IR 05000245/2011008

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ifiay 27, 20IIEA-11-047Mr. David A. HeacockPresident and Chief Nuclear OfficerDominion Resources5000 Dominion Blvd.Glen Allen, VA 23060-6711

SUBJECT: MILLSTONE POWER STATION UNIT 2 - NRC SPECIAL INSPECTIONREPORT 05000336/201 1 008; PRELIMINARY WHITE FINDING

Dear Mr. Heacock:

On April 14,2011, the U. S. Nuclear Regulatory Commission (NRC) completed a SpecialInspection at your Millstone Power Station (Millstone) Unit 2. The inspection was conducted inresponse to an unanticipated reactor power transient event that occurred on February 12,2011.The NRC's initial evaluation of this event satisfied the criteria in NRC lnspection ManualChapter 0309, "Reactive Inspection Decision Basis for Reactors," for conducting a specialinspection. The Special Inspection Team (SlT) Charter (Attachment 2 of the enclosed report)provides the basis and additional details concerning the scope of the inspection. The enclosedinspection report documents the inspection results, which were discussed at the exit meeting onApril 1 4, 2011, with Mr. A. J. Jordan, Millstone Site Vice President, and other members of yourstaff.The Special lnspection Team (the team) examined activities conducted under your license asthey relate to safety and compliance with Commission rules and regulations and with theconditions of your license. The team reviewed selected procedures and records, observedactivities, and interviewed personnel. In particular, the team reviewed event evaluations, causalinvestigations, relevant performance history, and extent-of-condition to assess the significanceand potential consequences of issues related to the February 12 event.The team concluded that the plant operated within acceptable power limits and no equipmentmalfunctioned during the power transient. Nonetheless, the team identified several issuesrelated to procedure discrepancies and human performance that complicated the event.Additionally, the team noted that Dominion's initial response to the event was not appropriatelythorough and timely, did not highlight the significance of the unplanned power increase andreactivity control issues, and was narrowly focused. The enclosed chronology (Attachment 3 ofthe enclosed report) provides additional details regarding the sequence of events and eventcomplications.This report documents one finding that, using the reactor safety Significance DeterminationProcess (SDP), has preliminarily been determined to be White, or of low to moderate safetysignificance. The finding is associated with a performance deficiency involving the failure ofMillstone personnel to carry out their assigned roles and responsibilities and inadequatea.** ttnut t-W;+**tt D. Heacockreactivity management during main turbine control valve testing, which contributed to theunanticipated reactor power increase. Specifically, the Millstone Unit 2 operations crew failed toimplement written procedures that delineated appropriate authorities and responsibilities forsafe operation and shutdown, and a procedure for controlling reactor reactivity. In addition, thelicensee failed to establish written procedures for Reactor Protection System (RPS) VariableHigh-Power Trip (VHT) setpoint reset and for power operation and transients involving multiplereactivity additions.This finding was assessed using NRC Inspection Manual Chapter (lMC) 0609, Appendix M,"SDP Using Qualitative Criteria," because it involved human performance errors. Preliminarily,the NRC has determined this finding to be of low to moderate safety significance based on aqualitative assessment. There were no immediate safety concerns following the transientbecause the event itself did not result in power exceeding license limits or fuel damage.Additionally, interim corrective actions were taken, which included removing the Millstone Unit 2control room crew involved in the transient from operational duties pending remediation, andestablishment of continuous management presence in the Millstone Unit 2 control room whilelong term corrective actions were developed.The finding involved two apparent violations (AVs) of NRC requirements involving TechnicalSpecification 6.8, "Procedures," that are being considered for escalated enforcement action inaccordance with the Enforcement Policy, which can be found on NRC's Web site athttp://www. nrc.oov/readinq-rom/doc-collections/enforcemenU.In accordance with NRC Inspection Manual Chapter (lMC) 0609, we will complete ourevaluation using the best available information and issue our final determination of safetysignificance within 90 days of the date of this letter. The significance determination processencourages an open dialogue between the NRC staff and the licensee; however, the dialogueshould nbt impact the timeliness of the staff's final determination. Before we make a finaldecision on this matter, we are providing you with an opportunity to (1) attend a RegulatoryConference where you can present to the NRC your perspective on the facts and assumptionsthe NRC used to arrive at the finding and assess its significance, or (2) submit your position onthe finding to the NRC in writing. lf you request a Regulatory Conference, it should be heldwithin 30 days of your response to this letter, and we encourage you to submit supportingdocumentation at least one week prior to the conference in an effort to make the conferencemore efficient and effective. lf a Regulatory Conference is held, it will be open for publicobservation. lf you decide to submit only a written response, such submittal should be sent tothe NRC within 30 days of your receipt of this letter. lf you decline to request a RegulatoryConference or submit a written response, you relinquish your right to appeal the final SDPdetermination, in that by not doing either, you failto meet the appeal requirements stated in thePrerequisite and Limitation Sections of Attachment 2 of IMC 0609.Please contact Sam Hansell by telephone at (610) 337-5046 and in writing within 10 days fromthe issue date of this letter to notify the NRC of your intentions. lf we have not heard from youwithin 10 days, we will continue with our significance determination and enforcement decision.The final resolution of this matter will be conveyed in separate correspondence.Because the NRC has not made a final determination in this matter, no Notice of Violation isbeing issued for this inspection finding at this time. Please be advised that the number andcharicterization of the apparent violations described in the enclosed inspection report may change as a result of further NRC review. In addition, the report documents one self-revealingfinding, of very low safety significance (Green). This finding did not involve a violation of NRCrequirements.ln accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any)will be available electronically for public inspection in theNRC Public Document Room and from the Publicly Available Records (PARS) component ofNRC's document system (ADAMS). ADAMS is accessible from the NRC Website athttp://www.nrc.qov/readinq-rm/adams.html (the Public Electronic Reading Room).

Sincerely,p2zz*Christopher G. Miller, DirectorDivision of Reactor SafetyDocket No. 50-336License No. DPR-65

Enclosure:

lnspection Report05000336/2011008

w/Attachments:

Supplemental Information (Attachment 1)Special Inspection Team Charter (Attachment 2)Detailed Sequence of Events (Attachment 3)Appendix M Table 4.1 (Attachment 4)cc w/encl: Distribution via ListServ

SUMMARY OF FINDINGS

........... .............3

REPORT DETAILS

.. .................51. Background and Description of Event..... ...............,........... 52. Human Performance................... ........................ 73. Organizational Response......,......... ............'...154OAO Meetings, Including Exi1............., ... ..".'....'."." 16ATTACHMENT 1 .

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

LIST OF DOCUMENTS REVIEWED

LIST OF ACRONYMS

ATTACHMENT 2 -

SPECIA L
INSPEC TION
TEAM [[]]
CHARTE R
...... ...........2-1
ATTACH MENT 3.
DETAIL [[]]
ED [[]]
SEQUEN [[]]
CE [[]]
OF [[]]
EVENTS [[]]
...... .3-1
ATTACH MENT 4 -
IMC 0609
APPEND IX M,
TAB [[]]
LE 4.1............ ..............4-1Enclosure
3SUMMAR Y
OF [[]]
FINDIN [[]]
GS lR 0500033 612011008; 0212212011 - 0411412011; Millstone Nuclear Power Station (Millstone)Unit 2; Special lnspection for the February 12,2011, Unanticipated Reactor Power TransientEvent; lnspection Procedure 93812, Special Inspection.A three-person
NRC [[team, comprised of two regional inspectors and one resident inspector,conducted this Special Inspection. One representative from the State of Connecticut,Department of Environmental Protection accompanied the team. One finding with potentialforgreater than Green safety significance and one Green finding were identified. The significanceof most findings is indicated by their color (Green, White, Yellow, or Red) using lnspectionManual Chapter (l]]
MC ) 0609, "Significance Determination Process" (SDP); the crosscuttingaspect was determined using
IMC 0310, "Components Within the Cross Cutting Areas;" andfindings for which the
SDP does not apply may be Green or be assigned a severity level afterNRC management review. The
NRC 's program for overseeing the safe operation ofcommercial nuclear power reactors is described in
NUREG -1649, "Reactor Oversight Process,"Revision 4, dated December
2006.NRC [[ldentified and Self Revealing FindingsCornerstone: Initiating Events.LrgI@:Aself-revealingfindingWaSidentifiedinvolvingthefailureoflrltittstone personnel to carry out their assigned roles and responsibilities and inadequatereactivity management during main turbine control valve testing on February 12,2011,which contributed to the unanticipated reactor power increase. Specifically, the MillstoneUnit 2 operations crew failed to implement written procedures that delineated appropriateauthorities and responsibilities for safe operation and shutdown and a procedure forcontrolling reactor reactivity. ln addition, the licensee failed to establish writtenprocedures for the Reactor Protection System (]]
RPS [[) Variable High-Power Trip (VHT),and for power operation and transients involving multiple reactivity additions.The finding has preliminarily been determined to be White, or of low to moderate safetysignificance. The finding is also associated with two apparent violations of]]
NRC [[requirements specified by Technical Specifications. There were no immediate safetyconcerns following the transient because the event itself did not result in powerexceeding license limits or fuel damage. Additionally, interim corrective actions weretaken, which included removing the Millstone Unit 2 control room crew involved in thetransient from operational duties pending remediation, and establishment of continuousmanagement presence in the Millstone Unit 2 control room while long term correctiveactions were developed. Dominion entered this issue, including the evaluation of extent-of-condition, into the corrective action program (]]

CR413602) and performed a root causeevaluation (RCE).The finding is more than minor because the performance deficiency (PD) was associatedwith the human performance attribute of the Initiating Events cornerstone and affectedthe cornerstone objective of limiting the likelihood of those events that upset plantEnclosure

4stability and challenge critical safety functions during power operations. Additionally, thePD could be viewed as a precursor to a significant event. Because the finding primarilyinvolved human performance errors, probabilistic risk assessment tools were not wellsuited for evaluating its significance. The team determined that the criteria for using

IMC [[0609, Appendix M, "significance Determination Process Using Qualitative Criteria," weremet, and the finding was evaluated using this guidance, as described in Attachment 4 tothis report. Based on the qualitative review of this finding, regional managementconcluded the finding was preliminary of low to moderate safety significance (preliminaryWhite).The team determined that the]]
PD [[resulted from several causes; however, the teamconcluded that the primary cause was ineffective reinforcement of Dominion standardsand expectations. The team also concluded that this finding had a cross-cutting aspectin the Human Performance area, Decision Making component, because Dominionlicensed personnel did not make the appropriate safety-significant decisions, especiallywhen faced with uncertain or unexpected plant conditions to ensure safety wasmaintained. This includes formally defining the authority and roles for decisions affectingnuclear safety, communicating these roles to applicable personnel, and implementingthese roles and authorities as designed H.1(a). (Section 2'1)Green: The team identified a self-revealing finding of very low safety significancetCreenl for improper operation of the turbine controls during turbine control valve testing.Specifically, the inspectors identified that control room operators failed to correctlyimplement surveillance procedure]]
SP [[-2651N, "Main Control Valve Testing." Incorrectoperation of the turbine controls caused an unplanned power increase from 88 percentto 96 percent. Dominion entered this issue into the corrective action program(cR4150e4).The team determined that this finding was more than minor because it was similar to]]

NRC Inspection Manual Chapter 0612, Appendix E, "Examples of Minor lssues,"Example 4b, in that the incorrect operation of the turbine load selector pushbuttoncaused a plant transient. The finding was associated with the human performanceattribute of the Initiating Events cornerstone and affected the cornerstone objective oflimiting the likelihood of those events that upset plant stability and challenge criticalsafety functions during power operations. The team concluded that the finding was ofvery [ow safety significance (Green) because it did not contribute to both the likelihood ofa reactor trip and the likelihood that mitigation equipment or functions would not beavailable. Enforcement action does not apply because the performance deficiency didnot involve a violation of a regulatory requirement. The team also determined that thefinding had a cross-cutting aspect in the Human Performance area, Resourcescomponent, because Dominion did not provide adequate training of personnel andsufficient qualified personnel H.2(b). (Section 2.2)Enclosure

1.5REPORT

DETAIL [[]]
SB [[ackqround and Description of EventIn accordance with the Special Inspection Team (SlT) Charter (Attachment 2), teammembers (the team) conducted a detailed review of the February 12,2011, unanticipatedreactor power transient event at Millstone Nuclear Power Station (Millstone) Unit 2,including a review of Millstone Unit 2 operators' response to the event. The teamgathered information from the plant process computer (PPC) alarm printouts andparameter trends, interviewed station personnel, observed an event reconstruction onthe simulator, observed on-going control room activities, and reviewed procedures, logs,and various technical documents to develop a detailed timeline of the event (Attachment3).On Saturday February 12,2011, Millstone Unit 2 experienced an unintended 8 percentreactor power transient (88 percent to 96 percent) during the performance of quarterlymain turbine control valve testing. As more fully described below, the transient wascaused by multiple human performance errors committed independently by the operatorsinvolved with the testing, and was compounded by problems in communications andcommand and control.Two days prior to the event, the control room operating crew that was involved with theevent attended a four hour just-in-time simulator training session for the planned reactorpower decrease to 88 percent and the Millstone Unit 2 main turbine control valve testingevolution. The crew also received a briefing on the planned evolution from MillstoneOperations Department management on February 12, just prior to beginning the mainturbine control valve test.On the day of the Millstone Unit 2 main turbine control valve test, the Millstone Unit 2control room was staffed with the following normalfive-person crew complement:. Shift Manager (SM);. Unit Supervisor (US);' Operator At The Controls Reactor Operator (OATC]]
RO );. Balance of Plant Reactor Operator (
BOP [[]]
RO ); and. Shift TechnicalAdvisor (
STA ), a non-licensed position.Additionally, 3 other individuals were in the control room specifically to supportperformance of the test:. an
SRO -licensed and
SM -qualified individualto provide operations managementoversight;. an
SRO -licensed individual designated as the "Reactivity

SRO" to directlysupervise all reactivity changes; and. a Reactor Engineer to assist with development and implementation of thereactivity plan.Enclosure

6lnitial conditions for the control valve testing were established as follows:1. Unit 2 reactor power was reduced to 88 percent.2. The main turbine valve control was transferred from Load Limit to Load Set,applying a control signal to position the turbine control valves to maintain theexisting main generator load.3. The crew adjusted turbine load and the turbine bypass valve controller automaticsetpoint to open one of the turbine bypass valves approximately 10 percent.Turbine bypass flow is established by the test procedure to allow the turbinebypass controller to automatically compensate for any small steam flowperturbations, thereby maintaining constant reactor power during testing.A 600 gallon reactor coolant system (RCS) dilution was initiated to compensate for theeffects of core fission product poison (Xenon) concentration changes initiated by thereactor power reduction.The test procedure provided direction to the operators to maintain constant turbine firststage pressure (t 10 psig) using the Load Set

INCREA [[]]
SE and
DECREA [[]]
SE [[pushbuttonswhile slowly rotating the turbine first stage pressure feedback potentiometer from theOUT to the lN position over a one minute period. lnsertion of first stage pressurefeedback into the control loop ensures the control valves change position in response tochanges in first stage pressure, which varies linearly with turbine load. When a controlvalve is stroked closed for testing, load set control with first stage pressure feedbackattempts to automatically maintain turbine load constant by opening the other threecontrol valves in response to decreasing first stage pressure.At approximately 11:30 am, the]]
BOP [[]]
RO correctly began rotating the turbine first stagepressure potentiometer toward the lN position. However, in response to increasingturbine first stage pressure, the
BOP [[]]
RO incorrectly depressed the
INCREA [[]]
SE loadselector button (rather than the
DECREA [[]]
SE load selector button), thereby increasingsteam supplied to the turbine and further increasing first stage pressure. When theoperator did not get the desired response (a reduction in first stage pressure), the
BOPRO pressed the
INCREA SE pushbutton 3 more times, followed by two depressions ofthe
DECREA [[]]
SE pushbutton. The increased steam demand by the turbine resulted inlower
RCS cold leg temperature, the automatic closure of the one partially open turbinebypass valve, and a reactor power transient over a three minute period which peaked at96 percent power.Neither the
STA (who was performing the peer-check) nor the
US (who was observingthe test) initially corrected the
BOP [[]]
RO , because both also incorrectly believed pressingthe

INCREASE button was the correct action. Additionally, none of these threeindividuals informed the rest of the crew that they had an unexpected response and thata transient was in progress.Enclosure

2.2.1a.7At the onset of the event, the

RPS [[]]
VHT setpoints were below 96 percent (Ch A at 95,7percent, Ch B at 95.4 percent, Ch C at 94.9 percent, and Ch D at94.4 percent). Duringthe turbine transient, reactor power increased toward the
VHT setpoints. The Reactivity
SRO observed the illumination of the
VHT setpoint reset permissive lights (one light per
RPS channel), and incorrectly assumed they were illuminating due to minor powerfluctuations associated with the fission product poison build-in and on-going
RCS dilution. Consequently, he increased the margin to the trip setpoint by resetting the
VHT setpoints upward four times during the power rise. lf the
SRO had not reset the
VHT ,the
RPS would have automatically initiated a high power reactor trip due to themagnitude of the reactor power increase from 88 to 96 percent. In addition to preventingthe automatic trip, the Reactivity
SRO did not understand or question why reactor powerwas increasing, and did not inform anyone on the crew of his actions to reset the
VHT setpoints.The
SM observed the closure of the partially open turbine bypass valve and directed theOATC
RO to lower the turbine bypass valve controller setpoint to re-open the valve anddirected the Reactivity
SRO to withdraw one bank of control rods four steps to raisereactor temperature. Each of these actions added further positive reactivity andcontributed to the reactor power increase. He also directed the
US to return to a positionof oversight and he directed the
BOP [[]]
RO to stop manipulating turbine controls.After the plant stabilized, the
SM [[incorrectly determined that the power transient hadbeen limited to a maximum of four percent power, based on using the excore nuclearinstruments instead of the more accurate Q-power indication, and decided to completethe turbine control valve testing before the end of the shift. Excore nuclear instrumentsdid not accurately indicate the amount of the power increase due to normal instrumentbehavior in a significantly reduced primary coolant temperature environment. The fullextent of the power transient was not identified until the next day when Millstone reactorengineers completed a formal assessment of the transient.Human PerformanceOverall Crew PerformanceInspection ScopeThe team interviewed the Millstone Unit 2 control room personnelthat responded to theFebruary 12,2011, event, including four]]
SRO s (
SM ,
US , reactivity
SRO , operationsmanager assigned to oversee evolution), two
RO s (
OATC [[]]
RO ,
BOP [[]]
RO ), the

STA andthe Reactor Engineer to determine whether these personnel performed their duties inaccordance with plant procedures and training. The team also reviewed narrative logs,sequence of events and alarm printouts, condition reports, PPC trend data, proceduresimplemented by the crew, and procedures regarding roles and responsibilities ofoperations personnel.Enclosure

8b. Findinqs/ObservationsMultiple Examples of Procedural Violations and Inadequate Procedures Relatinq toControl Room Crew Performance Durinq a Plant Transientlntroduction: A self-revealing finding was identified involving the failure of Millstonepersonnel to carry out their assigned roles and responsibilities and poor reactivitymanagement during main turbine control valve testing on February 12,2011, whichcontributed to the unanticipated reactor power increase. Specifically, the Millstone Unit 2operations crew failed to implement written procedures that delineated appropriateauthorities and responsibilities for safe operation and shutdown and a procedure forcontrolling reactor reactivity. In addition, the licensee failed to establish writtenprocedures for the

RPS [[]]
VHT [[setpoint reset and for power operation and transientsinvolving multiple reactivity additions.The finding has preliminarily been determined to be White, or of low to moderate safetysignificance. The finding is also associated with two apparent violations of]]
NRC on Load Set control. Operators were in the process of placingturbine first stage pressure feedback in service.During the conduct of the main turbine control valve testing, multiple operators failed tocorrectly implement written procedures as described below:a. Dominion Procedure]]
OP -AP-300, "Reactivity Management," states the ReactorOperator will stop and question unexpected situations involving reactivity, criticality,power level, or core anomalies and will meet the anomalous indication withconservative action. Dominion Procedure
OP -
AA -106, "lnfrequently Conducted orComplex Evolutions," establishes expectations for the need to stop the test orevolution when unexpected conditions arise or unexpected behavior is experienced.However, as the
BOP [[]]
RO placed turbine first stage pressure feedback in service, henoted an increase in first stage pressure and incorrectly pressed the turbine load setINCREASE pushbutton instead of the
DECREA [[]]
SE pushbutton. When the
BOP [[]]
RO did not get the desired response, he depressed the
INCREA [[]]
SE pushbutton threemore times, followed by two depressions of the
DECREA [[]]
SE pushbutton, rather thanstopping in the face of uncertainty as expected. The actions by the
BOP [[]]

RO resultedin a rapid, unintended reactor power rise.Enclosure

b.IDominion Procedure

OP -
AP -300, "Reactivity Management," states the ShiftTechnical Advisor will provide engineering expertise to shift operators, as required,during periods of significant reactivity changes. However, the
STA was peer-checking the turbine manipulations and did not identify that the
BOP [[]]
RO actionswere incorrect. Because the
STA [[was dedicated to supporting the turbine evolutionas the peer checker, he was unable to remain within his assigned role and did notprovide his engineering expertise to the crew regarding the multiple inappropriatereactivity additions by other members of the crew.Dominion Procedure]]
OP -
AA -100, "Conduct of Operations," states the UnitSupervisor will provide oversight of plant operations and ensure the plant is operatedsafely in accordance with procedures. Dominion Procedure
OP -
AP -300, "ReactivityManagement," states the Unit Supervisor will direct reactivity changes and ensurereactivity manipulations are made in a deliberate, carefully controlled manner.However, the
US was focused on the turbine evolution during the event and did notprovide effective oversight to the crew in responding to the power rise. The
US alsodid not initially identify that the
BOP [[]]
RO should have been depressing theDECREASE rather than the
INCREA [[]]
SE pushbutton. After the
SM directed the
US toresume his oversight role, the
US did not clearly report to the rest of the crew that apower increase was in progress.Dominion Procedure
OP -AA-100, "Conduct of Operations," states the Shift Managerwill maintain a broad perspective of plant operations as the senior managementrepresentative on shift. However, the
SM did not recognize that turbine operationswere causing changes in plant parameters. He observed the closure of the partiallyopen turbine bypass valve and, believing this to be the result of the effects of fissionproduct poison build-in, directed the
OATC [[]]
RO to lower the turbine bypass valvecontroller setpoint to re-open the valve.Dominion Procedure
OP -AP-300, "Reactivity Management," States the ReactorOperator will stop and question unexpected situations involving reactivity, criticality,power level, or core anomalies and will meet the anomalous indication withconservative action. However, the
OATC [[]]
RO , who was adding positive reactivity bydiluting the
RCS at the time, followed the
SM [['s direction without question andadjusted the turbine bypass valve setpoint to reopen the valve, thereby addingadditional positive reactivity to the core. The Millstone Unit 2 control room crew hadpracticed the control valve testing evolution on the simulator two days prior to theevent with the]]
OATC [[]]
RO monitoring the turbine bypass valve position. This trainingapparently led the
OATC [[]]
RO to think his primary responsibility during the event wasturbine bypass valve monitoring and control rather than his other reactivity controlresponsibilities as the Operator at the Controls.Dominion Procedure
OP -
AP [[-300, "Reactivity Management," States that addingpositive reactivity is never an appropriate way to address unstable plant conditions,and also that it is non-conservative to withdraw control rods in an attempt to restoreprimary coolant temperature during a transient. However, after directing reopening ofthe turbine bypass valve, the]]
SM directed the Reactivity

SRO to withdraw one bankd.e.f.Enclosure

10of control rods four steps to raise reactor temperature. This action added positivereactivity, thereby further exacerbating the power increase.g. Dominion Procedure

OP -
AP -300, "Reactivity Management," states the ReactivitySRO reports to the Unit Supervisor, has no concurrent duties, directly monitors thereactivity change, and will provide peer checks for the reactor operator for allreactivity manipulations. The Reactivity
SRO had been monitoring the rodrepositioning and
RCS dilutions that were performed by the
OATC [[]]
RO as expected.When the
OATC [[]]
RO began monitoring turbine bypass valve position, the ReactivitySRO continued to monitor the ongoing
RCS dilution. The Reactivity
SRO believedthat if he needed to personally manipulate any controls, he would no longer be actingas the Reactivity
SRO. When the
SM directed rod withdrawal, the Reactivity
SRO glanced at a digital readout of
RCS temperature, and, not noticing any change in theparameter, incorrectly concluded the plant was not in a transient and withdrewcontrol rods.h. Dominion Procedure
OP -
AA -106, "lnfrequently Conducted or Complex Evolutions,"states the Senior Operations Manager assigned to oversight of the test will ensuretests are conducted in a manner that maximizes the margin of safety of the Unit. AnSRO-licensed and
SM and for specificactions for power operation and transients involving multiple reactivity additions.Specific examples of these failures are provided below:a. At the onset of the event, the]]
RPS [[]]
VHT setpoints were below 96 percent. During theturbine transient, reactor power increased toward the
VHT setpoints. The ReactivitySRO observed the illumination of the
VHT setpoint reset permissive lights (one lightper
RPS [[channel), and incorrectly assumed they were illuminating due to minorpower fluctuations associated with the fission product poison increase and on-goingdilution. Consequently, he increased the margin to the trip setpoint by resetting theVHT setpoints upward four times during the power rise. lf the]]
SRO had not reset the
VHT , the
RPS would have automatically initiated a high power reactor trip due to themagnitude of the power increase from 88 percent to 96 percent. In addition topreventing the automatic trip, the Reactivity

SRO did not understand or question whyreactor power was increasing, and did not inform anyone on the crew of his actionsto reset the VHT setpoints. The inspection team reviewed existingEnclosure

11station procedures, and determined that there was no procedural prohibition forresetting the

VHT setpoint under any conditions.b. During the turbine steam flow increase power transient event (which introducedpositive reactivity to the reactor), the crew also added positive reactivity by 1) an on-going
RCS [[dilution, 2) opening a turbine bypass valve, and 3) withdrawing controlrods. The inspection team identified that station reactivity management proceduresdid not provide adequate guidance regarding multiple, concurrent, positive reactivityadditions during power operations.Analvsis: The performance deficiency was the failure of Millstone personnel to carry outtheir assigned roles and responsibilities and poor reactivity management during mainturbine control valve testing, which contributed to the unanticipated reactor powerincrease. Specifically, the Millstone Unit 2 operations crew failed to implement writtenprocedures that delineated appropriate authorities and responsibilities for safe operationand shutdown and a procedure for controlling reactor reactivity. In addition, the licenseefailed to establish written procedures for the]]
RPS [[]]
VHT [[setpoint reset and for poweroperation and transients involving multiple reactivity additions. Multiple factorscontributed to this deficiency; however, the primary cause was ineffective reinforcementof Dominion standards and expectations. Traditional enforcement does not apply sincethere were no actual safety consequences, impacts on the]]
NRC [['s ability to perform itsregulatory function, or willful aspects to the finding.The finding is more than minor because the finding was associated with the HumanPerformance attribute of the Initiating Events cornerstone and affected the cornerstoneobjective of limiting the likelihood of those events that upset plant stability and challengecritical safety functions during power operations. Additionally, the]]

PD could be viewedas a precursor to a significant event. Because the finding primarily involved humanperformance errors, probabilistic risk assessment tools were not well suited forevaluating its significance. The team determined that the criteria for using IMC 0609,Appendix M, "significance Determination Process Using Qualitative Criteria," were met,and the finding was evaluated using this guidance as described in Attachment 4 to thisreport. Based on the qualitative review of this finding, regional management concludedthe finding was preliminarily of low to moderate safety significance (preliminary White).The completed Appendix M table is attached (Attachment 4). There were no immediatesafety concerns following the transient because the event itself did not result in powerexceeding license limits or fuel damage. Additionally, interim corrective actions weretaken, which included removing the Millstone Unit 2 control room crew involved in thetransient from operational duties pending remediation, and establishment of continuousmanagement presence in the Millstone Unit 2 control room while long term correctiveactions were developed.This finding had a cross-cutting aspect in the Human Performance cross-cutting area,Decision Making component, because Dominion licensed personneldid not demonstrateadequate operational decision-making, especially when faced with uncertain orunexpected plant conditions. This includes formally defining the authority and roles fordecisions affecting nuclear safety, communicating these roles to applicable personnel,and implementing these roles and authorities as designed H.1(a).Enclosure

2Enforcement: The team identified two apparent violations of Technical Specification 6.8,"Procedures," which states, in part, that written procedures shall be established,implemented, and maintained covering the applicable procedures recommended inAppendix "A" of Regulatory Guide (RG) 1.33, February, 1978. Regulatory Guide 1.33,Appendix "A," Paragraph 1, "Administrative Procedures," requires written procedures forauthorities and responsibilities for safe operation and shutdown as well as general plantoperating procedures appropriate for power operation and transients. Regulatory Guide1.33, Appendix A, Paragraph 3, "Procedures for Startup, Operation, and Shutdown ofSafety-Related

PWR [[Systems," requires, in part, written procedures for changing modesof operation, as appropriate, for the reactor control and protection system. RegulatoryGuide 1.33, Appendix A, Paragraph 5, "Procedures Abnormal, Off-normal, or AlarmConditions," requires, in part, written procedures for other expected transients that maybe applicable.The first apparent violation involved the failure of the Millstone Unit 2 control room crewto implement written procedures that delineated appropriate authorities andresponsibilities for safe operation and shutdown and a procedure for controlling reactorreactivity. As noted in the Description section above, on February 12,2011, the sevenoperators in the control room (4]]
SRO s,
2 RO [[s and 1 non-licensed operator)inadequately implemented Dominion procedures for authorities and responsibilities forsafe operation and shutdown during the performance of main turbine controlvalvetesting. The inappropriate actions of the operators directly contributed to anunanticipated 8 percent increase in Millstone Unit 2 reactor power'The second apparent violation involved the licensee's failure to establish writtenprocedures for the]]
RPS [[]]
VHT setpoint reset and for power operation and transientsinvolving multiple reactivity additions. As noted in the Description section above, onFebruary 12,2011, Dominion did not have written procedures regarding operation of theMillstone Unit 2
VHT setpoint reset pushbuttons (a part of the reactor protection system)during steady-state or plant transient conditions. As a result, during the unanticipatedplant transient on February 12,2011, a Millstone Unit
2 SRO reset the
VHT setpoint atotal of four times without adequate guidance from a plant procedure, thereby prohibitingthe automatic trip that would have occurred, had the
VHT [[setpoint not been reset.Additionally, Dominion did not have an adequate written procedure related to reactivitycontrol regarding multiple concurrent positive reactivity additions during at-poweroperations. Specifically, during the unanticipated reactor transient event, three separatepositive reactivity additions occurred (]]

RCS dilution, manual opening of a turbine bypassvalve, and manual withdrawal of control rods), and the existing procedures did notprovide guidance to address this situation.Following review of the event, the licensee documented the condition in the correctiveaction process (CR 413602). lmmediate corrective actions included removal of theMillstone Unit 2 control room crew involved in the transient from operational dutiespending remediation, issuance of a Standing Order regarding VHT setpoint reset, andestablishment of continuous management presence in the Millstone Unit 2 control roomwhile long term corrective actions were developed.Enclosure

2.213Pending determination of final safety significance, this finding with the associatedapparent violations will be tracked as

AV [[05000336/2011008-01, Multiple Examples ofProceduralViolations and Inadequate Procedures Relating to Control Room CrewPerformance During a Plant Transient.Turbine OperationInspection ScopeThe team interviewed the control room personnel that were directly involved with theturbine load increase during the Febr:uary 12,2011, unanticipated reactor transientevent. The team also reviewed narrative logs, sequence of events and alarm printouts,condition reports,]]
PPC [[trend data, procedures implemented by the crew, and proceduresregarding roles and responsibilities of operations personnel.Find inos/Observationslmproper Operation of Turbine Control Valves During Testinqlntroduction: The inspectors identified a self-revealing finding of very low safetysignificance (Green) for improper operation of the Millstone Unit 2 turbine controls duringturbine control valve testing. Specifically, the inspectors identified that Millstone Unit 2control room operators failed to correctly implement surveillance procedure]]
SP [[-2651N,"Main Control Valve Testing." Incorrect operation of the turbine controls contributed toan unplanned reactor power increase from 88 percent to 96 percent'Description: On February 12,2011, the Millstone Unit 2 control room operatorsincorrectly performed step 4.1 .1 3.c of]]
SP [[-2651 N while conducting main turbine controlvalve testing. This step required the operator to use the turbine load selector pushbuttonto maintain turbine first stage pressure within t10 psig of the initial pressure for thecurrent power level, 88 percent. However, in response to an increasing trend in firststage pressure, the control operators improperly selected "INCREASE" on the turbineload set selector pushbutton instead of "DECREASE". This action caused the turbinecontrol valve to further open and compounded the increasing trend in turbine first stagepressure. The control operators pushed the "INCREASE" pushbutton a total of fourtimes before the operators recognized that they should have, instead, pressed the"DECREASE" pushbutton. The operators subsequently took action to stop the powerincrease and stabilize the plant by depressing the "DECREASE" push button twice. Theunexpected turbine load increase resulted in a plant transient, raising reactor power from88 percent to 96 percent before power was stabilized.The]]
STA conducted peer checking for the control operator during the control valvetesting evolution and the

US closely supervised the operation of the turbine controls.Both individuals failed to identify or correct the mis-operation of the turbine load selector.All three operators then failed to communicate the extent of the plant transient to the SMwhich contributed to additional human performance errors, thereby exacerbating theplant transient.a.b.Enclosure

14Analysis: The team determined that the control room operator's failure to correctlyimplement step 4.1 .13.c of

SP [[-2651 N was a performance deficiency. The cause of thisperformance deficiency was reasonably within Dominion's ability to foresee and correctto ensure proper operator response during turbine control valve testing. Traditionalenforcement does not apply since there were no actual safety consequences, impactson the]]
NRC 's ability to perform its regulatory function, or willful aspects to the finding.The finding is more than minor because it was similar to
NRC [[Inspection ManualChapter 0612, Appendix E, "Examples of Minor lssues," Example 4b, in that theincorrect operation of the turbine load selector pushbutton caused a plant transient.The finding was associated with the Human Performance attribute of the InitiatingEvents cornerstone and affected the cornerstone objective of limiting the likelihood ofthose events that upset plant stability and challenge critical safety functions duringpower operations. Specifically, the mis-operation of the turbine load selector upset plantstability by causing a plant transient that raised reactor power from 88 percent to 96percent. The inspectors conducted a Phase 1 screening in accordance with]]
NRC [[]]
IMCA [[ttachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," anddetermined that the finding was of very low safety significance (Green) because it did notcontribute to both the likelihood of a reactor trip and the likelihood that mitigationequipment or functions would not be available.The inspectors determined that this finding had a cross-cutting aspect in the HumanPerformance cross-cutting area, Resources component, because Dominion did notprovide adequate training of personnel and sufficient qualified personnel H.2(b). Thejust-in-time training (]]
JITT ) for turbine control valve testing had not adequately preparedthe control room operators to respond to a change in turbine first stage pressure. lnaddition, the use of the
STA [[for peer checking, although not prohibited by plantadministrative procedures, had been previously identified during recent (May 2010)licensed operator requalification training in plant-specific operating experience as beinga contributing cause for a plant transient during control valve testing on Unit 3 in 20Q7.Nevertheless, the shift allowed the]]
STA [[, who was not licensed, to be the peer checkerfor this evolution in place of a qualified licensed reactor operator.Enforcement: This finding does not involve enforcement action because no regulatoryrequirement violation was identified. Dominion entered this issue into their correctiveaction program (CR415094) and conducted an]]
RCE to determine corrective actions toprevent recurrence. Because this finding does not involve a violation of regulatoryrequirements and has very low safety significance, it is identified as

FIN05000336/2011008-02, lmproper Operation of Turbine Gontrol Valves DuringTesting.Enclosure

3.3.115Orqanizational Responselmmediate ResponseInspection ScopeThe team interviewed personnel, reviewed various procedures and records, andobserved control room operations to assess immediate response of station personnel tothe unanticipated reactor power transient event.FindinqsNo findings of significance were identified.The team noted that Dominion's initial response to the event was not appropriatelythorough and timely, did not highlight the significance of the unplanned power increaseand reactivity control issues, and was narrowly focused. Following postevent plantstabilization, a crew brief was conducted to assure good common understanding oftransient and to determine whether testing should proceed. However, the crew did notidentify the many human performance issues during the event, including control rodwithdrawal,

VHT [[reset, steam dump operation, multiple communication errors, andincorrect transient diagnoses.lnitially, Dominion personnel incorrectly concluded that Unit 2 reactor power increasedby four percent (rather than the actual eight percent) during the transient. This extent ofpower increase was challenged during immediate post-event discussions betweenbominion managers, but the Dominion management team did not correctly identify theextent of the power rise until the following day. Based on an incomplete and inaccurateinitial assessment of the event, Crew D was allowed to complete the test, return powerto 100% and stand an additional shift in the control room the following day beforeDominion management removed them from operating duties. Although all of Crew Dwas off-shift the following week (per normal shift rotation), two of the individuals involvedin the human performance errors were not formally disqualified from watchstanding untilseveral days after the event, after]]

NRC questioned Dominion's basis for not disqualifyingthose individuals. As of two weeks after the event, Dominion had only generated twocondition reports related to the event and these two condition reports did not address allidentified deficiencies related to the event. See the detailed sequence of events(Attachment 3).Millstone Operations department management issued a new standing order related toVHT setpoint reset. However, a number of weeks elapsed before operating procedureswere revised to provide updated approved plant procedures for the VHT setpointoperation.a.b.Enclosure

3.2b.16Post-Event Root Cause Evaluation and Actionslnspection ScopeThe team reviewed Millstone's

RCE [[Report for the unanticipated reactor power transientevent to determine whether the causes of the event and associated human performanceissues were properly identified. Additionally, the team assessed whether interim andplanned long term corrective actions were appropriate to address the cause(s).FindinqsNo findings of significance were identified.The]]

RCE was thorough and appeared to identify all underlying causal factors. Theassociated proposed corrective actions appeared to adequately address the underlyingcausalfactors. Dominion identified the root cause as an ineffective crew performancemanagement program. The identified contributing causes and issues included:. lmproper implementation of standards and fundamental work practices by thecrew;. Operator knowledge weakness related to understanding main turbine operation;. Inadequate guidance for VHT setpoint reset;. Inadequate pre-job briefs;. Inadequate just-in{ime training;. Weaknesses in test procedure guidance for controlling first stage pressure; ando Lack of guidance on control of multiple concurrent reactivity additions.Meetinos. lncludinq ExitExit Meetinq SummarvOn April 14,2011, the team discussed the inspection results with Mr. A. J. Jordan, SiteVice President, and members of his staff. The team confirmed that proprietaryinformation reviewed during the inspection period was returned to Dominion.40A6Enclosure

Dominion PersonnelL. ArmstrongD. BajumpaaB. BartronC. ChapinW. ChesnutS. ClaffeyT. ClearyG. ClosiusK. GroverJ. HamptonA. JordanR. MacManusG. MarshallH. McKenneyJ. RileyR. RileyJ. SemancikC. TanC. ZornOthersD. Galloway1-1SUPPLEMENTAL

INFORM [[]]
ATIONK EY
POINTS [[]]
OF [[]]
CONTAC [[]]
TM [[anager, TrainingNuclear Safety AnalystSupervisor, LicensingAssistant Operations ManagerSupervisor Nuclear Shift Operations Unit 2Reactor EngineerLicensing EngineerLicensing EngineerManager, OperationsSimulator TesterSite Vice PresidentDirector, Nuclear Station Safety & LicensingManager, Outage and PlanningSupervisor Shift Operations SupportLead Instructor - Unit 2 Operator Requalification TrainingSupervisor of Nuclear Shift Operations Unit 3Plant ManagerSimulation EngineerTurbine System EngineerProgram Supervisor, Connecticut Department of EnvironmentalProtection, Bureau of Air Management, Radiation DivisionLIST]]
OF [[]]
ITEMS [[]]
OPENED ,
CLOSED ,
AND [[]]
DISCUS SEDAVMultiple Examples of Procedural Violations andInadequate Procedures Relating to Control RoomCrew Performance During a Plant Transient(Section 2.1)lmproper Operation of Turbine Control ValvesDuring Testing (Section 2.2)LIST
OF [[]]
DOCUME NTS
REVIEW [[]]
ED cR415089 cR415096cR415091 cR415097cR415094
CR 415104Opened05000336/201 1 008-0105000336/2011008-02Condition Reports (

CR)cR413602cR415944cR415087FINAttachment 1

1-2SUPPLEMENTAL

INFORM [[]]
ATIONS tandinq OrderSO-11-04 (Retating to
VHT setpoint reset)Procedures
MP -PROC-OPS-SP 2651N, "Main Control Valve Operability Test," Rev 004-03MP-PROC-OPS-OP 2204, "Load Changes," Rev 023-06MP-PROC-000-AD-AA-102, "Procedure Use and Adherence," Rev
4MP -
PROC -OPS-OP 2304C, "Make Up (Boration and Dilution) Portion of
CVCS ," Rev 023-03
MP -PROC-000-OP-AA-100, "Conduct of Operations," Rev
11MP -
PROC -000-OP-AP-300, "Reactivity Management," Rev 1
1MP -
PROC -000-OP-AA-106, "lnfrequently Conducted or Complex Evolutions," Rev
5MP -
GARDMP -000-OP-AA-1 800, "Operator Fundamentals," Rev 2MiscellaneousControl Room Operations Narrative LogsUnit 2 Sequence of Events Recorder Printout for February 12,2011Unit 2 Alarm History Printout for February 12,2011Root Cause EvaluationRoot Cause Evaluation
RCE 001044, "Unplanned 8% Reactor Power Excursion"
ADAMSA VBOP
ROCFRC [[]]
RCVDRP DRSHEPtMcJITTMTMWNRCOATC
RO oMoc
PARSPD PPCPRApsigRCERCSRELIST
OF [[]]
ACRONY [[MSAgency-wide Documents Access and Management SystemApparent ViolationBalance of Plant Reactor OperatorCode of Federal RegulationsCondition ReportControlValveDivision of Reactor ProjectsDivision of Reactor SafetyHuman Error ProbabilityInspection Manual ChapterJust in Time TrainingMain TurbineMegawattNuclear Regulatory CommissionOperator at the Controls Reactor OperatorOperations Manager on CallPublicly Available RecordsPerformance DeficiencyPlant Process ComputerProbabilistic Risk Assessmentpounds per square inch gaugeRoot Cause EvaluationReactor Coolant SystemReactor EngineerAttachment 1]]
RGRORP [[]]
SSDPSM SROSITSTATSUSVCTVHT1-3SUPPLEMENTAL
INFORM [[]]
ATIONR [[egulatory GuideReactor OperatorReactor Protection SystemSignificance Determination ProcessShift ManagerSenior Reactor OperatorSpecial Inspection TeamShift Technical AdvisorTechnical SpecificationUnit SupervisorVolume ControlTankVariable High Power TripAttachment 1]]
MEMOMN [[]]
DUM [[]]
TO [[:]]
FROM SUBJECT:2-1SPECIAL
INSPEC [[]]
TION [[]]
TEAM [[]]
CHARTE RUNITED
STATES [[]]
NUCLEA R
REGULA [[]]
TORY [[]]
COMMIS [[]]
SIONRE GION I475
ALLEND [[]]
ALE [[]]
ROADKI [[]]
NG [[]]
OF [[]]
PRUSSI A,
PA 19406-1415
SPECIA L
INSPEC [[]]
TION [[]]
TEAM [[]]
CHARTE RFebruary 18,2011Samuel
L. HansellJr., ManagerSpecial Inspection TeamPeter A. Presby, LeaderSpecial lnspection TeamPeter R. Wilson, Acting Director /
RA /Division of Reactor SafetyDarrell
J. Roberts, Director /
RA /Division of Reactor ProjectsSPECIAL
INSPEC [[]]
TION [[]]
TEAM [[]]
CHARTE R -MILLSTONE
POWER [[]]
STATIO N
UNIT 2
OPERAT ORPERFORMANCE
DURING [[]]
MAIN [[]]
TURBIN E
CONTRO L
VALVET [[]]
ESTING [[]]
ON [[]]
FEBRUA [[RY 12,2011ln accordance with Inspection Manual Chapter (lMC) 0309, "Reactive Inspection Decision Basisfor Reactors," a Special Inspection Team (SlT) is being chartered to evaluate operatorperformance and organizational decision-making during a Millstone Power Station Unit 2 mainturbine control valve test on February 12,2011. The decision to conduct this special inspectionwas based on meeting the deterministic criteria (involved questions or concerns pertaining tolicensee operational performance) specified in Enclosure 1 of]]
IMC [[0309, and in accordance withSection 04.04, "Additional Factors That May Warrant an llT, AlT, or SlT." The risk associatedwith this event was not amenable to probabilistic risk analysis. The absence of a calculableincrease in conditional core damage probability (]]

CCDP) is based upon the inability toreasonably and accurately approximate the human performance reliability attributes associatedwith the operator performance that precipitated the unanticipated reactor power level changes.IMC 0309, Section 04.04 states that, "factors such as openness, public interest, and publicsafety should be appropriately considered by NRC when deciding whether to dispatch an llT,AlT, or SlT.".Attachment 2

2-2SPECIAL

INSPEC [[]]
TION [[]]
TEAM [[]]
CHARTE RThe
SIT will expand on the inspection activities started by the resident inspectors andaugmented by a Division of Reactor Safety (
DRS [[) inspector who was dispatched to the sitesoon after the event. The Team will review the causes of the event, and Dominion'sorganizational and operator response during the event. The Team will perform interyiews, asnecessary, to understand the scope of operator actions performed during the event. The Teamwill also assess whether the]]
SIT should be upgraded to an Augmented lnspection Team inaccordance with
IMC [[]]
0309.T he inspection will be conducted in accordance with the guidance contained in
NRC [[InspectionProcedure 93812, "Special lnspection," and the inspection report will be issued within 45 daysfollowing the final exit meeting for the inspection.The special inspection will commence on February 22,2011. The following personnel havebeen assigned to this effort:Manager:Team Leader:Team Members:Enclosure: Special lnspection Team CharterSamuel]]
L. Hansell, Jr., Branch ChiefOperations Branch,
DRS , Region
IP eter A. Presby, Senior Operations EngineerOperations Branch,
DRS , Region
IB rian C. Haagensen, Millstone Power Station Resident InspectorDivision of Reactor Projects (
DRP ), Region
IB rian J. Fuller, Operations EngineerOperations Branch,

DRS, Region IAttachment 2

2-3SPECIAL

INSPEC [[]]
TION [[]]
TEAM [[]]
CHARTE [[RSpecial Inspection Team CharterMillstone Power StationUnit 2 Operator Performance During Main Turbine ControlValveTesting on February 12,2011Backqround:Based on preliminary information, the following is a description of the event. On Saturday,February 12,2011, Millstone Power Station Unit 2 reduced power to 88 percent for main turbinecontrol valve testing. ln preparation for the test, Dominion procedure]]
SP 2651N, "Main ControlValve Operability Test," provides written instructions for the operators to slowly rotate theturbine first stage pressure feedback potentiometer from the "
OUT " to the "lN" position over aone minute period while maintaining turbine first stage pressure by using the "LOADSELECTOR
INCREA [[]]
SE and
DECREA [[]]
SE ' pushbuttons. As the Balance of Plant (BOP)Reactor Operator (RO) rotated the turbine first stage pressure potentiometer, turbine first stagepressure and reactor power increased. The
BOP [[]]
RO [[incorrectly went to increase instead ofdecrease on the load selector button. When he did not get the desired response, he pressedthe increase button at least two more times. The Shift Technical Advisor, who was acting asboth the peer checker and the Control Room Supervisor directing the evolution, did notapparently detect the incorrect manipulation and did not correct the]]
BOP [[]]
RO. [[The increasedsteam demand lowered reactor coolant average temperature (Tavg) and caused a powerincrease to 96 percent power over 90 seconds. While the transient was occurring, the VariableOver Power Trip (VOPT) reset lights were illuminated. The crew reset the]]
VOPT several timesduring the event.The Shift Manager recognized that a transient was occurring and directed the
BOP [[]]
RO [[to stophis actions. He directed the reactivity Senior Reactor Operator to withdraw control rods foursteps to stabilize Tavg while temperature was decreasing, an action that compounded thepower increase. After Tavg and reactor power were stabilized, the main turbine control valvetest was completed and Unit 2 was returned to 100 percent power.Currently, Millstone Unit 2 is in Mode 1 at normal operating pressure and temperature. Therewas no impact to Unit 3. Dominion is currently investigating the operators' response to thisevent. Additionally, Dominion has suspended the qualifications of the operations crew while theinvestigation continues. The]]
NRC resident inspectors and a
DRS senior operations engineerhave provided follow-up to this event under the Reactor Oversight Process (
ROP ) baselineinspection program.Basis for the Formation of the
SIT The

IMC 0309 review concluded that one of the deterministic criteria was met due to questionsor concerns pertaining to licensee operational performance. This criterion was met based onhuman performance errors that occurred and led to the unanticipated reactor power excursion.The human performance errors included:. Depressing the increase button on the load selector instead of decrease;r Inadequate self and peer checking;o The addition of positive reactivity (control rod withdrawal) while reactor power wasalready increasing, without understanding the nature of the transient;Attachment 2

2-4SPECIAL

INSPEC [[]]
TION [[]]
TEAM [[]]
CHARTE R. Manipulating control rods while in an oversighUsupervisory role; andr Resetting the
VOPT setpoint during a transient, without understanding the nature of thetransient.ln accordance with
IMC [[0309, the event was evaluated for risk significance because onedeterministic criterion was met. However, the risk associated with this event was not amenableto probabilistic risk analysis. The absence of a calculable increase in conditional core damageprobability (CCDP) is based upon the inability to reasonably and accurately approximate thehuman performance reliability attributes associated with the operator performance thatprecipitated the unanticipated reactor power level changes.f]]
MC 0309, Section 04.04 states that, "factors such as openness, public interest, and publicsafety should be appropriately considered by
NRC [[when deciding whether to dispatch an llT,AlT, or SlT." In light of the aforementioned human performance errors, and consistent withSection 4.04, Region I has decided to initiate an SlT.Obiectives of the Special Inspection:The Team will review the causes of the event, and Dominion's organizational and operatorresponse during the event. The Team will perform interviews, as necessary, to understand thescope of operator actions performed during the event.To accomplish these objectives, the team will:1. Develop a complete sequence of events including follow-up actions taken byDominion, and the sequence of communications within Dominion and to the]]
NRC [[subsequent to the event;2. Review and assess crew operator performance and crew decision making, includingtheir adherence to expected roles and responsibilities, including the command andcontrolfunction associated with reactivity manipulations, the use of procedures, logkeeping, and overall communications;3. Evaluate the extent of condition with respect to the other crews;4. Determine the appropriateness and safety significance of resetting the]]

VOPTsetpoint during this event;5. Evaluate the effectiveness of supervisory oversight of Senior Reactor Operators(SROs) in light of the on-duty Shift Manager directing the Reactivity Oversight SROto manipulate control rods while in the oversight role;6. Review and assess the effectiveness of Dominion's response to this event andcorrective actions taken to date. This includes overall organizational response, theroot cause evaluation, and adequacy of immediate, interim and proposed longtermcorrective actions;Attachment 2

2-5SPECIAL

INSPEC [[]]
TION [[]]
TEAM [[]]
CHARTE [[R7. Review the adequacy of operator requalification training as it relates to this event,including the integration of newly licensed operators into the operator requalificationtraining program;L Assess the decision making and actions taken by the operators to determine if thereare any implications related to the site's safety culture;L Evaluate_ Dominion's application of pertinent industry operating experience,including]]
INPO [[]]
SOER [[1Q-2, "Engaged, Thinking Organizations," to assess theeffectiveness of any actions taken in response to the operating experience; and10. Document the inspection findings and conclusions in a Special Inspection Team finalreport within 45 days of inspection completion.Guidance:lnspection Procedure 93812, "Special Inspection", provides additional guidance to be used bythe SlT. Team duties will be as described in Inspection Procedure 93812. The inspectionshould emphasize fact-finding in its review of the circumstances surrounding the event. Safetyconcerns identified that are not directly related to the event should be reported to the Region Ioffice for appropriate action.The team will conduct an entrance meeting and begin the inspection on February 22,2011.While on-site, the Team Leader will provide daily briefings to Region I management, who willcoordinate with the Office of Nuclear Reactor Regulation, to ensure that all other pertinentparties are kept informed. The Team will also coordinate with the Region / State Liaison Officerto implement the Memorandum of Understanding between the]]
NRC [[and the State ofConnecticut to offer observation of the inspection by representatives of the state. A reportdocumenting the results of the inspection will be issued within 45 days following the final exitmeeting for the inspection.Before the end of the first day onsite, the Team Manager shall provide a recommendation to theRegional Administrator as to whether the]]

SIT should continue or be upgraded to an Augmentedlnspection Team response.This Charter may be modified should the team develop significant new information that warrantsreview.Attachment 2

3-1DETAILED

SEQUEN [[]]
CE [[]]
OF [[]]
EVENTS [[February 12,2011 Power Transient EventThe team constructed the sequence of events fromplant process computer (PPC) data (alarm printout,graphs) and plant personnel interviews.a review of Control Room narrative logs,sequence of event printout, plant parameterMILLSTONE]]
UNIT 2
EVENT [[]]
TIMELI [[]]
NEC [[lock Time[date](hr:mm:ss)Event TimeDescription2110111Sperations Crew D attends four hour simulator just-in-time trainingsession to prepare for scheduled quarterly main turbine (MT) valve:esting. Partial evolution pre-job brief conducted.211211106:00Operations Crew D assumes the day shift watch. Unit 2 is in]]
MODE 1, 1A0% reactor power.07:50Quarterly main turbine (
MT ) stop valve testing complete.08:33Pre-job briefing for the downpower,
MT controlvalve (
CV ) testing,and up-power. Personnel in attendance for brief, and alsoihroughout the downpower and control valve testing:management to provide oversight for the reactivityevolutionssupervisor)(oATC
RO )
RO )08:593ommence downpower for
MT [[valve testing per reactivity plan.10:15Stabilize plant at 88% power, following 173 gallons boration, control"od insertion from 180 steps to 158 steps and turbine load reduction.rsing load limit.10:35102 gallon dilution to maintain steady Reactor Coolant System]]
RCS ) temperature during build-in of fission product poisons.10:44100 gallon dilution.10:53150 gallon dilution,11:02150 gallon dilution.11:06CATC RO begins 600 gallon dilution.Attachment 3
MILLST [[]]
ONE [[]]
UNIT 2
EVENT [[]]
TIMELI [[]]
NEG [[lock Time[date]{hr:mm:ss)Event TimeDescription11:193OP]]
RO shifts turbine load controlfrom Load Limit to Load Set.11:20
OATC [[]]
RO adjusts turbine bypass valve setpoint to open'A turbinebypass valve to 10% open.
BOP [[]]
RO adjusts main turbine load tomaintain
RCS temperature.
US ,
BOP [[]]
RO and
STA discuss andiointly agree on a planned action, to depress the Load SetINCREASE button, if l"tstage pressure increases while placing 1"'stage pressure feedback in service.11:24:42Start letdown diversion to waste to lower
VCT level 89o/o to 79o/o.11:26:15
BOP [[]]
RO , with peer checks from
STA and direct observation by
US ,regins to place 1" stage feedback in service and depresses .
INCREA SE pushbutton multiple times in response to rising 1"'stage pressure.11:26:3203ontrol valves begin opening. Beginning of transient. Conditions:RCS Tcold 542.8"F,
MT [[]]
CV position 38.1% open.
MT first stage)ressure 476 psig.11:26:4412 sec
RCS Tcold is decreasing.11:27:341 min, 2 secA' turbine bypass valve fully closes.11:27:561 min, 24 secReactivity
SRO resets ChannelA Variable High Power Trip (
VHT ).- 11:28:001 min, 28 secSM directs
OATC [[]]
RO to lower turbine bypass valve setting to re-)pen 'A' turbine bypass valve. Tcold approximately 541.5"F.11:28:021 min. 30 sec600 gallon dilution is comPlete.11:28:181 min. 46 sec)ATC
RO adjusts'A'turbine bypass valve setpoint. Valve opens to2% open position for approximately 6 seconds and then reclosesrutomatically.11:28:402 min. 8 secleactivity
SRO resets ChannelA
VHT (2nd time during transient).- 11:28:402 min. 8 seciM directs
US to return to position of oversight, away from the,urbine control panel.11:28:402 min. 8 secl-urbine 1" stage pressure is about 524 psig, up from 476 psig priorro transient.
US recalled later that at this point the Load Set
NCREAS E pushbutton had been depressed 4 times and the Loadiet
DECREA [[]]
SE pushbutton had been depressed 2 times.11:28:442 min, 12 sec?eactivity
SRO withdraws Group 7 Control Element Assemblies.control rods) 4 steps per
SM direction. Tcold approximatelyi38.7'F. Neither
SM nor Reactivity
SRO are aware of turbine loadncrease and temperature transient in progress.11:29:142 min. 42 secfurbine load stabilizes at new setpoint on Load Set. Control valves'each maximum open during transient al70.5o/o open position'11:29:182 min, 46 secleactivity
SRO resets Channel A
VHT (3'd time during transient)'3-2DETAILED
SEQUEN [[]]
CE [[]]
OF [[]]
EVENTS Attachment 3
MILLST [[]]
ONE [[]]
UNIT 2
EVENT [[]]
TIMELI [[]]
NEC [[lock Time[date](hr:mm:ss)Event TimeDescription11:29:282 min. 56 secfcold reaches minimum during transient at 537.5"F. Minimumrressurizer pressure is 2238 psia.11:29:323 min, O secleactivity]]
SRO resets ChannelA
VHT 14h time during transient).leactor power stabilized al -960/o.11:30:56itop letdown diversion to waste.11:31:563OP
RO shifts turbine load controlfrom Load Set to Load Limit.11:32:18leactivity
SRO resets Channel A
VHT. 11:35:52Reactivity
SRO resets ChannelA
VHT. -11:37l-urbine load gradually reduced by the operator to restore
RCS [[[cold to program value.-11:50furbine load stabilized at pre-event level.-12:0034 miniM calls his immediate supervisor (Senior Unit 2 Licensedndividual). The]]
SM characterizes the event as a 4o/o increase in'eactor power. After discussion, both agree, okay to complete
MT )V testing.12:18lurbine load control transferred to Load Set.-12:30iM calls immediate supervisor again. During this call, discussion'eveals
SM mistakenly believed the
SM -qualified individualrssigned by operations management to provide oversight for the'eactivity evolutions, who was in the control room, was fulfilling the'oll of Operations Manager on Call (OMOC). The immediate;upervisor directed the
SM to inform the actual
OMOC of the event.12:33Recommenced main turbine control valve stroking satisfactorily.-12:40Ihr, 14 minSM briefs
OMOC on the event (estimated time from
SM 'ecollection).12:55t hr. 29 minfMOC informs Assistant Operations Manager.12:563ompleted main turbine control valve stroking.-13:04t hr. 38 min\ssistant Operations Manager calls Operations Manager.13:063OP
RO returns turbine load controlto Load Limit.-13:252 hrsVlanagement conference call between Plant Manager, OperationsVanager, Assistant Operations Manager,
SM , Operations\rlanagement oversight person on shift. Discussed event aslnderstood at the time (single human performance error associatedrvith turbine load increase button causing a 4o/o power increase).)ecided to have
SM meet with mgmt team following morning to'ully debrief on the occurrence. Rearranged watch bill toaccommodate
SM debrief.DETAILED
SEQUEN [[]]
CE [[]]
OF [[]]
EVENTS Attachment 3
MILLST [[]]
ONE [[]]
UNIT 2
EVENT [[]]
TIMELI [[]]
NEC [[lock Time[date]{hr:mm:ss)Event TimeDescription-15:153.8 hrs\nother operations management conference call (estimated time/Jetails from Assistant Operations Manager recollection) betweenCps Manager, Assistant Ops Manager,]]
OMOC , the other twosenior Unit 2 ops mgmt licensed individuals and a
SM not currentlyrn shift. Decided to have the on-shift
SM meet with mgmt teambllowing morning (211312011) to fully debrief on the occurrence.Rearranged the dayshift watch bill to accommodate
SM debrief. A'eactor engineer was assigned during the evening shift to review:vent data for use the following day in reconstruction of the)ccurrence.15:38Srew D commences power increase to return Unit 2 to full power.17:055.5 hrsIhe
OMOC contacts one of the
NRC [[Resident Inspectors andnforms him of a human performance error during valve testingryhich resulted in approximately 4oh power rise, with no reactor trip,ro safety limits exceeded and that Dominion would be investigating'urther tomorrow.17:45Unit 2 returned to 100% reactor power.-18:003rew D relieved by on-coming night shift crew.23:0511.5 hrsReactor engineering email to Operations management team,:ontaining Unit 2 plant process computer data and summarydentifying transient details of 8% power change magnitude (not 4o/oas originally characterized), inappropriate rod withdrawal, andrariable high power trip setpoint resets.2113111-06:00lrew D assumes the dayshift watch from the night shift crew.2113111-15:0027.5 hrsCps Manager and Assistant Operations Manager update the]]
NRCS [[enior Resident Inspector that event was more serious thanrriginally realized, Station management considering pulling the;rew off-shift and a senior operations management licensedndividual observing remainder of dayshift operations until Crew Ds relieved at 18:00.2t13t11-18:00lrew D relieved by on-coming night shift crew.2114111-10:0046.5 hrs)perations Manager informs]]
NRC resident staff that Crew Dlualifications have been suspended. Crew will meet withnanagement to analyze the event to evaluate the exhibitedrerformance issues.3-4DETAILED
SEQUEN [[]]
CE [[]]
OF [[]]

EVENTSAttachment 3

1.2.3.4-1IMC 0609,

APPEND [[]]
IX M,
TABLE 4.1Qualitative Decision-Making Attributes for
NRC Management ReviewThe
SDP is the preferred path for determining the significance of findings in the ReactorOversight Process.
IMC 0609 Appendix M is provided for use when the existing
SDP guidance is not adequateto provide a reasonable estimate of the significance.
IMC [[0609 Appendix M could be used for this case. Appendix M utilizes a qualitativesignificance determination process focused on the below table where 6 of 8 attributes havesome level of applicability.Decision AttributeApplicabletoDecision?Basis for Input to Decision - Provide qualitativeand/or quantitative information for managementreview and decision making.Finding can be boundedusing qualitative and/orq uantitative information?NoThe at-power safety significance determination process,IMC 0609 Appendix A, quantitative analysismethodology is not adequate to provide reasonableestimates of the finding's significance. That]]
SDP [[doesnot model errors of commission and does not provide amethod of accurately estimating changes to the humanerror probabilities caused by errors of omission. As aresult, no quantitative risk evaluation can be performedfor this finding.Human errors have the potential to increase the humanerror probability (]]
HEP ) for credited operator actions.The probabilistic risk assessment models are highlysensitive to smallvariations in
HEP changes. Theexisting
PRA research does not currently support amethod for varying the performance shaping factors inresponse to defined error forcing contexts. lt is notpossible to calculate a valid single point risk estimate.Human performance is a very large contributor to
PRA [[uncertainty.Defense-in-Depthaffected?YesThe term "defense in depth" is commonly associatedwith the maintenance of the integrity and independenceof the three fission product barriers. The fission productbarriers were not actually compromised by the actionsof the crew during this event. While the Reactivity]]

SROreset the VHT and prevented a reactor trip fromoccurring, a reactor trip was not actually required toprotect the core during this event. The fuel barrier wasnot actually jeopardized by the crew's actions.On the other hand, the crew plays a vital role in theAttachment 4

4-2IMC 0609,

APPEND [[]]
IX M,
TABLE [[4.1Decision AttributeApplicabletoDecision?Basis for Input to Decision - Provide qualitativeand/or quantitative information for managementreview and decision making.maintenance of defense in depth from the perspectivethat they operate station controls. Human errors havethe potentialto compromise the three fission productbarriers. The commission of multiple unforeseenhuman errors in a short period of time during the turbinevalve testing was clearly related to a loss of situationalawareness and a failure to maintain the roles andresponsibilities assigned under the Dominionad ministrative procedures.Performance Deficiencyeffect on the SafetyMargin maintained?YesPlant safety analyses credit the variable high-power tripsetpoint for some events when determining boundingcases. The Final SafetyAnalysis Report Chapter 14safety analysis considers a similar event (a 10o/o powerincrease from a turbine control valve failing full open at100To power) that actually bounds this event where thecore is protected from fuel damage.Operator response to this event reduced the margin tothe reactor trip setpoint. Operators unintentionallyraised turbine load and then, in response, intentionallyopened a turbine bypass valve, raised the]]
VHT setpoints and withdrew control rods.However, the flux distribution remained bounded by thesafety analysis and
RPS actuation was not actuallyneeded to prevent exceeding the departure fromnucleate boiling or fuel centerline temperature designlimits.Operator action, post-event interviews and lack ofprocedural guidance for
VHT [[reset all indicate likelihoodthat other Unit 2 operators may have similarly resetVHT when a reset permissive light illuminates duringpower transient events where the underlying cause isnot immediately apparent. Under differentcircumstances, there is potential for exceedingacceptable fuel design limits if the]]
VHT were resetduring an event with a higher magnitude steam flowincrease and core peaking factors closer to operatinglimits. However, the potential for the event to progressto a core damage state due to operators incorrectly andcontinually resetting the

VHT is unlikely becauseredundant reactor trips (thermal margin/low pressureAttachment 4

Decision AttributeApplicabletoDecision?Basis for Input to Decision - Provide qualitativeand/or quantitative information for managementreview and decision making.and local power density trips) would limit the powerincrease.The extent theperformance deficiencyaffects other equipment.YesThe failure of the Unit 2 crews to remain within theirassigned roles and responsibilities has the potential toaffect the operation of equipment that requires operatormanual action to function. Other Unit 2 crews displayeda degree of degraded performance in the area ofconduct of operations based on post-eventassessment.Dominion documented a number of post-event issuesrelated to human performance by the other Unit 2operating crews. These issues were observed bylicensee management personnel during the three weekperiod immediately following the power transient eventand demonstrate the pervasiveness of the performancelapses of the Unit 2 control room operators. lmproperprocedure use and improper peer checking were readilyidentified behaviors on multiple Unit 2 crews.lneffective just-in-time training and procedureinadequacies were also factors that degraded all thecrews'ability to operate the plant.Degree of degradation offailed or unavailablecomponent(s).N/APeriod of time (exposuretime) affect on theperformance deficiency.YesWith respect to this specific event, Reactor CoolantSystem cold leg temperature began lowering at11:26:44 on 21121201 1. The first

VHT [[setpoint resetoccurred at 11:27:56. Reactor power stabilized at 96%at 11:29:32. The entire event lasted approximately 3minutes.With respect to the latent issues underlying thisperformance deficiency, the exposure time isindeterminate, but clearly developed over an extendedperiod. The procedural and training performanceweaknesses specified above existed for many years.The Dominion root cause evaluation team determinedthat the causal factors for the event had existed for a]]
IMC 0609,
APPEND [[]]
IX M,
TAB [[]]

LE 4.1Attachment 4

4-4IMC 0609,

APPEND [[]]
IX M,
TABLE [[4.1Decision AttributeApplicabletoDecision?Basis for Input to Decision - Provide qualitativeand/or quantitative information for managementreview and decision making.considerable period of time. However, they did notquantify the exposure time.The likelihood that thelicensee's recoveryactions wouldsuccessfully mitigate theperformance deficiency.YesThe licensee's root cause analysis was thorough andappeared to identify all underlying causalfactors. Theassociated proposed corrective actions appear toadequately address the underlying causal factors.During the recent April 2011 Unit 2 refueling outage,there were no significant configuration control issues,and no]]
NRC [[or self-revealing findings or violations.Resident inspectors have observed improvedprocedure adherence and an improvement in humanperformance since the Special lnspection in February2011.Additional q ualitativecircumstancesassociated with thefinding that regionalmanagement shouldconsider in theevaluation process.YesDuring this event, all control room operators on thecrew failed to either recognize or respond properly tothe unintended power transient. None of the operatorsinitially identified the breakdowns in command andcontrol or the deviations from defined roles andresponsibilities as worthy of note in the immediate post-event brief or in discussions regarding whether it wasappropriate to continue with the turbine testing (otherthan to identify that the event was initiated by theturbine operator's action to press the increase, ratherthan the decrease pushbutton).Dominion was initially slow to recognize the scope andthe significance of the event. Despite involvement ofmultiple layers of licensee management personnelduring and immediately following the event, numerousperformance problems during the event were not fullyrecognized until the next day after the event. Theinadvertent power rise was initially assessed as 4o/o,vice the actual 8% because the operators used neutronflux instead of Q-power as the indicator of powerincrease. Actions taken to withdraw reactor controlrods, reset]]
VHT setpoints, and open the turbine bypassvalve were not identified as inappropriate until a reactorengineering review of plant computer data many hoursafter the event.

NRC inspector challenges of licenseemanagement decisions relating to the event precededAttachment 4

4-5IMC 0609,

APPEND [[]]
IX M,
TABLE 4.1Decision AttributeApplicabletoDecision?Basis for Input to Decision - Provide qualitativeand/or quantitative information for managementreview and decision making.Dominion's disqualification of some of the operatingcrew members.
NRC questions led to recognition bylicensee that multiple concurrent positive reactivityadditions were not adequately addressed by stationprocedures.
NRC challenged the licensee's limitedinitial use of the condition reporting and procedurechange process in response to this event.Following the event, licensee operations managementissued a Standing Order to address when acceptable toreset the
VHT [[setpoints. However, Dominion delayedmaking any related changes to permanent plantprocedures.Dominion provided training on recent significantindustry reactivity control events. This training wasconducted in the training cycle immediately precedingthe February 2011 power transient event and wasadministered to all Millstone station supervisors,including the supervision of Operations Crew D. Thehuman performance errors exhibited during the eventindicate this training was not effective.Attachment 4]]