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Category:INSPECTION REPORT
MONTHYEARIR 05000003/19980191999-03-0909 March 1999 Insp Rept 50-003/98-19 on 981130-990222.No Violation Noted. Major Areas Inspected:Review of Facility Mgt & Control IR 05000247/19930261993-11-23023 November 1993 Insp Rept 50-247/93-26 on 931108-12.No Violations Noted. Major Areas Inspected:Mgt Support Plans,Protected & Vital Area Physical Barriers,Detection & Assessment Aids,Protected & Vital Area Access Control of Personnel IR 05000286/19930161993-10-19019 October 1993 Insp Rept 50-286/93-16 on 930802-06 & 0920-24.No Violations Noted.Major Areas Inspected:Isi Program,Procedures,Scope of ISI Work for Outage,Current Insp Plan & Testing Procedures IR 05000286/19930211993-09-17017 September 1993 Insp Rept 50-286/93-21 on 930830-0902.No Violations Noted. Major Areas Inspected:Mgt Support & Audits,Protected & Vital Area Physical Barriers,Detection & Assessment Aids & Protected Vital Area Access Control of Personnel ML20247B9531989-08-24024 August 1989 Enforcement Conference Rept 50-286/89-15 on 890808.Major Areas Discussed:Security Program During Spring 1989 Plant Outage IR 05000286/19890151989-07-24024 July 1989 Partially Withheld Physical Security Insp Rept 50-286/89-15 on 890605-07 (Ref 10CFR73.21).Violations Noted Re Physical Barriers,Vital Areas & Access Controls.Major Areas Inspected:Detection & Assessment Aids & Alarm Stations IR 05000286/19890031989-06-13013 June 1989 Enforcement Conference Rept 50-286/89-03 on 890428 in King of Prussia,Pa Re Findings of Insp Repts 50-286/89-03 & 50-286/88-22.Violations Noted.Areas Discussed:Security Program During Current Outage IR 05000286/19890051989-04-11011 April 1989 Partially Withheld Physical Security Insp Rept 50-286/89-05 on 890227-0303 (Ref 10CFR73.21).Violations & Noncompliances Noted.Major Areas inspected:non-routine Event,Mgt Support, Security Program Plans & Audits & Physical Barriers IR 05000247/19880121988-05-24024 May 1988 Physical Security Insp Rept 50-247/88-12 on 880407.No Noncompliance Noted.Major Areas Inspected:Program for Protection of Safeguards Info,Per 10CFR73.21,including Use of Required Storage Repositories & Handling Procedures IR 05000286/19880061988-05-19019 May 1988 Physical Security Insp Rept 50-286/88-06 on 880412-14.No Noncompliance Noted.Major Areas Inspected:Plan & Implementing Procedures,Organization,Program Audits,Testing & Maint,Physical Barriers & Security Sys Power Supply IR 05000286/19870131987-08-21021 August 1987 Safety Sys Outage Mod Insp Rept 50-286/87-13 on 870422-0714. Rept Describes Activities & Findings Associated W/First Portion of Team Insp Re Outage Design Insp IR 05000247/19870141987-06-0808 June 1987 Emergency Preparedness Insp Rept 50-247/87-14 on 870512-14. No Violations Identified.Major Areas Inspected:Licensee Annual Emergency Exercise Performed on 870513 IR 05000286/19870111987-05-14014 May 1987 Insp Rept 50-286/87-11 on 870420-24.No Violations Noted. Major Areas Inspected:Radiological Effluents Control Program,Mgt Controls,Air Cleaning Sys,Program Implementation & Previously Identified Items IR 05000286/19870091987-05-11011 May 1987 Insp Rept 50-286/87-09 on 870402-03.No Violations Noted. Major Areas Inspected:Nuclear Matl Control & Accounting, Including Organization & Operating,Shipping & Receiving, Storage & Internal Control & Records & Repts IR 05000286/19870021987-03-18018 March 1987 Insp Rept 50-286/87-02 on 870127-29.No Violations Noted. Major Areas Inspected:Dosimetry Staffing & Training, Facilities & Equipment Procedures,Dose Assessment QA & Documentation & Recordkeeping IR 05000247/19870041987-03-16016 March 1987 Insp Rept 50-247/87-04 on 870203-0302.No Violations Noted. Major Areas Inspected:Routine Daily Insps,As Well as Unscheduled Backshift Insps of Onsite Activities,Operations, Maint,Surveillance & Review of Periodic & Special Repts IR 05000247/19870021987-03-10010 March 1987 Insp Rept 50-247/87-02 on 870127-29.Violation Noted:Failure to Include Acceptance Limits for Battery Electrolyte Temp & Failure to Ensure Battery Room Temp within Normal Bounds IR 05000286/19870011987-03-0505 March 1987 Insp Rept 50-286/87-01 on 870106-0217.Major Areas Inspected: Plant Operations Including Shift Logs & Records,Reactor Trips/Engineered Safeguards Actuation,Surveillance,Maint & Followup to Generic Ltr 83-28 & TMI Action Items IR 05000247/19870011987-02-26026 February 1987 Insp Rept 50-247/87-01 on 870106-0202.Violation Noted:No post-maint (Mod) Test Performed After Changing Location of Emergency Diesel Generator Svc Water Flow Indication & Control Instruments IR 05000286/19860241987-02-0909 February 1987 Insp Rept 50-286/86-24 on 861215-19.Violation Noted:Raychem Splices Identified W/Less than Required 2-inch Overlap & Bending Radii Less than Allowed IR 05000247/19860331987-01-27027 January 1987 Radiation Protection Insp Rept 50-247/86-33 on 861215-19.No Violations Noted.Major Areas Inspected:Alara,Internal Exposure Control & External Exposure Control IR 05000247/19861361987-01-21021 January 1987 Meeting Rept 50-247/86-136 on 861209.Major Items Discussed: Plans for Integrated Assessment of Auxiliary Feedwater Sys. Mods Being Considered Include Providing Direct Indication of Overspeed Trip Mechanism Status in Control Room IR 05000286/19860231987-01-15015 January 1987 Onsite Regular & Backshift Insp Rept 50-286/86-23 on 861118- 870105.Violation Noted:Failure to Follow Administrative Procedures AP-6 & AP-25-3 Re Work Requests & Matl Substitutions,Respectively IR 05000247/19860321987-01-13013 January 1987 Insp Rept 50-247/86-32 on 861122-870105.No Violations Noted. Major Areas Inspected:Licensee Actions on Previously Identified Insp Findings,Operations,Maint,Surveillance & Review of Periodic & Special Repts IR 05000247/19860301987-01-0707 January 1987 Partially Withheld Physical Security Insp Rept 50-247/86-30 on 861117-21 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected:Security Plan & Implementing Procedures, Security Organization & Assessment Aids IR 05000247/19860281986-12-23023 December 1986 Insp Rept 50-247/86-28 on 861014-1121.Violation Noted: Failure to Perform Test Confirming That Mod Produced Expected Results & That Mod Did Not Reduce Safety of Operations IR 05000247/19860261986-09-22022 September 1986 Insp Rept 50-247/86-26 on 860826-28.Major Areas Inspected: Requalification & Initial Licensing Training Programs for Licensed Operators.No Tracking Sys for Assuring Compliance w/10CFR55.31(e) Requirements IR 05000247/19860171986-08-0505 August 1986 Health Physics Appraisal Rept 50-247/86-17 on 860616-20.No Violations Noted.Major Areas Inspected:Radiation Controls Program,Developed Per NRC 840927 Order Modifying License, Including ALARA & High Radiation Area Control IR 05000247/19860131986-07-0909 July 1986 Emergency Preparedness Insp Rept 50-247/86-13 on 860604.No Violations Noted.Major Areas inspected:full-participation Emergency Exercise IR 05000286/19860061986-04-15015 April 1986 Emergency Preparedness Insp Rept 50-286/86-06 on 860311-13. No Violations Identified.Major Areas Inspected:Observation of Annual Emergency Exercise on 860312 IR 05000247/19860011986-04-11011 April 1986 Mgt Meeting Rept 50-247/86-01 on 860320.Violation Noted: Environ Health & Safety Personnel Not Trained in Responsibilities for QC & QC Responsibilities Inadequately Specified IR 05000247/19860091986-04-0808 April 1986 Insp Rept 50-247/86-09 on 860304-31.Insp Identified Two Unresolved Items Re Environ Qualification.Major Areas Inspected:Licensee Action on Previously Identified Insp Findings,Ler Followup,Fire Protection & Plant Security IR 05000286/19860041986-04-0303 April 1986 Insp Rept 50-286/86-04 on 860303-06.No Violations Noted. Major Areas Inspected:Nonradiological Chemistry Program, Including Measurement Control,Analytical Procedure Evaluations & Training IR 05000247/19860021986-03-11011 March 1986 Enforcement Conference Rept 50-247/86-02 on 860213.Major Areas Discussed:Violations Noted in Insp Rept 50-247/86-02 & Corrective Actions Taken IR 05000247/19850141985-06-21021 June 1985 Emergency Preparedness Insp Rept 50-247/85-14 on 850604-06. No Violation or Deviation Noted.Major Areas Inspected: Observation of Licensee Annual Emergency Exercise Performed on 850605 IR 05000286/19820101982-07-29029 July 1982 IE Insp Rept 50-286/82-10 on 820616-0715.No Noncompliance Noted.Major Areas Inspected:Shift Logs & Records,Action on Previous Findings,Audits,Loss of Offsite Power & Followup on IE Bulletins IR 05000286/19820021982-07-22022 July 1982 IE Emergency Preparedness Appraisal Rept 50-286/82-02 on 820208-11.No Noncompliance Noted.Major Areas Inspected: Followup of Emergency Preparedness Items from Prior Appraisal on 810511-20 IR 05000286/19820091982-07-0101 July 1982 IE Insp Rept 50-286/82-09 on 820601-04.Noncompliance Noted: Failure to Install Sprinkler Head Specified Per Natl Fire Protection Assoc Code 15,1977 IR 05000003/19820011982-06-29029 June 1982 Revised IE Insp Repts 50-003/82-01 & 50-247/82-02 on 820208- 11.No Noncompliance Noted.Major Areas Inspected:Followup of Emergency Preparedness Items from 810511-20 Appraisal.Rept Includes Revised Page 22 IR 05000286/19820081982-06-28028 June 1982 IE Insp Rept 50-286/82-08 on 820516-0615.Noncompliance Noted:On 820527,solid Radwaste Operations Using Baling Machine Conducted W/O Following Written Procedure & Shroud Door Not Closed as Required During Operation IR 05000247/19820101982-06-24024 June 1982 IE Insp Rept 50-247/82-10 on 820524-28.Noncompliance Noted: Failure to Follow Field Const Procedures & Inadequate Design Interface Control ML20054L0501982-06-15015 June 1982 IE Insp Rept 50-247/82-09 on 820501-31.Noncompliance Noted:Failure to Revise Procedures to Include Mod to Operational Protection Sys Setpoints Completed in Mar 1981 IR 05000247/19820081982-05-20020 May 1982 IE Insp Rept 50-247/82-08 on 820503-07.No Noncompliance Noted.Major Areas Inspected:Fire Protection/Prevention Program,Completion of Fire Hazards Analysis Commitments & SER Commitments ML20062D8201978-10-19019 October 1978 IE Inspec Rept 50-247/78-30 on 780913-14 During Which No Items of Noncompliance Were Noted.Major Areas Inspected Incl:Licensee Response to IE Circular 78-08 Environ Qual of Safety Related Elec Equip IR 05000247/19780281978-09-14014 September 1978 IE Inspec Rept 50-247/78-28 on 780825 During Which No Items of Noncompliance Were Noted.Major Areas Inspec Incl: Previously Identified Unresolved Items W/Respect to Records 1999-03-09
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000003/19980191999-03-0909 March 1999 Insp Rept 50-003/98-19 on 981130-990222.No Violation Noted. Major Areas Inspected:Review of Facility Mgt & Control IR 05000247/19930261993-11-23023 November 1993 Insp Rept 50-247/93-26 on 931108-12.No Violations Noted. Major Areas Inspected:Mgt Support Plans,Protected & Vital Area Physical Barriers,Detection & Assessment Aids,Protected & Vital Area Access Control of Personnel IR 05000286/19930161993-10-19019 October 1993 Insp Rept 50-286/93-16 on 930802-06 & 0920-24.No Violations Noted.Major Areas Inspected:Isi Program,Procedures,Scope of ISI Work for Outage,Current Insp Plan & Testing Procedures IR 05000286/19930211993-09-17017 September 1993 Insp Rept 50-286/93-21 on 930830-0902.No Violations Noted. Major Areas Inspected:Mgt Support & Audits,Protected & Vital Area Physical Barriers,Detection & Assessment Aids & Protected Vital Area Access Control of Personnel ML20247B9531989-08-24024 August 1989 Enforcement Conference Rept 50-286/89-15 on 890808.Major Areas Discussed:Security Program During Spring 1989 Plant Outage IR 05000286/19890151989-07-24024 July 1989 Partially Withheld Physical Security Insp Rept 50-286/89-15 on 890605-07 (Ref 10CFR73.21).Violations Noted Re Physical Barriers,Vital Areas & Access Controls.Major Areas Inspected:Detection & Assessment Aids & Alarm Stations IR 05000286/19890031989-06-13013 June 1989 Enforcement Conference Rept 50-286/89-03 on 890428 in King of Prussia,Pa Re Findings of Insp Repts 50-286/89-03 & 50-286/88-22.Violations Noted.Areas Discussed:Security Program During Current Outage IR 05000286/19890051989-04-11011 April 1989 Partially Withheld Physical Security Insp Rept 50-286/89-05 on 890227-0303 (Ref 10CFR73.21).Violations & Noncompliances Noted.Major Areas inspected:non-routine Event,Mgt Support, Security Program Plans & Audits & Physical Barriers IR 05000247/19880121988-05-24024 May 1988 Physical Security Insp Rept 50-247/88-12 on 880407.No Noncompliance Noted.Major Areas Inspected:Program for Protection of Safeguards Info,Per 10CFR73.21,including Use of Required Storage Repositories & Handling Procedures IR 05000286/19880061988-05-19019 May 1988 Physical Security Insp Rept 50-286/88-06 on 880412-14.No Noncompliance Noted.Major Areas Inspected:Plan & Implementing Procedures,Organization,Program Audits,Testing & Maint,Physical Barriers & Security Sys Power Supply IR 05000286/19870131987-08-21021 August 1987 Safety Sys Outage Mod Insp Rept 50-286/87-13 on 870422-0714. Rept Describes Activities & Findings Associated W/First Portion of Team Insp Re Outage Design Insp IR 05000247/19870141987-06-0808 June 1987 Emergency Preparedness Insp Rept 50-247/87-14 on 870512-14. No Violations Identified.Major Areas Inspected:Licensee Annual Emergency Exercise Performed on 870513 IR 05000286/19870111987-05-14014 May 1987 Insp Rept 50-286/87-11 on 870420-24.No Violations Noted. Major Areas Inspected:Radiological Effluents Control Program,Mgt Controls,Air Cleaning Sys,Program Implementation & Previously Identified Items IR 05000286/19870091987-05-11011 May 1987 Insp Rept 50-286/87-09 on 870402-03.No Violations Noted. Major Areas Inspected:Nuclear Matl Control & Accounting, Including Organization & Operating,Shipping & Receiving, Storage & Internal Control & Records & Repts IR 05000286/19870021987-03-18018 March 1987 Insp Rept 50-286/87-02 on 870127-29.No Violations Noted. Major Areas Inspected:Dosimetry Staffing & Training, Facilities & Equipment Procedures,Dose Assessment QA & Documentation & Recordkeeping IR 05000247/19870041987-03-16016 March 1987 Insp Rept 50-247/87-04 on 870203-0302.No Violations Noted. Major Areas Inspected:Routine Daily Insps,As Well as Unscheduled Backshift Insps of Onsite Activities,Operations, Maint,Surveillance & Review of Periodic & Special Repts IR 05000247/19870021987-03-10010 March 1987 Insp Rept 50-247/87-02 on 870127-29.Violation Noted:Failure to Include Acceptance Limits for Battery Electrolyte Temp & Failure to Ensure Battery Room Temp within Normal Bounds IR 05000286/19870011987-03-0505 March 1987 Insp Rept 50-286/87-01 on 870106-0217.Major Areas Inspected: Plant Operations Including Shift Logs & Records,Reactor Trips/Engineered Safeguards Actuation,Surveillance,Maint & Followup to Generic Ltr 83-28 & TMI Action Items IR 05000247/19870011987-02-26026 February 1987 Insp Rept 50-247/87-01 on 870106-0202.Violation Noted:No post-maint (Mod) Test Performed After Changing Location of Emergency Diesel Generator Svc Water Flow Indication & Control Instruments IR 05000286/19860241987-02-0909 February 1987 Insp Rept 50-286/86-24 on 861215-19.Violation Noted:Raychem Splices Identified W/Less than Required 2-inch Overlap & Bending Radii Less than Allowed IR 05000247/19860331987-01-27027 January 1987 Radiation Protection Insp Rept 50-247/86-33 on 861215-19.No Violations Noted.Major Areas Inspected:Alara,Internal Exposure Control & External Exposure Control IR 05000247/19861361987-01-21021 January 1987 Meeting Rept 50-247/86-136 on 861209.Major Items Discussed: Plans for Integrated Assessment of Auxiliary Feedwater Sys. Mods Being Considered Include Providing Direct Indication of Overspeed Trip Mechanism Status in Control Room IR 05000286/19860231987-01-15015 January 1987 Onsite Regular & Backshift Insp Rept 50-286/86-23 on 861118- 870105.Violation Noted:Failure to Follow Administrative Procedures AP-6 & AP-25-3 Re Work Requests & Matl Substitutions,Respectively IR 05000247/19860321987-01-13013 January 1987 Insp Rept 50-247/86-32 on 861122-870105.No Violations Noted. Major Areas Inspected:Licensee Actions on Previously Identified Insp Findings,Operations,Maint,Surveillance & Review of Periodic & Special Repts IR 05000247/19860301987-01-0707 January 1987 Partially Withheld Physical Security Insp Rept 50-247/86-30 on 861117-21 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected:Security Plan & Implementing Procedures, Security Organization & Assessment Aids IR 05000247/19860281986-12-23023 December 1986 Insp Rept 50-247/86-28 on 861014-1121.Violation Noted: Failure to Perform Test Confirming That Mod Produced Expected Results & That Mod Did Not Reduce Safety of Operations IR 05000247/19860261986-09-22022 September 1986 Insp Rept 50-247/86-26 on 860826-28.Major Areas Inspected: Requalification & Initial Licensing Training Programs for Licensed Operators.No Tracking Sys for Assuring Compliance w/10CFR55.31(e) Requirements IR 05000247/19860171986-08-0505 August 1986 Health Physics Appraisal Rept 50-247/86-17 on 860616-20.No Violations Noted.Major Areas Inspected:Radiation Controls Program,Developed Per NRC 840927 Order Modifying License, Including ALARA & High Radiation Area Control IR 05000247/19860131986-07-0909 July 1986 Emergency Preparedness Insp Rept 50-247/86-13 on 860604.No Violations Noted.Major Areas inspected:full-participation Emergency Exercise IR 05000286/19860061986-04-15015 April 1986 Emergency Preparedness Insp Rept 50-286/86-06 on 860311-13. No Violations Identified.Major Areas Inspected:Observation of Annual Emergency Exercise on 860312 IR 05000247/19860011986-04-11011 April 1986 Mgt Meeting Rept 50-247/86-01 on 860320.Violation Noted: Environ Health & Safety Personnel Not Trained in Responsibilities for QC & QC Responsibilities Inadequately Specified IR 05000247/19860091986-04-0808 April 1986 Insp Rept 50-247/86-09 on 860304-31.Insp Identified Two Unresolved Items Re Environ Qualification.Major Areas Inspected:Licensee Action on Previously Identified Insp Findings,Ler Followup,Fire Protection & Plant Security IR 05000286/19860041986-04-0303 April 1986 Insp Rept 50-286/86-04 on 860303-06.No Violations Noted. Major Areas Inspected:Nonradiological Chemistry Program, Including Measurement Control,Analytical Procedure Evaluations & Training IR 05000247/19860021986-03-11011 March 1986 Enforcement Conference Rept 50-247/86-02 on 860213.Major Areas Discussed:Violations Noted in Insp Rept 50-247/86-02 & Corrective Actions Taken IR 05000247/19850141985-06-21021 June 1985 Emergency Preparedness Insp Rept 50-247/85-14 on 850604-06. No Violation or Deviation Noted.Major Areas Inspected: Observation of Licensee Annual Emergency Exercise Performed on 850605 IR 05000286/19820101982-07-29029 July 1982 IE Insp Rept 50-286/82-10 on 820616-0715.No Noncompliance Noted.Major Areas Inspected:Shift Logs & Records,Action on Previous Findings,Audits,Loss of Offsite Power & Followup on IE Bulletins IR 05000286/19820021982-07-22022 July 1982 IE Emergency Preparedness Appraisal Rept 50-286/82-02 on 820208-11.No Noncompliance Noted.Major Areas Inspected: Followup of Emergency Preparedness Items from Prior Appraisal on 810511-20 IR 05000286/19820091982-07-0101 July 1982 IE Insp Rept 50-286/82-09 on 820601-04.Noncompliance Noted: Failure to Install Sprinkler Head Specified Per Natl Fire Protection Assoc Code 15,1977 IR 05000003/19820011982-06-29029 June 1982 Revised IE Insp Repts 50-003/82-01 & 50-247/82-02 on 820208- 11.No Noncompliance Noted.Major Areas Inspected:Followup of Emergency Preparedness Items from 810511-20 Appraisal.Rept Includes Revised Page 22 IR 05000286/19820081982-06-28028 June 1982 IE Insp Rept 50-286/82-08 on 820516-0615.Noncompliance Noted:On 820527,solid Radwaste Operations Using Baling Machine Conducted W/O Following Written Procedure & Shroud Door Not Closed as Required During Operation IR 05000247/19820101982-06-24024 June 1982 IE Insp Rept 50-247/82-10 on 820524-28.Noncompliance Noted: Failure to Follow Field Const Procedures & Inadequate Design Interface Control ML20054L0501982-06-15015 June 1982 IE Insp Rept 50-247/82-09 on 820501-31.Noncompliance Noted:Failure to Revise Procedures to Include Mod to Operational Protection Sys Setpoints Completed in Mar 1981 IR 05000247/19820081982-05-20020 May 1982 IE Insp Rept 50-247/82-08 on 820503-07.No Noncompliance Noted.Major Areas Inspected:Fire Protection/Prevention Program,Completion of Fire Hazards Analysis Commitments & SER Commitments ML20062D8201978-10-19019 October 1978 IE Inspec Rept 50-247/78-30 on 780913-14 During Which No Items of Noncompliance Were Noted.Major Areas Inspected Incl:Licensee Response to IE Circular 78-08 Environ Qual of Safety Related Elec Equip IR 05000247/19780281978-09-14014 September 1978 IE Inspec Rept 50-247/78-28 on 780825 During Which No Items of Noncompliance Were Noted.Major Areas Inspec Incl: Previously Identified Unresolved Items W/Respect to Records 1999-03-09
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000003/19980191999-03-0909 March 1999 Insp Rept 50-003/98-19 on 981130-990222.No Violation Noted. Major Areas Inspected:Review of Facility Mgt & Control ML20237D1381998-08-19019 August 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:Between 971024 & 980528,licensee Failed to Assure That Design Change in Oct 1997 Subject to Design Control Measures ML20236M6011998-07-0606 July 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $110,000.Violation Noted:On 970808,double Verifications of Steps 3.4.1 & 3.5.2 of PT-W1,which Involved Checks of DG Compressor,Not Performed,But Records Created ML20154Q1951998-01-22022 January 1998 Partially Deleted Investigation Rept 1-97-038.Noncompliance Noted.Major Areas Investigated:Falsification of Surveillance Test Records by Nuclear Production Technician ML20217H3531997-10-0707 October 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $110,000.Violation Noted:Con Edison Did Not Operate within Restrictions of TS Figure 3.1.A-3,in That Pressurizer Level Was Greater than 30% PNO-I-97-053, on 970826,special Security Insp Will Be Performed,That Will Examine Security Activities at Vermont Yankee,Pilgrim & Indian Point 3.Team Will Include Security Specialists from Region I & NRR1997-08-22022 August 1997 PNO-I-97-053:on 970826,special Security Insp Will Be Performed,That Will Examine Security Activities at Vermont Yankee,Pilgrim & Indian Point 3.Team Will Include Security Specialists from Region I & NRR ML20217R3361997-08-19019 August 1997 NOV & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:Measures Were Not Established to Assure That Applicable Regulatory Requirements & Design Basis,Were Correctly Translated Into EOPs IR 05000247/19930261993-11-23023 November 1993 Insp Rept 50-247/93-26 on 931108-12.No Violations Noted. Major Areas Inspected:Mgt Support Plans,Protected & Vital Area Physical Barriers,Detection & Assessment Aids,Protected & Vital Area Access Control of Personnel IR 05000286/19930161993-10-19019 October 1993 Insp Rept 50-286/93-16 on 930802-06 & 0920-24.No Violations Noted.Major Areas Inspected:Isi Program,Procedures,Scope of ISI Work for Outage,Current Insp Plan & Testing Procedures IR 05000286/19930211993-09-17017 September 1993 Insp Rept 50-286/93-21 on 930830-0902.No Violations Noted. Major Areas Inspected:Mgt Support & Audits,Protected & Vital Area Physical Barriers,Detection & Assessment Aids & Protected Vital Area Access Control of Personnel PNO-I-90-094, on 901016,transfer of Fuel Assemblies Stuck in Upper Core Internals.No Apparent Damage to Dropped Fuel Assembly Occurred.Recovery Operations Secured1990-10-17017 October 1990 PNO-I-90-094:on 901016,transfer of Fuel Assemblies Stuck in Upper Core Internals.No Apparent Damage to Dropped Fuel Assembly Occurred.Recovery Operations Secured PNO-I-90-077, on 900906,unplanned Shutdown Greater than 48 H Occurred Due to RCS Packing Leak from Pressurizer Spray Valve.Plant Placed in Hot & Cold Shutdown.Licensee Activities Monitored & State of Ny Informed1990-09-0707 September 1990 PNO-I-90-077:on 900906,unplanned Shutdown Greater than 48 H Occurred Due to RCS Packing Leak from Pressurizer Spray Valve.Plant Placed in Hot & Cold Shutdown.Licensee Activities Monitored & State of Ny Informed PNO-I-90-065, on 900814,licensee Reported That Licensed Reactor Operator Tested Positive for Marijuana as Result of Random Fitness for Duty Test.Operator Unescorted Site Access Suspended for 14 Days1990-08-15015 August 1990 PNO-I-90-065:on 900814,licensee Reported That Licensed Reactor Operator Tested Positive for Marijuana as Result of Random Fitness for Duty Test.Operator Unescorted Site Access Suspended for 14 Days PNO-I-90-063, on 900809,plant Shutdown Due to Potential Loss of Three Emergency Diesel Generators.Caused by Blown Control Power Fuse.Fuse Replaced1990-08-0909 August 1990 PNO-I-90-063:on 900809,plant Shutdown Due to Potential Loss of Three Emergency Diesel Generators.Caused by Blown Control Power Fuse.Fuse Replaced ML20247K5281989-09-14014 September 1989 EN-89-086:on 890919,notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000 Will Be Issued to Licensee Based on Security Violations Re Access Control & Illumination in Protected Area ML20247B9531989-08-24024 August 1989 Enforcement Conference Rept 50-286/89-15 on 890808.Major Areas Discussed:Security Program During Spring 1989 Plant Outage IR 05000286/19890151989-07-24024 July 1989 Partially Withheld Physical Security Insp Rept 50-286/89-15 on 890605-07 (Ref 10CFR73.21).Violations Noted Re Physical Barriers,Vital Areas & Access Controls.Major Areas Inspected:Detection & Assessment Aids & Alarm Stations ML20245G2181989-06-21021 June 1989 PNS-I-89-010:on 890621,Dept of Investigation in New York City Received Call Threatening Destruction of Plant & Ref 1977 Incident Where Damage Inflicted on Plant.Bomb Threat Contingency Procedures Implemented & Security Maintained IR 05000286/19890031989-06-13013 June 1989 Enforcement Conference Rept 50-286/89-03 on 890428 in King of Prussia,Pa Re Findings of Insp Repts 50-286/89-03 & 50-286/88-22.Violations Noted.Areas Discussed:Security Program During Current Outage ML20247A1051989-05-0909 May 1989 Notice of Violation from Insp on 890228-0417.Violation Noted:Technicians Failed to Secure Pump When Vibration Level Observed on Pump Motor Exceeded Procedural Limit of 3.5 Mils ML20247A0681989-05-0505 May 1989 Notice of Violation from Insp on 890314-25.Violation Noted: Workers Allowed to Enter High Radiation Areas W/O Being Provided or Accompanied by Individual Authorized in Radiation Protection Procedures IR 05000286/19890051989-04-11011 April 1989 Partially Withheld Physical Security Insp Rept 50-286/89-05 on 890227-0303 (Ref 10CFR73.21).Violations & Noncompliances Noted.Major Areas inspected:non-routine Event,Mgt Support, Security Program Plans & Audits & Physical Barriers ML20154Q7231988-09-21021 September 1988 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $75,000.Violations Noted:Qualification of Containment high-range Radiation Monitors Cable Connector Assembly Deficient PNO-I-88-065, on 880617,unit Tripped Due to High Water Level in Steam Generator 22.Caused by Contractor Cleaner Inadvertently Activating Boiler Feed Pump.Licensee Elected to Enter Cold Shutdown to Repair Connoseals1988-06-20020 June 1988 PNO-I-88-065:on 880617,unit Tripped Due to High Water Level in Steam Generator 22.Caused by Contractor Cleaner Inadvertently Activating Boiler Feed Pump.Licensee Elected to Enter Cold Shutdown to Repair Connoseals IR 05000247/19880121988-05-24024 May 1988 Physical Security Insp Rept 50-247/88-12 on 880407.No Noncompliance Noted.Major Areas Inspected:Program for Protection of Safeguards Info,Per 10CFR73.21,including Use of Required Storage Repositories & Handling Procedures IR 05000286/19880061988-05-19019 May 1988 Physical Security Insp Rept 50-286/88-06 on 880412-14.No Noncompliance Noted.Major Areas Inspected:Plan & Implementing Procedures,Organization,Program Audits,Testing & Maint,Physical Barriers & Security Sys Power Supply PNO-I-88-003, on 880101,steam Generator (SG) 23 Boiled Dry During Plant Heatup.Cause Not Stated.On 880104,station Mgt Started Evaluating Safety Significance of Event & Best Method to Refill Generator.Sg 23 Refilled on 8801051988-01-0707 January 1988 PNO-I-88-003:on 880101,steam Generator (SG) 23 Boiled Dry During Plant Heatup.Cause Not Stated.On 880104,station Mgt Started Evaluating Safety Significance of Event & Best Method to Refill Generator.Sg 23 Refilled on 880105 IR 05000286/19870131987-08-21021 August 1987 Safety Sys Outage Mod Insp Rept 50-286/87-13 on 870422-0714. Rept Describes Activities & Findings Associated W/First Portion of Team Insp Re Outage Design Insp IR 05000247/19870141987-06-0808 June 1987 Emergency Preparedness Insp Rept 50-247/87-14 on 870512-14. No Violations Identified.Major Areas Inspected:Licensee Annual Emergency Exercise Performed on 870513 IR 05000286/19870111987-05-14014 May 1987 Insp Rept 50-286/87-11 on 870420-24.No Violations Noted. Major Areas Inspected:Radiological Effluents Control Program,Mgt Controls,Air Cleaning Sys,Program Implementation & Previously Identified Items IR 05000286/19870091987-05-11011 May 1987 Insp Rept 50-286/87-09 on 870402-03.No Violations Noted. Major Areas Inspected:Nuclear Matl Control & Accounting, Including Organization & Operating,Shipping & Receiving, Storage & Internal Control & Records & Repts PNO-I-87-039, on 870430,licensee Identified Potential Circuit Failure Preventing Automatic Start of Auxiliary Feedwater Pumps by Loss of Main Feedwater or lo-lo Steam Generator Signals.Circuit Modified for Independent Relays1987-05-0101 May 1987 PNO-I-87-039:on 870430,licensee Identified Potential Circuit Failure Preventing Automatic Start of Auxiliary Feedwater Pumps by Loss of Main Feedwater or lo-lo Steam Generator Signals.Circuit Modified for Independent Relays IR 05000286/19870031987-04-12012 April 1987 Exam Rept 50-286/87-03OL on 870224-26.Exam Results:Seven Senior Operator Candidates Passed All Portions of Exams.One Candidate Failed All Portions PNO-I-87-025, on 870326,licensee Announced Plans to Shut Down Reactor on 870327 Due to Steadily Increasing Leakage on Reactor Coolant Pump Seal.Caused by Degraded Seal.Shutdown Expected to Last 10 Days1987-03-26026 March 1987 PNO-I-87-025:on 870326,licensee Announced Plans to Shut Down Reactor on 870327 Due to Steadily Increasing Leakage on Reactor Coolant Pump Seal.Caused by Degraded Seal.Shutdown Expected to Last 10 Days IR 05000286/19870021987-03-18018 March 1987 Insp Rept 50-286/87-02 on 870127-29.No Violations Noted. Major Areas Inspected:Dosimetry Staffing & Training, Facilities & Equipment Procedures,Dose Assessment QA & Documentation & Recordkeeping IR 05000247/19870041987-03-16016 March 1987 Insp Rept 50-247/87-04 on 870203-0302.No Violations Noted. Major Areas Inspected:Routine Daily Insps,As Well as Unscheduled Backshift Insps of Onsite Activities,Operations, Maint,Surveillance & Review of Periodic & Special Repts ML20207S3401987-03-11011 March 1987 Notice of Violation from Insp on 870127-29 IR 05000247/19870021987-03-10010 March 1987 Insp Rept 50-247/87-02 on 870127-29.Violation Noted:Failure to Include Acceptance Limits for Battery Electrolyte Temp & Failure to Ensure Battery Room Temp within Normal Bounds ML20207R1791987-03-0606 March 1987 PNS-I-87-003:on 870306,security Officer at Offsite Training Ctr in Toddville,Ny Received Bomb Threat by Telephone.Search of Site Produced Negative Results.Local Law Enforcement Agencies Responded.Security Measures Heightened IR 05000286/19870011987-03-0505 March 1987 Insp Rept 50-286/87-01 on 870106-0217.Major Areas Inspected: Plant Operations Including Shift Logs & Records,Reactor Trips/Engineered Safeguards Actuation,Surveillance,Maint & Followup to Generic Ltr 83-28 & TMI Action Items ML20212J3921987-03-0202 March 1987 Notice of Violation from Insp on 870106-0202 IR 05000247/19870011987-02-26026 February 1987 Insp Rept 50-247/87-01 on 870106-0202.Violation Noted:No post-maint (Mod) Test Performed After Changing Location of Emergency Diesel Generator Svc Water Flow Indication & Control Instruments PNO-I-87-010, on 870211,reactor Scrammed from Full Power During Transient Initiated by Loss of Instrument Bus.Safety Injection Signal Received on High Steam Flow Coincident W/Low Steam Line Pressure.Plant Stabilized in Hot Shutdown1987-02-12012 February 1987 PNO-I-87-010:on 870211,reactor Scrammed from Full Power During Transient Initiated by Loss of Instrument Bus.Safety Injection Signal Received on High Steam Flow Coincident W/Low Steam Line Pressure.Plant Stabilized in Hot Shutdown ML20210V6021987-02-10010 February 1987 Notice of Violation from Insp on 861215-19 IR 05000286/19860241987-02-0909 February 1987 Insp Rept 50-286/86-24 on 861215-19.Violation Noted:Raychem Splices Identified W/Less than Required 2-inch Overlap & Bending Radii Less than Allowed IR 05000247/19860331987-01-27027 January 1987 Radiation Protection Insp Rept 50-247/86-33 on 861215-19.No Violations Noted.Major Areas Inspected:Alara,Internal Exposure Control & External Exposure Control ML20213A4821987-01-22022 January 1987 Notice of Violation from Insp on 861116-870105 IR 05000247/19861361987-01-21021 January 1987 Meeting Rept 50-247/86-136 on 861209.Major Items Discussed: Plans for Integrated Assessment of Auxiliary Feedwater Sys. Mods Being Considered Include Providing Direct Indication of Overspeed Trip Mechanism Status in Control Room ML20212K3521987-01-20020 January 1987 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000 Based on 860811-0922 Insp.Violation Noted:Reactor Heated Up Above 200 F W/Both Recirculation & Containment Spray Pumps Inoperable IR 05000286/19860231987-01-15015 January 1987 Onsite Regular & Backshift Insp Rept 50-286/86-23 on 861118- 870105.Violation Noted:Failure to Follow Administrative Procedures AP-6 & AP-25-3 Re Work Requests & Matl Substitutions,Respectively 1999-03-09
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U. S. NUCLEAR REGULATORY COMMISSION
REGION I
Repo.t No. 50-286/82-10 Dock?t No. 50-286
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License No. DPR-64 Priority --
Category C Licensee: Power Authority of the State of New York 10 Columbus Circle New York, New York 10019 Facility Name: Indian Point Nuclear Generating Station, Unit 3 ;
Inspection at: Buchanan, New York
- nspection Conducted: June 16, 1982 to July 15, 1982 !
Inspectors: 2 f T Foley,S, eft)rResi nt Inspector date CHUwY- W J. Kenng4 Residen Inspector 7 /M/FL date CrtD L hv H Kistergjlhfef, Inffan Point o b&n date Resident SRtion, Division of Project and Resident Programs Inspection Summary:
- Inspections on June 16, 1982 to July 15,1982 (Inspection Report 50-286/82-10)
Areas Inspected: Routine onsite regular and backshift inspections of plant operations including shift logs and records; licensee action on previous find-ings; plant tour; surveillance; maintenance; review of audits; loss of offsite power; review of monthly report; and follow-up on IE Bulletins. The inspection involved 147 inspector hours by the resident inspector Results: No violations were identifie ;
8208160010 820730 PDR ADOCK 05000286 0 PDR ,
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t DETAILS * Persons Contacted M. Albright, Instrument and Control Superintendent J. Brons, Resident Manager J. Dube, Security and Safety Supervisor D. Halama,-Q.A. Superintendent ,
W. Hamlin, Assistant to the Resident Manager '
W. Josiger, Superintendent of Power J. Perrotta, Radiological and Environmental Services Superintendent 3 S. Munoz, Technical Services Supervisor E. Tagliamonti, Operations Superintendent J. Vignola, Maintenance Superintendent The inspector also interviewed and observed other licensee employees including members of the operations, health physics, technical services, maintenance, and security staff . Licensee Actions on Previous Inspection Findings (Closed) Unresolved Item (50-286/79-18-03). -Failure to correct identified deficiencies. The identified deficiencies were related to housekeepin Recent tours of the facility by the resident inspector indicates these deficiencies have been correcte (Closed) Inspector Follow Item (50-286/79-21-02). Review Changes in dosimetry implementation using TLD's and neutron dosimetry. The inspector reviewed HPP-4.3 Issuance and the Use of Neutron' Dosimetry, which uses the Eberline PNR-4 survey meter and calculated stay times for dose measure-
, ments. Neutron film is used for back up. These procedures are consistent ,
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with Regulatory Guide 8.1 (Closed) Inspector Follow Item (50-286/80-11-10). Failure to determine ,
rate of changes of Delta TC by differential ratio. This requirement has :
been removed from Technical Specification (Closed) Unresolved Item (50-286/81-02-04). Review of outside containment l leakage tests. A review has been conducted by the inspector. See section
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(Closed) Deviation (50-286/81-09-01). Install a fire damper in the ventilation opening between the cable tunnel and the transformer yar The inspector reviewed design change 80-03-079FP and ECM FP-001 and ,
observed the installation of said fire dampe (Closed) Inspector Follow Item (50-286/81-10-04). Finish the unfinished room under the Cable Tunnel. The licensee has diverted the drain from the Boron Injection Tank cell to a monitored area and has cleaned out the drains in the pipe chase. A program of floor drain maintenance has also
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been put into effect. The licensee intends to finish this room at a later dat The inspector no longer considers this an inspector follow ite (Closed) Inspector Follow Item (50-286/81-10-05). Drain Sump Maintenance Program. The licensee is currently in the process of implementing a Drain Sump Maintenance Program. The inspector has no further questions relating to this matte (Closed) Unresolved Item (50-285/81-12-02). Service Water Pump Area Housekeeping. A recent tour by the ir.spector confirms housekeeping in this area has improved. The inspector considers this item close . Plant Tour Normal and backshift inspections were conducted during routine entries into the protected area of the plant, including the control room, PAB, fuel building, and containment. During the inspection activities, discussions were held with operators, technicians (HP &
I&C), mechanics, foremen, supervisors, and plant management. The purpose of the inspection was to affirm the licensee's commitments and compliance with 10 CFR, Technical Specifications, and Administra-tive Procedures. Particular attention was directed in the following areas:
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Instrumentation and recorder traces for abnormalities;
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Proper control room and shift manning;
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Proper use of procedures;
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Review of logs to obtain plant conditions;
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Verification of proper radiologically controlled areas and access points;
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Verification of surveillance testing for timely completion;
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Verification of safety related tagouts;
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Plant housekeeping and cleanliness;
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That protected area access controls were in conformance with the security plan, including sufficient guards to perfrom duties, and that selected gates and doors were closed and locked;
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Selected liquid and gaseous samples to verify conformance with regulatory requirements prior to release; and,
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Boric acid samples to confirm proper boric acid level for plant shutdown condition . .
B. During the inspection, the inspector reviewed the following procedures, documents, or evolutions:
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Radioactive Waste Release Permit (liquid)
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Various shift turnover checklists
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Security Station Logs and Radio Checks
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Jumper Log
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Selected Operators' Logs
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Selected Tagouts
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Selected Radiation Exposure Authorizations (REA's)
C. Findings:
The inspector conducted a review of the control room jumper and lifted lead log book for conformance with 10 CFR 50.59, Technical Specifications, the licensee's procedure AP-13 Jumper Control, and NUREG 0737 requirements. No jumpers or lifted leads were identified in safety related system The inspector noted that procedure AP-13 provides guidance for installing and controlling jumpers, and conforms with the above referenced requirements, except that when a jumper is installed in a safety related system, AP-13 requires that a determination be made concerning an unreviewed safety question, by the operations super-intendent and concurred in by the superintendent of powe The inspector informed the licensee's representative that in accordance with Technical Specifications a proposed change or modification (i.e. a jumper or lifted lead) which affects nuclear safety must be reviewed by the Plant Operating Review Committee (PORC) and the PORC is the only authority that can render a determination whether an unreviewed safety question exists as determined in 10 CFR 50.5 Additionally, neither AP-10.1, Operating Orders and Control of Stop Tags and Do Not Operate Tags, nor AP-13 Jumper Control, specifies that licensed operators are required to verify correct implementation of equipment control measures as required by NUREG 0737. Nor is it documented that a " qualified" licensed operator verify proper align-ment during return to service of equipment important to safet After discussions with plant operators, the inspector determined that Nuclear Plant Operators (NPO) generally verify the correct return to service alignmen NUREG 0737 I.C.6. notes that a qualified operator is a licensed individual, knowledgeable of plant system The licensee maintains that an NPO is qualified and generally performs the return to service alignment under tne direction of a licensed operato The licensee's position with regard to NUREG 0737 item I.C.6 is consistent with their response to the NRC dated December 30, 198 . .
The licensee's representative stated that AP-13 will be revised to require a PORC approval and a 10 CFR 50.59 review for jumpers associ-ated with safety related systems, and that a licensed operator will verify the removal of the jumper and return to service alignment of that system. The licensee continues to maintain that NP0's are <
qualified to verify the return to service alignment for safety related systems and will continue this practic ,
Revision of AP-13 will be reviewed during a subsequent inspection (50-286/82-10-1).
4. Surveillance The inspector conducted an in depth review of surveillance activities to ascertain the following:
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That the instrumentation used was properly calibrated;
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That the redundant system or component was operable where required;
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That properly approved procedures were used by qualified personnel;
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That the acceptance criteria were met; ,
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That the test data were accurate and complete;
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That proper reviews, by the licensee, had been conducted;
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That the results of the tests met Technical Specification requirements; and,
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That the testing was done within the required _ surveillance schedul Tests reviewed:
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3PTR70 Post Accident Containment Air Sampling System Integrity Test
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3PTR72 Volume Control Tank Integrity Test
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3PTR74 Reactor Coolant Accident Sampling System Integrity Test l
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3PTR67 Low Head to High Head Safety Injection Flow Path !
Inspector Comments:
These tests were written to conform with the NUREG 0737 Requirement III.D.1.1, Primary Coolant Outside Containment Leakage Reduction. The tests were performed for the first time this outage; all tests were performed satisfactorily except 3PTR70 which failed because of leakage by the R11 and R12 solenoid valves. A maintenance request was submitted and '
the valves have been repaired. A retest has been schedule No violations were identifie , - . - -
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5. Maintenance
, The inspector selected maintenance activities being conducted on ESF equipment to ascertain that redundant trains were in service, and that approved procedures and qualified personnel were conducting the maintenance.
, The inspector observed portions of maintenance activities listed ,
below to ascertain the following:
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The activities did not violate a limiting condition for operation;
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That redundant components we-e operable; 1 i I
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That equipment was tagged out in accordance with licensee ,
approved procedures;
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That approved procedures, adequate to control the activity, ,
were being used by qualified technicians;
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That Q/C hold points were observed, and that materials were properly certified;
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That radiological controls were proper and in sccordance with licensee approved radiation exposure authorization's; and,
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That the equipment was properly tested prior to return to servic ) 81-03-055 FCU - Installation of New Fan Cooler Unit cooling coils, framework and associated pipin ) 82-03-002 EL - Audibility Improvements (addition of speakers in i key areas in response to Bulletin 79-BU-18).
3) 81-03-040 MS - Replacement of M55 Control Bypass valves for MS ) 82-03-033 FW - Installation of Leading Edge Flow Meters in the Steam Generator Feedwater line ; The inspector also selected completed maintenance activities listed below to ascertain compliance with "B" abov ) Seismic Peak Shock Recorder PSR 1200-H/U-12 Repair of a broken switch contact. Maintenance Request IC-1028-3 _
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2) Reactor Trip Bypass Breakers BYA and BY Installation of ;
support brace in the breaker compartment to prevent misalignment i of pins in the auxiliary switches. Maintenance Request IC- ,
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No violations were identifie . .-- ~ . _ _ - - - --, - __ - - --
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l Audits f The inspector conducted a review of;-A) The Onsite neview Committees ,
(PORC) and B) The Station Audit Program as discussed below: Onsite Review Committes l
The inspector attended a PORC meeting (82-13) conducted on July 7, ;
1982 and observec that: i
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The meeting was conducted with the necessary quorum in attendanc ;
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The meeting was timely and conducted within the time frame ,
required by Technical Specification An agenda was followe '
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Timely events were discussed, such as Temporary Changes to Procedure, Plant Modifications, Significant Occurrence Reports, !
and the latest NRC inspectio The inspector also reviewed minutes of meetings covering the last
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six months noting that:
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Meetings conformed with the meeting frequency established by .
Technical Specification Follow-up actions were being taken by the PORC on previous items in accordance with the PORC minutes follow lis That Bulletins, Circulars, and Information Notices were being reviewed on a timely basi No violations were observe [ Station Audit Program 1) The inspector conducted an in depth review of the Station Audit [
Program utilizing the following document .
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Technical Specifications !
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Quality Assurance Procedure 18.1 (Plant Audit Program) l
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Reg Guide 1.144 - Auditing of QA Programs for Nuclear j Power Plants.
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ANSI N18.7 - Audit Program Requirement !
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ANSI N45.2.12 - Requirements for Auditing of QA Program ANSI N45.2.13 - Requirements for Audit Personne Various Plant Record '
2) The inspector ascertained that the onsite audit program was being conducted in accordance with the licensee's commitments, ,
Technical Specifications and ANSI standards. The inspector also determined that: 1
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The adequacy of the qualifications of the personnel con-ducting the audits were delineated in writing and auditabl Special training had been given to Audit personne .
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Audit personnel have independence from station managemen I
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Written reports were being generated as a result of the ,
audits and were distributed to the proper department head Responses were generated in writing by the personnel being audite ) The inspector had one finding in this are The Quality Assurance department deviated from the form delineated in the QA manual by using a more comprehensive two page form. Discussions with management personnel indicate the inspector's concerns will be rectified in the futur !
, 4) The inspector also observed an audit in progress of Technical Specifications Amendments that have been incorporated into Applicable Operating Procedures, being conducted by the QA
, department. The inspector also reviewed three audits conducted I in 1981 and three audits conducted in 1982 observing that:
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The content of the audits clearly defined the scope of the audi ;
They were conducted by qualified personne "
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The audits were in conformance with the yearly audit list j and Technical Specification l
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Appropriate follow-up action had been taken both by the audited party and the follow-up audit.
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5) The inspector had one finding in this area. The responses to the audits are not being received by the QA department in the recommended 30 day period. Several instances were identified to licensee management by the inspector. This item remains unresolved pending action by licensee management (50-286/81-10-02). Loss of Offsite Electrical Power At 1123 AM on June 22, Unit 3 experienced a total loss of offsite electrical power. All three of the emergency diesel generators functioned normally, and assumed the vital loads. The unit was in a cold shutdown condition utilizing RHR tc, circulate the primary coolant. All emergency equipment functioned as designe An unusual event was declared by the licensee at 1200 noon. Normal power was restored at 1208 PM. Notification was mace in accordance with the site Emergency Pla Inspector Findings The licensee was conducting trip checks on feeder 95331, which was out of service in order to check breaker BT 2-6. Power was being supplied through BT 5-6 from feeder 93332. The switch yard at Buchanan was initiating trip signals in order to do the testin The licensee had completed testing and, while restoring conditions to normal, a spurious trip signal was initiated, which tripped breaker BT- The electrical system was returned to normal at 1208 PM with power being supplied through breaker BT-5.6. The resident inspectors followed the event from its inception until power was restore No violations were identifie . Review of Monthly Report Monthly Operating Report The Monthly Operating Report for June 1982 was reviewed. The review included an examination of selected maintenance work requests, and an examination of significant occurrence reports to ascertain that the summary of operating experience was properly documented.
I Findings:
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The inspector verified through record reviews and observations of maintenance in progress that:
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The corrective action was adequate for resolution of the identified j items; and, L
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The Operating Report included the requirements of TS 6.9. The inspector has no further questions relating to this repor . Follow-up on IE Bulletin The inspector reviewed the following IE Bulleti In addition to his commants, he ascertained that: The written response was within the time period stated in the Bulletin;
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The written response included the information required to be reported;
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The written response includes adequate corrective action commitments ,
based on the information presented in the Bulletin ard licensee's !
response; !
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The licensee's management forwarded copies of the written response to the appropriate onsite management representatives;
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The information discussed in the licensee's written response was accurate; and, l
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The corrective action taken by the licensee was described in the written respons '.
(Closed) 79-BU-18 Audibility problems encountered on evacuation. This Bulletin was reviewed in inspection report 80-13 and closed except for the implementation of the modifications listed in the licensee's letter of March 3, 1980. The inspector recently reviewed Modification Procedure MOD 82-03-003-EL Audibility Improvements which has installed or is currently installing additional speakers in the areas delineated in the letter of March 3, 198 . Unresolved Items An item about which more information is required to determine acceptability is considered unresolved. Paragraph 6.B.5 contains an unresolved ite ;
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11. Exit Interview
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l At periodic intervals during the course of the inspection, meetings were ,
held with senior facility management to discuss the inspection scope and r findings. An additional exit interview was held on July 15, 1982 to summarize inspection findings, and to discuss plant status and current inspector concern i l i
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