2 LPI Pumps

Introduction:

The inspectors identified a NCV having a very low safety significance (Green) of 10 CFR Part 50, Appendix B, Criterion III, Design Control. Specifically, safety-related pump flow curves used for test acceptance criteria, which were created in the design basis calculation for the number 2 HPI pump and the number 2 LPI pump, were not correctly translated into the plant procedure used for testing. The acceptance curves used for the pumps, were incorrect and non-conservative.

Description:

At the Davis-Besse Nuclear Power Station, flow testing of the HPI and the LPI Pumps were performed quarterly. To ensure proper operation of the pumps, flow and pressure readings taken during the quarterly test were compared to curves from design basis calculations. These curves established the acceptance criteria for the quarterly flow tests.

During the inspection, the inspector identified that the acceptance curves used for two of the pumps, the number 2 HPI pump and the number 2 LPI pump, were incorrect. In the case of the number 2 HPI pump, the licensees procedure contained a degraded pump curve instead of the correct curve. In the case of the number 2 LPI pump, the procedure contained a curve for the number 2 LPI pump that was really the curve for the number 1 LPI pump. In both instances, the curves in the test procedures contained non-conservative acceptance criteria.

Because of this non-conservative acceptance pump testing criteria, the licensee initiated Condition Report (CR) 06-00219. The licensee subsequently agreed that the correct pump curves, which were created in the design basis calculation for each pump, were not correctly translated into the plant procedure containing the acceptance criteria.

Additionally, the licensee reviewed the most recent test data for these pumps and compared the results to the correct (conservative) acceptance criteria for the pumps.

This review determined that even though the curves that were used for the test were non-conservative, the pumps would have still tested satisfactory using the correct pump curves.

In addition, since two pumps were found to have non-conservative acceptance values, the licensee, as an immediate corrective action for CR 06-00219, reviewed other safety related pump procedural quarterly acceptance criteria to ensure their accuracy. The review did not identify any other non-conservative acceptance criteria.

Analysis:

The inspectors determined that this failure to translate the correct acceptance criteria from the design basis calculation to the testing procedure for the number 2 LPI and number 2 HPI pumps was a performance deficiency warranting a significance determination. The issue was more than minor because it was associated with the Mitigating System cornerstone attribute of Design Control, and affected the cornerstone objective of ensuring the capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, performing required flow testing of safety-related pumps with non-conservative acceptance criteria could allow the pumps to operate during an accident with less than acceptable flows.

The finding screened as having very low significance (Green) using IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for the At-Power Situations, because the inspectors answered no to all five questions under the Mitigating Systems Cornerstone column of the Phase 1 worksheet. While the failure to apply conservative test acceptance criteria during flow tests for the HPI and LPI pumps could have eventually caused the pumps to be outside of their acceptable flow rates without it being detected, the licensee verified that the most recent test data for these pumps would have still been acceptable if the correct pump curves had been used.

Enforcement:

10 CFR Part 50, Appendix B, Criterion III, Design Control states, in part, that measures shall be established to assure that applicable design basis are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, sometime prior to 2004 at the Davis-Besse Nuclear Power Station, the correct design basis pump curves for the number 2 HPI pump and the number 2 LPI pump were not correctly translated as acceptance criteria into the testing procedure. Because this failure to apply appropriate test control measures was determined to be of very low safety significance and because it was entered in the licensees corrective action program as CR 06-00219, this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy. (NCV 06000346/2006006-01 (DRS))

b.2 Change to Design Basis Tornado Differential Pressure Design Limit for the Auxiliary Building

Introduction:

The inspectors identified an Unresolved Item (URI) involving the adequacy of a 10 CFR 50.59 safety evaluation for Updated Safety Analysis Report (USAR)changes that the licensee had implemented. Specifically, the inspectors questioned the adequacy of the licensees basis for determining that changes to USAR Sections 3.3.2, Tornado Criteria and 3.8.1.1.1, Auxiliary Building did not require a license amendment. This issue is unresolved pending further NRC review of Davis-Besses licensing basis for tornado protection.

Description:

Davis-Besse USAR Section 3.3.2.2.1 previously referenced DEPRELLIN as the analytical method/software used to evaluate the differential pressure between the compartments for the Auxiliary Building. This section indicated that by using the DEPRELLIN computer program, the maximum differential pressure between compartments in the Auxiliary Building was 0.5 psi. Condition Report (CR) 03-01132 identified a concern regarding the tornado differential pressure analysis of the auxiliary building, in that the DEPRELLIN methodology did not consider closed doors and hatches, and modeling of these closed barriers could impact the calculated differential pressure.

Due to limitation of the DEPRELLIN software, the licensee chose to use the COMPARE computer code as an alternate method to DEPRELLIN to re-determine the maximum tornado depressurization loading. The licensee evaluated the use of the COMPARE computer code in 10 CFR 50.59 Evaluation Number 04-02210 UCN 03-058 Tornado Subcompartment Pressurization Methodology Change Permitting COMPARE Methodology. The inspectors reviewed the screening/evaluation written on April 5, 2005, and questioned the changes that were made to the USAR per USAR Change Notice (UCN)03-058. The inspectors were concerned about the adequacy of the licensees basis, as stated in the 10 CFR 50.59 screening and evaluation, for determining that changes to USAR Sections 3.3.2 Tornado Criteria and 3.8.1.1.1 Auxiliary Building did not require a licensee amendment.

Prior to the implementation of UCN 03-058, USAR Section 3.3.2 stated, in part, that the structures for the Auxiliary Building were analyzed for tornado loading using an assumed value of 1.5 psi positive differential pressure between the inside and outside with the provision of venting the structure in order to control the differential pressure to within the 1.5 psi limit. Section 3.8.1.1.1 also stated:

The Auxiliary Building has been designed with sufficient venting area in order to keep the differential pressure drop within the 1.5 psi design limit. The external walls and the roof slabs are designed to withstand the forces due to a tornado, as described in Section 3.5.1(1). This 1.9 x 10 6 cubic foot building has natural venting area on roof slabs, in the external walls, internal walls, and internal slabs.

Each floor has an adequate opening or a number of openings to allow the air flow during tornado depressurization. The pressure drop is assumed to be 3.0 psi in 3 seconds, which is quite conservative.

Using the computer program COMPARE, the licensee re-calculated that the maximum deferential pressure between subcompartments in the auxiliary building was 3.0 psi. The licensee re-evaluated the Auxiliary Building for the revised differential pressure loads due to tornado depressurization. This evaluation was documented in Calculation C-CSS-099.20-029. The calculation concluded that the auxiliary building structure is adequate for these increased loads. Based on this, the licensee revised USAR Section 3.3.2 per UCN 03-058, and indicated that the structures for the Auxiliary Building subcompartments were analyzed for tornado loading using an assumed value of 3.0 psi maximum. The UCN also deleted the above discussion from USAR Section 3.8.1.1.1.

The licensee justified the revision of these two sections in 10 CFR 50.59 Screen Number 04-02210, Revision 1, which indicated that these sections incorrectly identified the original tornado depressurization load of 1.5 psi as a design limit.

The inspectors were concerned that the licensee might have decreased a margin of a design limit (1.5 psi with venting capability) that was a basis for NRC staff acceptance of the original auxiliary building design for tornados. Additionally, the licensees new calculation for the auxiliary building was a change in methodology and was not evaluated under 10 CFR 50.59 as required.

Following identification of this issue, the licensee entered the issue into their corrective action program as Condition Reports (CRs) 06-00246 and 06-00472. This issue is unresolved pending further NRC review of Davis-Besses licensing basis for tornado protection to determine if the licensee had decreased design margin that was used by the NRC staff as a basis for acceptance of the licensees safety analysis for a tornado event. (URI 05000346/2006006-02(DRS))

1R17 Permanent Plant Modifications

.1 Review of Permanent Plant Modifications

a. Inspection Scope

From January 23 through February 10, 2006, the inspectors reviewed eight permanent plant modifications that had been installed in the plant during the last two years. The modifications were chosen based upon risk significance, safety significance, and complexity. As per inspection procedure 71111.17B, one modification was chosen that affected the barrier integrity cornerstone. The inspectors reviewed the modifications to verify that the completed design changes were in accordance with the specified design requirements and the licensing bases and to confirm that the changes did not adversely affect any systems' safety function. Design and post-modification testing aspects were verified to ensure the functionality of the modification, its associated system, and any support systems. The inspectors also verified that the modifications performed did not place the plant in an increased risk configuration.

The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an attachment to this report.

b. Findings

b.1 Failure to Consider Adverse Ampacity Effects of High Temperature Conditions in the Diesel Fire Pump Room

Introduction:

The inspectors identified a NCV having very low safety significance (Green)of 10 CFR Part 50, Appendix B Criterion III, Design Control. Specifically, the licensee had not evaluated and updated the plant cable ampacity calculation to determine the potential consequences of adverse effects to cabling due to higher ambient temperatures in the Diesel Fire Pump Room.

Description:

The licensee revised calculation 67.005, Service Water Pump Room Ventilation System Capacity, which increased the potential maximum ambient temperature in the Diesel Fire Pump room from 104 degrees F to 120 degrees F. The potential high ambient temperatures could occur when the outside temperature is at the extreme limit of 104 degrees F and the Diesel Fire Pump engine is running.

The licensee used 10 CFR 50.59 Screening Number 04-03226, Revision 1, to evaluate the effects of high ambient temperature on the diesel fire pump engine and the safety-related equipment (i.e., Motor Control Center (MCC) E12C, MCC E12D and small circuit breakers) located in the Diesel Fire Pump Room. The evaluation concluded that the operability of the diesel fire pump engine and the safety-related equipment were acceptable for an ambient room temperature of 120 degrees F. However, the licensee failed to address the effects of these heightened temperatures on the ampacity of electrical cables in the room.

During the inspection, the team identified that Davis-Besse Electrical Ampacity Calculation C-EE-015.07-002 assumed ambient temperatures of 110 degrees F for cables located in the Diesel Fire Pump room. This was clearly non-conservative for this room. Since higher temperatures adversely affect the ampacity of electrical cables, the higher temperatures in the Diesel Fire Pump room had the potential to adversely affect the functionality and/or operability of equipment important to safety fed by cabling in the room. Specifically, the possibility existed that some of the equipment that were fed by cables located in the area may not function due to possible faulting of the supply cables.

The inspectors also reviewed Condition Report Number 1998-0001, which identified that ambient temperature in several areas in the plant (i.e., Diesel Generator Rooms, Low Voltage Switchgear/Battery Rooms, Electrical Isolation Rooms, Component Cooling Water Room and Auxiliary Feed Water Pump Rooms) could exceed the rooms design temperatures when the outside temperature is above 95 degrees F. The inspectors noted that the licensee did not address the effects of these heightened temperatures on the electrical cables in these areas. Since the licensees bounding ampacity calculations only evaluated cable ampacity to 110 degrees F, the inspectors were concerned that the possibility existed that some of the equipment that were fed by cables located in these areas may not function due to possible faulting of the supply cables or due to inadequate voltage caused by higher voltage drop. As a result of the inspectors concerns, the licensee issued CR 06-00327.

After performing a preliminary evaluation that assessed cabling in Diesel Fire Pump room and the above listed areas, the licensee determined that there was no evidence that safety related Structures, Systems, and Components (SSCs) would not function as required. While the higher temperatures decreased the ampacity margins for the effected cabling, the licensee preliminarily determined that it did not decrease the margins to the limit where the cabling would fail if called upon to provide power to equipment important to safety.

Analysis:

The inspectors determined that this issue was a performance deficiency warranting a significant determination. The issue was more than minor because it was associated with the Mitigating System Cornerstone attribute of Design Control, and affected the cornerstone objective of ensuring the capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee did not account for high temperature conditions in the Diesel Fire Pump Room and other several rooms (i.e., Low Voltage Switchgear, Electrical Isolation, Component Water Pump, and Auxiliary Feed Water Pump Rooms) that adversely affected cables supplying power to equipment important to safety.

The finding screened as having very low significance (Green) using IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for the At-Power Situations, because the inspectors answered no to all five questions under the Mitigating Systems Cornerstone column of the Phase 1 worksheet. In particular, the licensees preliminary evaluation determined that the higher temperatures would not prevent pertinent equipment from functioning.

Enforcement:

10 CFR Part 50, Appendix B, Criterion III, Design Control states, in part, that measures shall be established to assure that applicable design basis are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, the licensee did not have a design basis calculation for cable ampacity that supported the high temperatures that the Diesel Fire Pump Room and other plants areas could experience. Hence, an adequate design basis was not translated into applicable documents. The Davis-Besse calculation that did address ampacity was significantly less conservative, since temperatures 110 degrees F were assumed where temperatures in these areas could exceed 120 degrees. This condition was known to have existed since 1999.

Because the failure to address the adverse effects of heightened temperatures on cables located in these rooms was determined to be of very low safety significance and because it was entered in the licensees corrective action program as CR 06-00327, this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000346/2006006-03 (DRS))

b.2 Failure to Provide Testing for Boron Precipitation Control Flow Instrumentation

Introduction:

Specifically, after performing modifications to implement a new Boron Precipitation Control method for post-LOCA operations, the licensee failed to implement adequate test controls. The inspectors identified a NCV having very low safety significance (Green) of 10 CFR Part 50, Appendix B, Criterion XI. The licensee failed to both identify and establish testing for the flow instrumentation that the operators would use post-LOCA to ensure minimum flow for proper boron dilution.

Description:

The licensee performed Engineering Change Packages (ECP) 03-0146-00 and 03-0146-01 to implement a new Boron Precipitation Control method. Boron Precipitation Control ensures that flow is being provided through the core to dilute borated water that has been concentrated by evaporation during post-LOCA operations.

The new method required that the LPI pump discharge flow to the reactor vessel via the decay heat drop line. Included in the design change was the refurbishment of an abandoned flow element, FE4909, that would be used for flow indication for the primary BPC flow. During the post-modification test for this new BPC method, the licensee performed a calibration on flow transmitter FT4909 and a flow test to ensure that the minimum BPC flow could be achieved. Davis-Besse operating procedures used for post-accident operations contained steps that measure the BPC flow to ensure that it is greater than the minimum required to establish adequate flow for proper boron dilution.

The revised procedures used this flow element to verify the minimum BPC flow.

Because of the importance of this flow element, the inspectors requested that the licensee provide the inspection team with the Preventive Maintenance (PM) task that should have been established to ensure that FT4909 was always in calibration. The licensee was unable to find an existing PM or a PM in the planning stages. Because of this, the licensee issued CR 06-00217. Subsequent investigation determined that FT4909 was last calibrated in September 2003 when the post-modification flow testing was conducted. While FT4909 had not been calibrated for over 28 months, the vendor manual for the instrument established a +/- 2 percent drift for a 30 month period, so it was reasonable to conclude that the flow transmitter would still have been accurate for use in its design basis function.

However, the team noted that had this issue not been detected, the instrument could have fallen well out of tolerance in the future, leading to inaccurate readings. Because of the importance of FT4909 for establishing BPC post-LOCA, inaccurate readings could have led to the establishment of insufficient BPC flows. As an immediate corrective action for CR 06-00217, the licensee intended to develop a PM to calibrate FT4909 with a 24 month periodicity.

Analysis:

The inspectors determined that this failure to identify and establish testing that ensured satisfactory operation of the boron precipitation control function was a performance deficiency warranting a significance determination. Specifically, after implementing a modification that established a new method for boron precipitation control, the licensee failed to identify and establish calibration testing for the flow instrumentation that would be used post-accident to ensure sufficient boron dilution flow.

The issue was more than minor because if it was left uncorrected, the finding would become a more significant safety concern. Had this issue not been detected, the instrument could have fallen well out of tolerance in the future leading to inaccurate readings. During post-LOCA operations, these inaccurate readings could have caused operators to establish insufficient BPC flows. The finding screened as having very low significance (Green) using IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for the At-Power Situations, because the inspectors answered no to all five questions under the Mitigating Systems Cornerstone column of the Phase 1 worksheet. While the lack of calibration procedures for the flow instrumentation would have eventually caused the instrument to read inaccurately, the inspection team identified the problem early enough so that the instrument drift (as provided in the vendor instructions) would not be large enough to cause inaccuracies that would adversely affect BPC flows.

Enforcement:

10 CFR Part 50, Appendix B, Criterion XI, Test Control states, in part, that a test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Contrary to the above, the licensee failed to identify and establish calibration testing for the flow instrumentation that would be used post-accident to ensure sufficient boron dilution flow.

This flow instrumentation was placed into service in September 2003.

Because this failure to apply appropriate test control measures was determined to be of very low safety significance and because it was entered in the licensees corrective action program as CR 06-00217, this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy. (NCV 06000346/2006006-04 (DRS))

OTHER ACTIVITIES (OA)

4OA2 Identification and Resolution of Problems

.1 Routine Review of Condition Reports

a. Inspection Scope

From January 23 through February 10, 2006, the inspectors Action Process documents that identified or were related to 10 CFR 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent plant modifications and evaluations for changes, tests, or experiments issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the team are listed in the attachment to this report.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. B. Allen and others of the licensees staff, on February 10, 2006 and March 2, 2006. Licensee personnel acknowledged the inspection results presented. Licensee personnel were asked to identify any documents, materials, or information provided during the inspection that were considered proprietary. No proprietary information was identified.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Loehlein, Engineering Director
K. Zellers, Engineering Analysis Supervisor - Design Engineering
C. Price, Regulatory Affairs Manager
J. Grabnar, Engineering Design Manager
G. Wolf, Staff Engineer - Regulatory Affairs
D. Nassor, Engineer - Design Engineering
G. LeBlanc, Engineer - Design Engineering

Nuclear Regulatory Commission

C. Lipa, Reactor Projects Branch 4
D. Hills, Chief, Engineering Branch 1
J. Rutkowski, Senior Resident Inspector

R Smith, Resident Inspector

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000346/2006006-02 URI Change to Design Basis Tornado Differential Pressure Design Limit for the Auxiliary Building

Opened and Closed

05000346/2006006-01 NCV Non-Conservative Flow Testing Acceptance Criteria for the number 2 HPI and number 2 LPI Pumps
05000346/2006006-03 NCV Failure to Consider Adverse Ampacity Effects of High Temperature Conditions in the Diesel Fire Pump Room
05000346/2006006-04 NCV Failure to Provide Testing for Boron Precipitation Control Flow Instrumentation

Discussed

None.

LIST OF DOCUMENTS REVIEWED