IR 05000004/2000002
| ML033010576 | |
| Person / Time | |
|---|---|
| Site: | Harris, 05000004 |
| Issue date: | 01/24/2003 |
| From: | Ogle C NRC/RGN-II/DRS/EB |
| To: | Scarola J Carolina Power & Light Co |
| References | |
| FOIA/PA-2003-0358 IR-02-011 | |
| Download: ML033010576 (34) | |
Text
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--.4 aspx 24UNITED STATES tA
°tNUCLEAR REGULATORYZCOMMISSION
SUBJECT:
SHEARON HARRIS NUCLEAR PLANT - NRC INSPECTION REPORT 50-400/02-11
Dear Mr. Scarola:
On December 20,2002, the Nuclear Regulatory Commission (NRC) completed a triennial fire protection inspection at your Shearon Harris Nuclear Plant. The enclosed inspection report documents the inspection findings which were discussed on that date with you and other members of your staff.
The Inspection examined the effectiveness of activities conducted under your license relating to implementation of your NRC-approved fire protection program. The Inspectors reviewed selected procedures and records, observed activities, and Interviewed personnel.
Based on the results of this inspection, the Inspectors Identified eight Issues of very low safety significance (Green). Each of these issues was determined to Involve a violation of NRC requirements. However, because of their very low safety significance and because they have been entered Into your corrective action program, the NRC is treating these issues as Non-Cited Violations (NCVs), In accordance with Section VI.A.1 of the NRC's Enforcement Policy.
In addition, while three of these findings are related to your corrective action for the previous violation associated with the Thermo-Lag fire barrier assembly between the '8' train switchgear room/auxiliary control panel room and the A train cable spreading room, that violation will be closed because the net effect of corrective actions completed to date have significantly reduced the overall risk related to that finding. If you deny any NCV in this report, you should provide a response with the basis for your denial, within 30 days of the date of this Inspection report, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region II; Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C.'20555-0001; and the NRC Resident Inspector at the Shearon Harris Nuclear Plant.
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In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be publicly available in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS Is accessible from the NRC Web site at httrvAvww.nrc.aov/readina-rrl/adams.html (the Public Electronic Reading Room).
Sincerely, Charles R. Ogle, Chief Engineering Branch I Division of Reactor Safety Docket No.: 506400 License No.: NPF-63
Enclosure:
NRC Inspection Report 50-400/02-11 w/Attachments
REGION II==
Docket No.:
License No.:
50-400 NPF-63
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Licensee:
Facility
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50-400/02-11 Carolina Power & Light (CP&L)
Shearon Harris Nuclear Plant Location:
Dates:
5413 Shearon Harris Road New Hill, NC 27562 October 21 - 25, 2002 (Week 1)
November 4 - 8, 2002 (Week 2)
December 16 - 20,2002 (Week 3)
Inspectors:
Accompanying Personnel:
Approved by:
P. Fillion, Reactor Inspector, Region II R. Hagar, Resident Inspector, Shearon Harris (Week 3 only)
C. Payne, Fire Protection Team Leader, Region II (Week 3 only)
R. Schin, Senior Reactor Inspector, Region II (Lead Inspector)
S. Walker, Reactor Inspector (Week 3 only)
G. Wiseman, Senior Fire Protection Inspector, Region II (Weeks 1 & 2)
H. Christensen, Deputy Director, Division of Reactor Safety, Region II (Week 3 only)
C. Ogle, Chief, Engineering Branch 1, Division of Reactor Safety, Region Al (Week 3 only)
N. Staples, Inspector Trainee, Region II (Weeks 1 & 2)
Charles R. Ogle, Chief Engineering Branch 1 Division of Reactor Safety Enclosure
SUMMAY OF FINDINGS
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IR 05000400 02-11; Carolina Power&-Lght; on 10121f2002 -12120/2002, Shearon Hamris--
N Ue a re a
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nspection of the Fire Protection P oram Th - inspecon was conducted by a team odf reglona Inspectors and the Shearon Harris resldent-iii CGEr2Elgh reon findings, each a Non-Cited Violation (NCV),i were Identified. T.-he-signiicance of Issues Is Indicatedb their color-(Green, White, Yellow, Red) using IMC 0609
- -;- - -Ni~in-Ition Process" (SDP).Findings for which the SDP doesnot apply may;;
be '13reetWor be assigned a severity level after-NRC management revlew. The:NRCs program
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for ovrseeig the safe operaton of commercial nuclear power teactors Is described In-.
NUREG16494 ReactorOversight Process>Revion 3,4atedJuly2000.
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'Isidng'
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- ,Greern.
fC`of Shearon Harris Operating Li e Conditon (OLC) 2.F,-Fre
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Poram; and Technidcal -Specficat (TS) 6.B.1, Procedures andrograms.
was identified for faling to protect equrpmentoioperated valve (MOV).CS-165,
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- -aloperation due to a fire. Consequently a fire In any'of three different Safe'Shutdown
- volue conrol tnk (~PT) oulet t chyrg uilding ety S
njcton l
pum s-CaP)
fromd Afialysis (SSA) areas of the reactor auxliary building (RAB) could resultn a reator
c!-oolant pup (RCP) seal toss of coolant accident (LOCA) with no operable igh.
p:ressuresafety injectIon.
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.T.is findinghad a credible impact onsafetybecause it could result n a tossf equipment that was relied upon for safe shutdown from a fire and.could initiate a t.OC
- eve'nt,-However, tihe fning was o very low safetysignificance.because if the low fire - -
I.nitiation frequency and probability of spurous actuations, and the effectiveness of
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-- automatic sprinklers, fire brigade, and remaining safe shutdown (SSSD) equipment to limit-the effects of a fire'and to shut down the nuclear reactor. Therefore, this finding i.
cliaracterized as Green (Section"1'R05.03.b.1).
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-Green. An NCVof OLC 2.F and TS 6.8.1 was Identified for falling to protect 'equipment
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- -' tMO~s ICS-169. CSIP suction cross-connect; lCS-214, CSIP mini-flow Isolatbon CS-
-218,CS!P discharge cross-connect; and ICS-21, CSIP discharge cross-connect] from
- opera
,
Con due to a fire.
osequently, a fire In one SSA area of the RA could
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result'in a loss of-all charging and high pressure safety injection.
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This finding had a credible Impact on safety because It could result In a'loss of
equipment that was relied upon for safe shutdown from a fire. However, the finding was 4f verylow-.safety significance because of the low fire Initiation frequency and probability
'of spurious actuations, and the effectiveness of automatic sprinklers, fire brigade, and remaninng SSD.equIpment to limit the effects of a fire and to shut down the nuclear reactor. 'Therefore, this finding Is characterized as Green (Section 1 R05.03.b.2).
- *. '-Green. An NCV of OLC 2.F and TS 6.8.1 was Identified for failing to protect equipment IMOVs 1CS-166,'VCT outlet to CSIPs; and 1CS-168, OSIP suction cross-connect] from
maloperation due to a fire. Consequently, a fire in one SSA area of the RAB could result In a loss of all charging and high pressure safety injection.
This finding had a credible impact on safety because it could result in a loss of equipment that was relied upon for safe shutdown from a fire. However, the finding was of very low safety significance because-of the low fire initiation-frequency and probability
,p..f spurious actuations, and the effectiveness of automatic sprinklers, fire brigade, and
-,,u, irdngSS1-equipment-to imittheeffects-of-a-firenand toshutrdown the -nuclear reactor. Therefore, this finding Is characterized as Green (Section 1 R05.03.b.3).
- Green. An NCV of OLC 2.F and TS 6.8.1 was identified for failing to protect equipment IMOVs 1CC-208, component cooling (CC) supply to RCP seals; and 1CC-251, CC return from RCP seals] from maloperation due to a fire. Consequently, a fire In one SSA area of the RAB could potentially result in an RCP seal LOCA.
This finding had a credible impact on safety because It could result In a loss of equipment that was relied upon for safe shutdown from a fire and could potentially initiate a LOCA event. However, the finding was of very low safety significance because of the low fire initiation frequency and probability of spurious actuations, and the effectiveness of automatic sprinklers, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor. Therefore, this finding Is characterized as Green (Section 1 R05.03.b.4).
- Green. An NCV of TS 6.8.1 and OLC 2.F was identified for Inadequate procedural steps and for inadequate corrective action. For a fire in the new auxiliary control panel (ACP) fire area, certain SSD procedure steps Involved excessive challenges to operators. There was not reasonable assurance that all non-licensed operators (NLOs)
could perform the steps during a fire. Consequently, a fire In the ACP fire area could result In a loss of all auxiliary feedwater (AFW). The licensee had added these inadequate procedure steps during this Inspection, as part of the corrective action for violation 50-400/02-08-01 regarding an Inadequate fire barrier wall.
This finding had a credible Impact on safety because it could result in Inability to operate equipment that was relied upon for SSD from a fire. However, the finding was of very low safety significance because of the low fire Initiation frequency, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor. Therefore, this finding Is characterized as Green (Section 1 R05.04.b.2).
- Green. An NCV of TS 6.8.1 and OLC 2.F was identified for an inadequate procedure for SSD from a fire and for inadequate corrective action. For a fire In certain SSA areas of the RAB, including the new ACP fire area, there were too many SSD procedure contingency actions to respond to potential spurious actuations for the one available SSD NLO to perform all of them. Consequently, equipment that was relied on for SSD may not be available. The licensee had added some of these procedure steps as part of the corrective action for violation 50-400/02-08-01 regarding an inadequate fire barrier wall.
This finding had a credible Impact on safety because it could result In Inability to prevent an initiating event or to operate equipment that was relied upon for SSD f rom a fire.
However, the finding was of very low safety significance because of the low fire initiation frequency, automatic sprinklers, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor. Therefore, this finding is characterized as Green (Section 1 R05.04.b.3).
- Green. An NCV of TS 6.8.1 was identified for an inadequate procedure for SSD from a fire. For a fire In two SSA areas of the fRAB, the SSD procedure directed operators to take CSIP suction from the boric acid tank (BAT) even If BAT level indication were lost.
However, the charging volume needed for reactor coolant system (RCS) cooldown would have emptied the BAT and damaged the CSIP.
This finding had a credible impact on safety because it could result In loss of equipment that was relied upon for SSD from a fire. However, the finding was of very low safety significance because of the low fire initiation frequency, automatic sprinklers, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor. Therefore, this finding is characterized as Green (Section 1 R05.04.b.4).
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Green. An NCV of OLC 2.F and TS 6.8.1 was Identified for falling to provide battery-
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backed emergency lights for operators to perform actions for SSD from a fire and for inadequate corrective action. For a fire in all of the SSA areas inspected In the RAB, Including the new ACP fire area; many SSD procedure operator action locations did not have the required battery-backed emergency lights. The licensee had added some of these procedure steps as part of the corrective action for violation 50-400/02-08-01 regarding an inadequate fire barrier wall.
This finding has a credible impact on safety because it could result in Increased risk of operators failing to perform SSD actions In an accurate and timely manner. However, the finding was of very low safety significance because operators had flashlights available which would have enabled them to perform the actions. Therefore, this finding Is characterized as Green (Section 1 R05.06.b).
I Report Details 1.
REACTOR SAFETY Cornerstones: Initiating Events and Mitigating Systems IR05 FIRE PROTECTION--
.01 Syciems roUired-TcAchieveand-MaintairPost-Ftre SSD-Ci-cuil AfalksisT-a.
Inspection Scope The team evaluated the licensee's approved fire protection program (FPP) against applicable requirements, Including Operating License NFP-63, Ucense Condition 2.F, FPP; Branch Technical Position (BTP) Chemical Engineering Branch (CMEB) 9.5-1 (NUREG-0800), July 1981; related NRC Safety Evaluation Reports (SERs) In NUREG 1038, and plant Technical Specifications (TS). The team evaluated all areas of this inspection, as documented below, against these requirements. The team used the licensee's Individual Plant Examination for External Events (IPEEE) and In-plant tours to select four risk significant fire areas/zones for inspection. The four fire areas/zones selected were:
Fire Zone 1-A-4-CHLR; part of Fire Area 1-A-BAL-B:
This fire zone was located on the 261 foot level (ground level) of the RAB. It was further subdivided In the licensee's SSA into SSA areas 1-A-BAL-B-B1 [including the WAU chiller and motor-driven AFW pump flow control valves (FCVs)] and 1-A-BAL-B-B2 [Including the 13B chiller and turbine-driven TDAFW pump FCVs]. A significant fire in either of these areas would require shutdown of the unit from the main control room (MCR) and additional manual operator actions In various areas of the plant.
- Fire Zone 1-A-4-COM-E; part of Fire Area 1-A-BAL-B:
This fire zone was located on the 261 foot level (ground level) of the RAB. It was further subdivided in the licensee's SSA to SSA areas 1-A-BAL-B-B4 (including 480V MCC 1B35-SB) and 1-A-BAL-B-B5 (including 480V MCC1A35-SA). A significant fire in either of these areas would require shutdown of the unit from the MCR and additional manual operator actions In various areas of the plant.
- Fire Area 1-A-EPA.
This fire zone was located on the 261 foot level (ground level) of the RAB. It included electrical penetration room 'A'. A significant fire in this area would require shutdown of the unit from the MCR and additional manual operator actions in various areas of the plant.
a
Fire Area 1-A-BATB:
9sire-zone-was-located-on-the-2864oot-level(aboveground-level) of the RAB. It included the 'B' electrical battery room. A significant fire In this area would require shutdown of the unit from the MCR and additional manual operator actions In various a'reas'ofthe'plant.'-_.
-- tsteaiirreviewed-thepost-fie-s that at least one post-fire safe shutdown success path would be maintained free of fire damage during a fire in any of the selected fire areas/zones. The team reviewed the licensee's -fire protection program, Including the SSA and supporting calculations, to determine the systems required to achieve post-fire SSD. The team also reviewed the Safe Shutdown Equipment Ust,.system flow diagrams, and the Fire Hazards Analysis (FHA) in the Updated Final Safety Analysis Report (UFSAR) for each of the selected fire
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'areas t Ii6-- &leteneT-bard:adquiacy of-the SSD analysislanrthe-systeys relied upon to mitigate fires in the selected fire areas. Specific licensee documents and drawings reviewed during the inspection are listed in Attachment 1 to this report.
b.
Findings The team found that the licensee's SSA method for dealing with problem cables (i.e.,
cables that were required for control room operation of SSD equipment during a fire 1n a certain area but were not physically protected from that fire) was to primarily rely on operator manual actions (e.g., locally open the breaker to an MOV and locally operate the MOV using the handwheel). Only if no operator action could be found would the licensee physically protect the cables. Consequently, the licensee had over 100 local manual operator actions that they relied on for achieving hot shutdown conditions during a fire. The licensee had not requested deviation approvals from the NRC for these operator actions and had not verified or validated the operator actions to the extent that would have been Involved In NRC reviews of deviation requests. This SSD methodology contributed to the findings and unresolved item (URI) that are described In the following sections of this report.
.02 Fire Protection of SSD Capability a.
InsDection ScoDe The team reviewed UFSAR Section 9.5.1, Appendix 9.5A, Fire Hazards Analysis (FHA);
the FPP manual; and plant administrative fire prevention/combustible hazards-ignition source control. procedures. This review was to verify that the objectives established by the NRC-approved FPP were satisfied. The team also toured the selected plant fire areas observing the licensee's implementation of these procedures. The team also reviewed the FPP transient combustible permit logs, and fire emergency/incident investigation reports, for the years 2000-2002. Corrective action program Action Requests (ARS) resulting from fire, smoke, sparks, arcing, and equipment overheating incidents for the same period were also reviewed to assess the effectiveness of the fire prevention program and to identify any maintenance or material condition problems related to fire Incidents.
A
The team reviewed flow diagrams and engineering calculations associated with the 'B'
battery room heating, ventilation, and air conditioning (HVAC) systems. This review was done to verify that systems used to accomplish safe shutdown would not be inhibited by a potential hydrogen gas fire in the 'B' battery room due to inoperable ventilation supply and exhaust fans. The team also reviewed the TS LCO requirements for loss of
-- ventilation in the 'B' battery room to verify that appropriate timely actions were specified to ensure that hydrogen gas concentrations generated by the station batteries remained
-- below xplosiveimIts.
The team toured the plant's primary fire brigade staging and dress-out areas to assess the condition of fire fighting and smoke control equipment. Fire brigade personal protective equipment located in brigade staging area lockers was reviewed to evaluate equipment accessibility and functionality. Additionally, the team examined whether backup emergency lighting was provided for access pathways to and within the fire
-: ::igatagi g-rfdkes reiasirk support.of fire~rigadoperationszhoul a-power failure occur during the fire emergency. The team also observed whether emergency exit lighting was provided for personnel evacuation pathways to the outside exits as identified in the National Fire Protection Association (NFPA) 101, Life Safety Code and Occupational Safety and Health Administration (OSHA) Part 1910, Occupational Safety and Health Standards. The adequacy of the fire brigade self-contained breathing apparatus (SCBAs) was reviewed as well as the availability of supplemental breathing air tanks.
Team members also toured the selected fire areas and compared the associated fire pre-plans with as-built plant conditions. This was done to verify that they were consistent with the fire protection features and potential fire conditions described In the UFSAR.
Additionally, the team reviewed drawings and engineering flood analysis associated with the 261-foot elevation reactor auxiliary building floor and equipment drain system to verify that those-actions required for SSD would not be inhibited by fire suppression activities or leakage from fire suppression systems.
The team reviewed the fire brigade response procedure, fire brigade organization, and training and drill program administration procedures. Fire drill critiques of operating shifts for the period of March 2001 through October 2002 were reviewed to verify that fire brigade drills had been conducted In high fire risk plant areas. Fire brigade training/drill records for 2002 were also reviewed to verify that the fire brigade personnel qualifications, brigade drill response time, and brigade performance met the requirements of the licensee's approved FPP. Additionally, the team observed a fire drill to verify the licensee's implementation of the fire brigade organization, training, and drill program administration procedures. The team observed the actions of the site fire brigade, offsite fire department, and fire drill monitors; and attended the drill critique.
b.
Findincs No findings of significance were Identified.
.03 Post-Fire SSD Circuit Analysis
'a.Yl=-ns~eCtiofl-ScOe_
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The team reviewed the adequacy of separation and fire barriers provided for the power and control cabling of equipment relied on for SSD during a fire in any of the selected fire areas/zones. On a sample basis, the team reviewed the SSA and the electrical
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schematics-er-pewer-and-controircuits-of-S emponents,-and4ooked-for-the potential effects of open circuits, shorts to ground, and hot shorts. This review focused o'n the cabling of selected components for the charging/safety Injection system, AFW system, and CC system. The team traced the routing of cables by using the cable schedule and conduit and tray drawings. Walkdowns were performed to compare 1-hour and 3-hour barriers (conduit and tray fire barrier wraps) to barriers indicated on the drawings. Circuit and cable routings were reviewed for the following equipment: 1Cog
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=cSnri-tY;1C-8B8-CSIP -suctionwcross!rnectMfOI,-
1CS-214, CSIP minimum flow MOV; 1CS-217, CSIP discharge cross connect MOV; 1CS-218, CSIP discharge cross connect MOV; 1CS-219, CSIP discharge cross connec MOV; 1 CS-i 65, volume control tank (VCT) outlet MOV; 1 CS-i 66, VCT outlet MOV; 1CS 278, boric acid tank (BAT) to CSIP MOV; BAT level Instrumentation; I CC-207, CC suppi)
to RCP seals MOV; 1 CC-208, CC supply to RCP seals MOV; 1 CC-252, CC return from RCP seals MOV; 1CC-251, CC return from RCP seals MOV; lCC-249, CC return from RCP seals MOV; 1 RC-1 17, pressurizer power-operated relief valve (PORV) block valve; ISI-310, containment sump to 'A' RHR pump MOV; ISI-31 1, containment sump to 'B'
RHR pump MOV; motor-driven AFW pump 1A; motor-driven AFW pump 1B; and turbine/
driven AFW pump.
The team also reviewed studies of overcurrent protection on both AC and DC systems to Identify whether fire Induced faults could result in defeating the safe shutdown functions.
b.
Findings (1)
MOV 1CS-1 65. VCT Outlet to CSIPs Introduction The team identified an NCV of OLC 2.F and TS 6.8.1 for failing to protect equipment
[MOV 1 CS-1 65] from maloperation due to a fire. Consequently, a fire In any of three different SSA areas of the RAB could result In an RCP seal LOCA with no operable high pressure safety Injection.
Description The team found that the control power cable for charging system MOV 1 CS-1 65; which was relied upon to remain open for SSD during a fire In SSA areas 1 -A-BAL-B-B1 and 1-A-BAL-B-B2, and in fire area 1-A-EPA; was routed through those areas with no fire barrier. As a result, the control power cable for the MOV was vulnerable to fire-induced hot shorts which could result in spurious valve operation. The lack of a required fire barrier was not recognized In the SSA and no procedural guidance was included In AOP-36, Safe Shutdown Following a Fire, Rev. 21, for operators to prevent maloperation of
1 CS-1 65 prior to damage occurring to SSD equipment. Consequently, a fire in one of the three SSA areas could cause 1CS-165 to spuriously close, Isolate all CSIP suction
-. '-=-flowpathsrandtmmediately damage the operating SSD CSIP.
The SSD analysis for a fire In SSA areas 1-A-BAL-B-B1, 1-A-BAL-12, or 1-A-EPA was to-rely-oh-SSD-ivAslon-2-equipmont.--This-included reliance on CSIP 'B' for RCS-makeup water, RCP seal cooling, reactivity control by boration, and high pressure safety injection.
--- T.-eSSkassumedthat C1SIP'!A'was-not-as iird-to=be-unaffectedbyefire and CSIP
'C' was not assured to be available. Consequently, a failure of CSIP 'B' could result in a loss of all charging and high pressure safety injection. Also, for a fire In any of these three SSA areas, CC flow to the RCP seals was not protected. The team found that the control power. cable to MOV ICC-207, CC flow to RCP seals, was also routed through the same three SSA areas in the same cable tray with the control power cable to I CS-
'165. AOP-36 Included no operator action to prevent spurious operation of MOV ICC-
- 27.puriO u
oCM2 ustopga CWfiow-to4heseals-ofrall.three RCPs., Thus the potential consequences of a fire in any of the three SSA areas could be.
an RCP seal LOCA with no charging or high pressure injection.
Also, the team found that the control power cables for MOVs lCC-252, CC return from RCP seals, and 1CC-249, CC return from RCP seals, were routed through SSA area 1-A-BAL-1B-2 and could be affected by a fire in that area. AOP-36 Included an operator action to prevent spurious actuation of 1 CC-252 for a fire in SSA area 1 -A-BAL-B-B2.
That action included opening the breakerto MOV ICC-252 on MCC lE12. However, the SSD NLO would likely not be able to safely do that action during a fire in SSA area 1-A-BAL-B-B2 because MCC I El 2 was located in that SSA area. AOP-36 included no operator action for 1 CC-249. Spurious closure of 1CC-252 or 1 C-249 would stop all CC flow to the RCP seals. The team noted that, while the operator action for 1 CC-252 may not be needed for a fire in SSA area 1-A-BAL-B-B2 because the charging system was supposed to provide RCP seal cooling, this inappropriate procedural action (sending an operator Into an area where there was a fire) could delay the SSD NLO from performing other procedure actions that were required to achieve SSD.
In addition, the team found that modification ESR 01-00087, which was installed In January 2002, had affected this condition and missed an opportunity to correct It. ESR 01-00087 changed the CSIP mini-flow path so that It would go to the VCT instead of going directly to the CSIP suction. Prior to the ESR, if I CS-1 65 spuriously closed, the running CSIP would still have some suction although probably not enough to prevent pump damage. After the ESR; I lCS-165 spuriously closed, the running CSIP would have no suction and CSIP failure would be more certain and more immediate. ESR 01-00087 failed to recognize this effect and missed an opportunity to identify and correct the condition.
Analysis This finding had more than minor safety significance because it affected the Mitigating Systems and Initiating Events objectives of the Reactor Safety Cornerstone. The finding affected the availability and reliability of systems that mitigate initiating events to prevent undesirable consequences It also affected the likelihood of occurrence of initiating t-cl njo crt1 Clsafei1Yd rrtIscowevershe findingwasofvary-ow
safety significance because of the low fire initiation frequency and probability of spurious actuations, and the effectiveness of automatic sprinklers, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor.
Therefore, this finding is characterized as Green.
Enforcement OLC 2.F required that the licensee implement and maintain in effect all provisions of the approved fire protection program as described in the Final Safety Analysis Report. The UFSAR, Section 9.5.1, FPP, stated that outside containment, where cables or equipment (including associated non-essential circuits that could prevent operation or cause maloperation due to hot shorts, open circuits, or shorts to ground) of redundant safe shutdown divisions of systems necessary to achieve and maintain cold shutdown conditions are located within the same fire area outside of primary containment, one the redundant divisions must be ensured to be free of fire damage. Section 9.5.1 further stated that if both divisions are located in the same fire area, then one division is to be protected from fire damage by one of three methods: 1) a three-hour fire barrier, 2) a one-hour fire barrier plus automatic detection and suppression, or 3) a 20-foot separation with no intervening combustibles and with automatic detection and suppression.
TS 6.8.1 required procedures as recommended by Regulatory Guide (RG) 1.33 and procedures for fire protection program Implementation. RG 1.33 recommended procedures for combating emergencies, including fires. The licensee's Interpretation of their fire protection program was that they could and would rely on operator actions in place of physical protection of SSD equipment (see Section 1 R05.04.b.1). However, the licensee had failed to provide procedural guidance in AOP-36 for operators to prevent maloperation of MOV 1CS-165.
Contrary to the above requirements, the licensee failed to protect MOV ICS-1 65 from maloperation due to a fire where It was relied on for SSD. Because the licensee entered the finding into the corrective action program as AR 76260, this Item is being treated as an NCV In accordance with Section VE.A.1 of the NRC's Enforcement Policy. This item Is identified as NCV 50-400/02-11-01, Failure to Protect MOV 1 CS-1 65, VCT Outlet to CSIPs, From Maloperation Due To a Fire.
(2)
MOV 1CS-169. CSIP Suction Cross-connect: MOV 1CS-214. CSIP Mini-flow Isolation:
MOV 1CS-218. CSIP Discharge Cross-connect: and MOV 1CS-219. CSIP Discharge Cross-connect Introduction The team identified an NCV of OLC 2.F and TS 6.8.1 for failing to protect equipment
[MOVs 1 CS-1 69, 1 CS-214,1 CS-218, and 1 CS-219] from maloperation due to a fire.
Consequently, a fire in one SSA area of the RAB could result In a loss of all charging and high pressure safety injection.
Descriotion
--- Tdh-tem-that-the-controlpower-cables-for-charging system MOVs 1CS-169, lCS-214, 1CS-218, and 1CS-219, which were relied upon to remain open for SSD during a fire in SSA area 1-A-BAL-B-B5, were routed through that area with incomplete fire
- a-riers7T ff e ro61'able sWereunpro-t-e-d forabout one foot above-MCCI -A35-SA
_and inside the MCC.
This lack of required fire barriers was recognized in the SSA for 1 CS-1 69, 1 0S-214, and I CS-218, and procedural guidance was included in AOP-36 f6r operators to prevent maloperation of these valves. However, the procedural guidance was not adequate.
AOP-36 directed operators to go to MCC 1A35-SA and open the breakers for lCS-169 and 1 CS-214 to prevent spurious operation. However, operators would not be able to safely do that because the actions were in the area of the fire that could cause the
--siurio~-~p~eratio7 CP-3 irtcte6boperatorrs-gooto-MCGi B39SB-SinAanotherfroem, to open the breaker for 1CS-218. However, operators would not be able to do that because the breaker for 1CS-218 was actually located on MCC 1A35-SA. The SSA had not identified a need for operator action to prevent maloperation of 1 CS-219 and AOP-36 included no action steps for that valve.
AOP-36 did include the following guideline for operators: "Monitor for spurious valve and'
pump operation which may result In equipment damage (for example, CSIP suction valves.)" The team noted that closure of a CSIP suction valve could result In pump damage within seconds; before operators could respond to an annunciator, analyze the condition, and take action to prevent pump damage. Another AOP-36 guideline was:
OWhen directed by the Unit Shift Supervisor, then shut down equipment and de-energize electrical busses located within the fire area.' Operators stated that they would de-energize MCC 1A35-SA If the fire brigade team leader or another operator told them that the MCC was on fire or if they observed spurious actuations that could be initiating from the MCC. However, the team noted that the fire brigade would not arrive and attack the fire until about 20 minutes after the control room sounded the fire alarm, and spurious actuations could occur well before that. By procedure, control room operators would respond to a single fire detector annunciator by sending an NLO to verify that there was a fire and that the fire was large enough to warrant sounding the fire alarm and calling out the fire brigade. However, if the control room operators received annunciation from two or more fire detectors, which would be very likely in the event of fire large enough to present an operational safety concern, then they would not send an NLO but instead would immediately sound the fire alarm and call out the fire brigade. So it was likely that the first visual report on the fire would not be received in the control room until about 20 minutes after the fire alarm. By that time, the fire would have likely filled the room with smoke so that the fire brigade would not be able to immediately identify if the MCC was on fire.
The team concluded that it was unlikely that the control room would de-energize MCC 1A35-SA before spurious actuations could occur. Consequently, a fire in this area, near or in MCC 1A35-SA, could cause any of the four MOVs to spuriously close. Closure of 1CS-214 would stop all mini-flow from all CSIPs. Closure of 1CS-218 or 1CS-219 would stopchargigflowrom SSD :SlEB', If such a loss o
~fcrging flow or CSIP mini-flow-occurred,-operators would receive-an alarm n rne-ontrod-room.andwould probably have
time to diagnose the condition and Initiate recovery actions before CSIP damage occurred. However, closure of 1CS-169 would stop all suction to SSD CSIP 'B' and
-- -- immediately-damage-the-pu p. - -
The SSD analysis for a fire In SSA area 1-A-BAL-B-BS was to rely on SSD DivisIon 2-equipment. This included reliance on CSIP 'B' for RCS makeup water, RCP seal cooling, reactivity control by boration, and high pressure safety injection. CSIP 'A' was not dssured1tbeisn-affectaOby the-fire-and GSIP-G' was-not-assured-to be-available. -The tearni noted that MOVs powered from MCC 1A35-SA could affect CSIP 'A' and CSIP 'C'.
While the SSA did not assure that CC would be available, the team did not identify any vulnerabilities of CC to a fire in this area. Consequently, the team concluded that the potential consequences of a fire In SSA area 1 -A-BAL-B5 could be a loss of all charging and high pressure safety injection.
- = ~2
-o--A ^~:~ * z-=
- ~
--.
- v=- --
In -- *-s This finding had more than minor safety significance because It affected the Mitigating Systems objectives of the Reactor Safety Comerstone. The finding affected the availability and reliability of systems that mitigate initiating events to prevent undesirable consequences. However, the finding was of very low safety significance because of the low fire Initiation frequency and probability of spurious actuations, and the effectiveness of automatic sprinklers, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor.
During the Inspection, a question arose about whether a fire Initiating Inside an MCC could credibly cause spurious actuations. A premise was that the power breaker to the MCC would always trip before spurious actuations could occur. The team noted that the frequency of a fire Initiating Inside an MCC was higher than the frequency of a fire initiating just outside of an MCC. However, after further review, the team concluded that the frequency-for a fire starting either outside or inside an MCC would still result In a very low safety significance for the observed condition. Therefore, this finding is characterized as Green.
Enforcement As described in Section 1A05.03.b.1 above, OLC 2.F required that equipment relied upon for SSD be physically protected against maloperation due to the fire. Also, TS 6.8.1 required procedures for implementing the fire protection program and for combating fires.
Contrary to the above requirements, the licensee failed to protect MOVs 1 CS-1 69,1 CS-214, 1 CS-218, and 1 CS-219 from maloperation due to a fire where they were relied on for SSD. Because the licensee entered the finding into the corrective action program as ARs 76260 and 80212, this Item Is being treated as an NCV in accordance with Section VI.A.1 of the NRC's Enforcement Policy. This item is identified as NCV 50-400/02-11-03, Failure to Protect Charging System MOVs 1 CS-1 69, 1 CS-214, 1 CS-218, and 1 CS-219 From Maloperation Due To a Fire.
a
(3)
MOV 1CS-166. VOT Outlet to CSIPs: MOV 1CS-168. CSIP Suction Cross-connect: and MOV lCS-217. CSIP Discharge Cross-connect Introduction The team identified an-NCV of OL-C-2.F-and-TS-6.8.1 for failing-to-protect-equipment
[MOVs 1 CS-1 66, 1 CS-1 68, and 1 CS-217] from maloperation due to a fire.
C6nseijuently, a fire in one SSA area of the RAB could result in a loss of all charging and high pressure safety Injection.
Descriotion The team found that the control power cables for charging system MOVs 1 CS-1 66, 1 CS-168, and 1 CS-217, which were relied upon to remain open for SSD during a fire In SSA
.- BAI;;A;B4.e:tbuto3,'
d ugethrougihatareaxwith incomplete lire barrTers>rThe:
control cable for MOV 1 CS-1 66 was unprotected for about one foot above MCC 1 B35-SB and inside the MCC. The control power cables for MOVs ICS-168 and ICS-217 were unprotected inside MCC 1 B35-SB. This lack of required fire barriers was not recognized in the SSA and no procedural guidance was included in AOP-36 for operators to prevent or mitigate maloperation of these valves. Consequently, a fire In this area, near or In MCC 1 B35-SB, could cause 1CS-166 or 1CS-168 to spuriously close, which would stop all suction to SSD CSIP 'A', and immediately damage the pump. If CSIP 'C' were aligned to be used in place of CSIP 'A', then the fire could cause spurious closure of 1CS-217 and stop charging flow from CSIP 'C'.
The SSD analysis for a fire in SSA area 1-A-BAL-B-B4 was to rely on SSD Dvision 1 equipment. This Included reliance on CSIP 'A' for RCS makeup water, reactivity control by boration, and high pressure safety Injection. CSIP 'B' was not assured to be unaffected by the fire and CSIP 'C' was not assured to be available. Also, when all three CSIPs were available, the 'C' CSIP would be aligned to the 'B' train; and It would take licensee personnel several hours to align the 'C' CSIP to the 'A' train. Consequently, a.
failure of CSIP 'A' could result In a loss of all charging and high pressure safety Injection.
If CSIP 'C' were aligned to be operating in place of CSIP 'A', and a maloperation of 1CS-217 caused a loss of charging flow, operators would receive a loss of charging flow alarm and would probably have time to diagnose and respond to the condition before the CSIP was damaged.
In addition, the team found that modification ESR 01-00087, which was installed In January 2002, had affected the significance of the lack of protection for 1 CS-1 66. As described above for 1 CS-1 68, ESR 01-00087 was a missed opportunity to Identify and correct the lack of protection for 1CS-1 66.
Analstis This finding had more than minor safety significance because it affected the Mitigating Systems objectives of the Reactor Safety Cornerstone. The finding affected the availability and reliability of systems that mitigate initiating events to prevent undesirable consequences. However, the finding was of very low safety significance because of the lowi1ireinitiatimn frequencypaid-babityof.spuuciusactia 0i, no, al Ii.yle Aif nesss
of automatic sprinklers, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor. Therefore, this finding Is characterized as Enforcement As described In Section 1 R05.03.b.1 above, OLC 2.F required that equipment relied
-- TptmorSSDt-bphysicalyprotected-against ifialoperation-cueto the-fire.-Alsoi TS -- 6.8.1 required procedures for Implementing the fire protection program and for combating fires.
Contrary to the above requirements, the licensee failed to protect MOVs 1 CS-1 66, 1 CS-168, and I CS-217 from maloperation due to a fire where they were relied on for SSD.
Because the licensee entered the finding into the corrective action program as AR 76260,'this Item is being treated as an NCV in accordance with Section VIA1 of the NRC's Enforcement Policy. This item is identified as NCV 50-400/02-11-04, Failure to Protect Charging System MOVs 1 CS-1 66, 1 CS-1 68, and 1 OS-217 From Maloperation Due To a Fire.
(4) MOV 1 CC-251. CC Return From RCP Seals:
and MOV 1 CC-208. CC SupDIV To RCP Seals Introduction The team Identified an NCV of OLC 2.F and TS 6.8.1 for failing to protect equipment
[MMOVs 1CC-251 and 1CC-208] from maloperation due to a fire. Consequently, a fire In one SSA area of the RAB could potentially result In an RCP seal LOCA.
Description The team found that the control power cables for CC system MOVs 1CC-251 and ICC-208, which were relied upon to remain open for SSD during a fire In SSA area I -A-BAL-C, were routed through that area and into MCC 1 B31 in that area with no fire barrier.
Fire area 1 -A-BAL-C was located on the 286 foot level of the auxiliary building, above electrical penetration room 'B'. This lack of required fire barriers and need for operator actions was recognized in the SSA but no procedural guidance was included in AOP-36 for operators to prevent or mitigate maloperation of these valves. Consequently, a fire In this area could cause 1 CC-251 or 1 CC-208 to spuriously close, which would stop all CC flow to the RCP seals.
The SSD analysis for a fire In area 1 -A-BAL-C was to rely on SSD Division 1 equipment.
This included reliance on CC to cool the RCP seals. CSIP supply to the RCP seals was not assured to be unaffected by the fire. Consequently, a loss of CC to the RCP seals could potentially result In a loss of all RCP seal cooling which could in turn result in an RCP seal failure and a LOCA.
Analysis-T-his-finding had more than minor safety significance because it affected the Initiating Events objective of the Reactor Safety Cornerstone. The finding affected the likelihood of occurrence of Initiating events that challenge critical safety functions. However, the finding was of very low safety significance because of the low fire initiation frequency and
.probab of spurious actuations, and the effectiveness of automatic sprinklers, fire-brigaderandremainingSS.O-equip mentlo-imt-th-effects-ofafire and to shut down the nuclear reactor. Therefore, this finding Is characterized as Green.
Enforcement As described In Section 1 R05.03.b.1 above, OLC 2.F required that equipment relied upon for SSD be physically protected against maloperation due to the fire. Also, TS-6-re quired-procedures4 fnr>T plementingthe-firezprotectiorrprogram and for-combating fires.
Contrary to the above requirements, the licensee failed to protect MOVs 1CC-251 and 1CC-208 from maloperation due to a fire where they were relied on for SSD. Because the licensee entered the condition Into the corrective action program as AR 80089, this item is being treated as an NCV In accordance with Section VI.A.1 of the NRC's Enforcement Policy. This Item is identified as NCV 50-400/02-11-02, Failure to Protect MOVs 1 CC-251 and 1 CC-208, CC for RCP Seals, From Maloperation Due To a Fire.
.04 Operational ImDlementation of SSD Capabilitv a.
Inspection Scope The team reviewed and walked down the local manual actions, needed to achieve and maintain hot shutdown, that were described In procedure AOP-036, Safe Shutdown Following a Fire, Rev. 21, for fires In all of the selected areas/zones as described In Section 1 R05.01.a.
The team also followed up on open violation (VIO) 50-400/02-08-01, Failure to Implement and Maintain NRC Approved Fire Protection Program Safe Shutdown System Separation Requirements. That VIO and related White finding had been left open In IR 50-400/02-08. In a supplement to that IR dated October 4, 2002, the NRC had stated that licensee modifications had reduced the risk significance of the degraded Thermo-Lag barrier to that of a Green finding. However, VIO 50-400/02-08-01 was left open pending further NRC review of licensee corrective actions and the development of internal NRC inspection guidance, related to use of local manual actions as opposed to one of the protection methods identified In NRC Position C.5.b.(2) of Branch Technical Position (BTP) CMEB 9.5-1. During this inspection, the team reviewed and walked down the local manual actions, needed to achieve and maintain hot shutdown, that were proceduralized by the licensee during this inspection In AOP-36, Rev. 24, for the new ACP room fire area. The team performed these reviews and walkdowns using NRC inspection guidance.
The team reviewed and walked down the manual actions described above to verify that:
The procedures used for SSD were available to the appropriate staff.
- The procedures used for SSD were consistent with the SSA methodology and assumptions and also were consistent with fire pre-plan procedures.
- The actions were described in the fire-protection-related licensing-basis documents.
- The procedures were written so that operator actions could be correctly performed within the times assumed In the SSA.
-
Personnel required to achieve and maintain the plant in hot shutdown condition-from the MCR could be provided from normal -onsite staff, exclusive of the fire brigade.
- Operator and fire brigade staffing would be adequate to complete the required manual actions.
- Operators had sufficient access to the equipment to perform the required actions.
- Access to remote shutdown equipment and operator manual actions would not be inhibited by smoke migration from one area to adjacent plant areas used to accomplish SSD.
-*
The training program for operators' included appropriate lesson plans and job performance measures (JPMs) for SSD activities.
b.
Findinas (1)
Reliance on Manual Actions In Place of Reguired Physical Separation or Protection Introduction The team identified a URI related to the licensee's reliance on manual actions In place of the required physical separation or protection.
Descri tion The team found that the licensee routinely relied on manual actions in place of the required physical separation or protection. For a fire in SSA areas 1 -A-BAL-B-B1, -B2, -
B4, or -B5; AOP-36 included about 39 local manual operator actions to achieve and maintain hot shutdown. For a fire in the new ACP room, fire area 1 -A-ACP, AOP-36 included about 55 local manual operator actions to achieve and maintain hot shutdown.
The local manual actions for each of the areas reviewed are listed in Attachment 2 to this report. The team assessed that an SSD NLO would reasonably be able to perform each of the operator actions that were reviewed (except those that are identified below as findings)'during'a fire; However, reliance on all of these manual actions in-place of
physical separation or protection could increase the risk of failure of SSD equipment to operate during a fire.
Analysis-This issue could have more -than -minor-safety significance-because-it-could affect the Mitigating Systems objectives of the Reactor Safety Cornerstone. The Issue could affect
- -teavairability-and-reliability-ofsystems that-mitigate4nitiating-eventsto-preclude undesirable consequences.
Enforcement As stated In Section 1 R05.03.b.1, OLC 2.F and the licensee's approved FPP required that If both divisions (that could be used for SSD) are located in the same fire area, then
-
nCe dhsion-is to-be physically protected4rom fire-damage-by.yonef three-approved,-z-:
methods. The licensee's approved FPP did not provide for reliance on operator actions In place of physical separation or protection of SSD equipment. However, the licensee's Incorrect interpretation of their fire protection program was that they could and would rely on operator actions in place of physical separation or protection of SSD equipment, without obtaining NRC approval for deviating from the requirements. Consequently, the licensee had not requested NRC approval for reliance on any operator actions in place of physical separation or protection.
Per current NRC Inspection guidance, this issue will be identified as a URI, pending the commission's acceptance of a proposed NRC staff Initiative to change the related NRC requirements. It will be identified as URI 50-400/02-11-05, Reliance on Manual Actions in Place of Required Physical Separation or Protection.
(2)
Fire SSD ODerator Actions With Excessive Challenges Introduction The team identified an NCV of TS 6.8.1 and OLC 2.F for Inadequate procedural steps and for inadequate corrective action. For a fire in the new auxiliary control panel (ACP)
fire area, certain SSD procedure steps involved excessive challenges to operators.
There was not reasonable assurance that all NLOs could perform the steps during a fire.
Consequently, a fire In the ACP fire area could result In a loss of all AFW. The licensee had added these inadequate procedure steps during this inspection, as part of the corrective action for violation 50-400/02-08-01.
DescriDtion For a fire In Fire Area 1-A-ACP, AOP-36 steps 2.c and 14.a required the NLO to remove fuses from transfer panel I B. Completing these steps would include the following challenges:
The subject transfer panel was physically located approximately 20 feet from the ACP room door. With a fire in the ACP room, the area around the transfer panel could become uninhabitable before the NLO could complete these steps,
II
because some smoke from the fire could enter the transfer panel area from around the door while the door was closed, and because smoke would certainly
-
--enter-theetransferpanel-area-when-the-door-was-opened-by-the fire brigade to attack the fire.
- To physically reach the subject fuses,- the NLO would need to place his or her entire body inside a cabinet with an opening that was approximately 15 inches-wide--Aso,-theinside of-the-cabinetincluded-energized electrical-components on each side of the cabinet, with about 15 inches of width between them, The licensee had not ensured that all NLOs were physically capable of safely entering that cabinet - the team noted that some NLOs were more than 15 inches wide.
- Because the subject fuses were located on a panel inside the cabinet and approximately seven feet above floor level, all but the tallest NLOs would need to-use-eafaroW, custom..madevwo6deistep-stool inside 4e cabinetitobe ablerto reach the fuses. The team noted that the location of the step-stool was not controlled.
- Because the subject fuses were also located behind a plexiglass fuse cover that was held In place by small metal screws, the NLO would need to raise his or her hands above the level of his or her head and use a metal screwdriver to remove the fuse cover. The licensee had not ensured that all NLOs were physically capable of completing this activity. Furthermore, because this activity involved manipulating a metal screwdriver Inside an energized electrical cabinet, the team considered the activity to Involve a personnel safety hazard.
- To identify the correct fuses to be pulled, the NLO must first identify the cabinet In which the fuses are located, and then identify the fuses themselves, within that cabinet The team observed that the subject cabinet was physically adjacent to four identical cabinets, that these cabinets were not labeled on the side from which the NLO would enter, and that the instructions In NLOP-036 did not identify the subject cabinet. Furthermore, the team observed that the labels which uniquely identified the subject fuses within the cabinet were difficult to see - they were partially obscured by cables which had been landed on adjacent terminal blocks.
The team considered that these challenges were excessive and that there was not reasonable assurance that all NLOs would be able to perform the actions during a fire.
Consequently, operators would not able to start the turbine-driven AFW pump and the AFW system could become unavailable; The team concluded that these procedure steps were inadequate and that they represented inadequate corrective action for violation 50-400/02-08-01.
Analysis This finding had more than minor significance because It affected the Mitigating Systems objectives of the Reactor Safety Cornerstone. The finding affected the availability and
[eliab>i f sy te s that.mitigate Initiating events to prevent undesirable consequences.
However, the finding was of very low safety significance because of the low fire Initiation frequency, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor. Therefore, this finding is characterized as Green.
.
Enforcem ent.__________._____
__._.
As described in Section 1 R05.03.b.1 above, OLC 2.F required that equipment relied upon SS-tie pyeialfr-ofe-ce-d fomvthe fire-.A-So 6-8.Teqdure-dprocedures'
for implementing the fire protection program and for combating fires. In addition, OLC 2.F and the UFSAR, Section 9.5.1, FPP, included quality assurance requirements for fire protection. The FPP stated that a QA program was being used to identify and rectify any possible deficiencies in design, construction, and operation of the fire protection systems.
Contrary to the above requirements, the licensee failed to protect the turbine-driven EFW pum rome ofa i':rhef6-I reli6d dh-for SSI In addition,,ihte fcensee's corrective actions for a previous violation were inadequate. Because the licensee entered the finding into the corrective action program as AR 80214, this Rtem Is being treated as an NCV In accordance with Section VI.A.1 of the NRC's Enforcement Policy.
This Item is identified as NCV 50-400/02-11-06, Fire SSD Operator Actions With Excessive Challenges.
(3)
Too Many SSD Actions for Operators to Perform Introduction The team identified an NCV of TS 6.8.1 and OLC 2.F for an Inadequate procedure for SSD from a fire and for inadequate corrective action. For a fire in certain SSA areas of the RAB, Including the new ACP fire area, there too many SSD procedure contingency actions to respond to potential spurious actuations for the one available SSD NLO to perform them all. Consequently, equipment that was relied on for SSD may not be available. The licensee had added some of these procedure steps as part of the corrective action for violation 50-400102-08-01.
Descri tion The team found that for each fire SSA area inspected, AOP-036 required operators to complete a relatively large number of manual actions outside the main control room. The team determined that the normal shift operating crew Included four NLOs; three were assigned to the fire brigade and one was assigned to be the SSD NLO. The local manual operator actions required to achieve and maintain hot shutdown for each of the fire areas Inspected are listed In Attachment 2 to this report. The most demanding fire areas were fire area 1 -A-ACP, which Included about 55 such actions, and fire area 1-A-BAL-B, which Included about 39 such actions.
Also, since the SSA did not ensure that offsite power would not be lost due to a fire In any of the SSA areas inspected, operators were expected to be able to respond to a loss of offsite power (LOOP) and reactor trip while performing the fire SSD actions. The team noted that a LOOP or reactor trip could-place even more demands on the one NLO who was not fighting the fire.
--
The team found that while most of the manual actions in these SSA areas involved one-
-timeationsikeopening-breaker)-others-cokidrequirethe-NLO-G-monitor-plant conditions and make system adjustments over an extended period of time. The manual actions which could require dedicated NLO attention, and thus possibly detract from the sUcCessful and timely perfrmanceo-fsiubsequeintreqIired local manual -operator--
actions,.included the following:
In Section 3.0 of AOP-036, which was to be performed for a fire in any of the SSA areas inspected, Step 1 3.b(3) required the NLO to establish continuous communications with the MCR, locally shut I CS-228 to isolate the normal charging flow control valve (FCV) and then to locally control charging flow by throttling the bypass valve, 1CS-227. Both valves were in close proximity and located In the scalloped area of the 248-ft level In the RAB. This area was-7-le*
ed-he-iadlation e 11olldi'rea'(RC-A)-aid-radiatioroevels atholesevalves were elevated but within 10 CFR 20 limits. A sound powered phone with a long extension cord was located in the area to allow the NLO to wait In low dose areas between valve manipulations if the NLO's radio was not functional. However, local manual operator actions subsequent to this step could be adversely impacted [e.g., Section 3.0, Step 14.b for locally responding to a failed open steam generator power operated relief valve (PORV)].
In Attachment 1 of AOP-036, Step 13.c for fire area 1-A-ACP required the NLO to locally operate a PORV on the C steam generator, to obtain and maintain the desired RCS temperature. Because the unit would likely not be at steady state when this action was undertaken, and because a fire in this area may complicate operator efforts to stabilize the plant, the NLO who undertakes this action may be required to monitor RCS temperature and make appropriate adjustments to the PORV position almost continuously and for some time, until the plant Is reasonably stable.
- In Attachment 1 of AOP-036, Step 1 4.b for fire area 1 -A-ACP required the NLO to throttle 1AF-149 to maintain level in the C steam generator. For the same reasons as described above, the NLO who undertakes this action may be required to continue to monitor steam-generator level and make appropriate adjustments to the position of 1AF-149 almost continuously and for some time, until the plant Is reasonably stable.
The team found that some of the required manual actions would be completed Inside the radiologically controlled area (RCA),'while others would be completed outside the RCA.
The team also observed that completing the manual actions in AOP-036, in the order In which they are described in that procedure, would require the SSD NLO to enter and exit the RCA several times. The team noted that:
some manual actions involved valves Identified as potentially contaminated or located In contamination areas,
- -radioactive.-radon gas-can become associated wit anyone who passes through the RCA,
- hand or foot contamination as well as radon gas can cause a portal monitor to
--.---------elarred
anyone who is in a portal monitor when it alarms must wait at the exit point for
--ihealth physics (HP) technicians-to-complete-a-detailedsurveyto-determine the true cause of the alarm, before proceeding.
The team noted that the licensee had no emergency dosimeters or rapid ingress/egress procedures in place for use during plant emergency situations. The team therefore considered that every time the SSD NLO exited the RCA, that NLO may experience a portal-monitor alarm, and may therefore be forced to wait for HP technicians to arrive at the exit and complete a detailed survey before proceeding. The team received a portal monitor alarm on many occasions during this inspection. Operators stated that, If they r
bceifovee-d-zru-n~
gt--fire;tbey-would-wait for-an*HP.-Aechnician-betoA proceeding to perform SSD actions.
The team considered that the manual actions In AOP-036 could not reasonably be completed by the available staff, because:
- -
the SSD NLO may be required to complete as many as 55 manual actions,
several manual actions required dedicated operator attention,
some of the manual actions could require a considerable amount of time to complete,
some manual actions could be delayed by RCA portal-monitor alarms, and
only one NLO would have been available to complete all SSD manual actions.
The team concluded that the SSD NLO may not be able to accomplish some required manual actions In a timely manner. Consequently, some equipment relied on for SSD may not be available. For example, the SSD NLO may not be able to respond to a failed open steam generator PORV, locally throttle a steam generator PORV, or throttle AFW.
The team therefore considered AOP-36 to be inadequate.
Analysis This finding had more than minor significance because it affected the Mitigating Systems objectives of the Reactor Safety Cornerstone. The finding affected the availability and reliability of systems that mitigate initiating events to prevent undesirable consequences.
However, the finding was of very low safety significance because of the low fire initiation frequency, automatic sprinklers, fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor. Therefore, this finding is characterized as Green.
Enforcement As described in Section 1 R05.03.b.1 above, OLC 2.F required that equipment relied upon for SSD be physically protected from the fire. Also, TS 6.8.1 required procedures for implementing the fire protection program and for combating fires. In addition, OLC 2.F and the UFSAR, Section 9.5.1, FPP, included quality assurance requirements for fire protection. The FPP stated that a QA program was being used to identify and rectify any possible deficiencies in design, construction, and operation of the fire protection systems.
Contrary to the above requirements, the licensee failed to protect various equipment from the effects of a fire where that equipment was relied on for SSD. In addition, the licensee's corrective actions for a previous violation were inadequate. Because the licensee entered the finding into the corrective action program as AR 80215, this Item is being treated as an NCV in accordance with Section VI.A.1 of the NRC's Enforcement Policy. This item is identified as NCV 50-400/02-11-07, Too Many SSD Actions for Operators to Perform.
(4)
Using the BAT Without Level Indication Introduction The team identified an NCV of TS 6.8.1 for an inadequate procedure for SSD from a fire.
For a fire in SSA area 1-A-BAL-B, the SSD procedure directed operators to take CSIP suction from the BAT even if BAT level indication were lost. However, the charging volume needed for RCS cooldown would have emptied the BAT and damaged the SSD CSIP.
DescriDtion The team found that, for a fire In SSA area 1 -A-BAL-B-B2 or -B3, near the BAT, AOP-36 directed operators to use the BAT as a suction source for the CSIPs even If the BAT level indication was lost due to the fire. This alignment was to be used in preparation for and during a cooldown of the RCS. However, the team analyzed that the charging-volume needed for RCS cooldown would have emptied the BAT and damaged the SSD CSIP.
The SSA stated that, if BAT level Indication was lost due to a fire, then the RWST was to be used as a suction source for the CSIPs. However, this analysis was not implemented in AOP-36. AOP-36 was inadequate because it failed to recognize that the charging volume needed for RCS cooldown would have emptied the BAT and damaged the SSD CSIP.
Analysis This finding had more than minor significance because it affected the Mitigating Systems objectives of the Reactor Safety Cornerstone. The finding affected the availability and reliability of systems that mitigate initiating events to prevent undesirable consequences.
However, the finding was of very low safety significance because of the low fire initiation frequency, automatic sprinklers, fire brigade, and remaining SSD equipment to limit the
effects of a fire and to shut down the nuclear reactor. Therefore, this finding is characterized as Green.
Enforcement As described-in Sect~in R05.03ib.1 abo-ve, Ot2.FT redqit8lhat-equlpmunt relied-upon for SSD be. physically protected from the fire. Also, TS 6.8.1 required procedures for implementing the fire protection program and for combating fires.
Contrary to the above requirements, the licensee failed to protect the BAT level indication from effects of a fire where it was relied on for SSD, and the AOP-36 reliance on using the BAT without level indication was inadequate. Because the licensee entered the finding into the corrective action program as AR 75065, this item is being treated as an
.NCV in accordance with Section VI.A.1 of the NRC's Enforcement Policy. This item is
- -Is-idntifidns-56400/02i ltng thebBATIWIthout LeveaPtdioation a-t
.05 Emergency Communications a.
Inspection ScoDe The team reviewed the adequacy of the communication systems relied upon to coordinate the shutdown of the unit and fire brigade duties, including the site paging (PA), portable radio, and sound-powered phone systems. The team reviewed the licensee's portable radio channel features to assess whether the system and Its repeaters were protected from exposure fire damage. During walkdowns of sections of the post-fire SSD procedure, the team checked if adequate communications equipment would be available for the personnel performing the procedure. The team also reviewed the periodic testing of the site fire alarm and PA systems; maintenance checklists for the sound-powered phone circuits and amplifiers; and inventory surveillance of post-fire SSD operator equipment to assess whether the maintenance/surveillance test program for the communications systems was sufficient to verify proper operation of the systems.
b.
Findings No findings of significance were Identified.
.06 Emergency Liahting a.
inspection Scooe The team reviewed the design and operation of the direct current (DC) emergency lighting system self-contained, battery powered emergency lighting units (ELUs) as described in UFSAR Sections 9.5.1.2.2.e and 9.5.3. During plant walk downs of selected areas where operators performed local manual actions defined in the post-fire SSD procedure, the team inspected area ELUs for operability and checked the aiming of lamp heads to determine if adequate illumination was available to correctly and safely perform the actions required by the procedures. The team inspected emergency lighting features along access and egress pathways used during SSD activities for adequacy and personnel safety. The locations and identification numbers on the ELUs were compared
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to design drawings to confirm the as-built configuration. The team also checked If these battery power supplies were rated with at least an 8-hour capacity. In addition, the team
- -reviewed4he-manufacturefs-information-and -thelicensee]s-licensee-periodic i maintenance tests to verify that the ELUs were properly designed and were being maintained in an operable manner.
b.
Findinas "
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Introduction A violation of OLC 2.F was identified for failure to provide fixed, self-contained lighting with individual eight-hour-minimum battery power supplies in areas that must be manned for safe shutdown.
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In the SSA areas In which the team walked down safe shutdown manual actions, the team identified that the locations for local manual operator actions listed in Attachment 3 to this report would not be Illuminated by fixed, self-contained lighting with individual eight-hour-minimum battery power supplies.
The team observed that about 17 of the locations for local manual operator actions had no emergency lighting, as identified in Attachment 3. The team also observed that many more locations for local manual operator actions had fluorescent lights,-that would be powered by the safety-related emergency diesel generators, that could provide emergency Illumination. However, these lights did not meet the requirements for lights with eight-hour batteries. These locations are separately identified In Attachment 3.
Also, the team noted that the licensee had not requested NRC exemptions from the requirement to provide lights with eight-hour batteries.
The team also observed that all NLOs routinely carried flashlights and had access to more flashlights that were stored In the auxiliary building. The team assessed that, by using a flashlight, the SSD NLO would be able to perform the required actions but that those actions would take more time to perform when relying on illumination by a flashlight and could be less reliable.
Analysis This finding had more than minor safety significance because It affected the Mitigating Systems cornerstone. The finding affected the availability and reliability of systems that mitigate initiating events to prevent undesirable consequences. However, the finding was of very low safety significance because of the low fire initiation frequency and the effectiveness of automatic sprinklers (in all but the ACP fire area), fire brigade, and remaining SSD equipment to limit the effects of a fire and to shut down the nuclear reactor. Therefore, this finding is characterized as Green.
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Enforcement OLC 2. F. and UFSAR Section 9.5.1 stated that BTP 9.5-1 was used in the design of the fire protection program for safety-related systems and equipment and for other plant areas containing fire hazards that could adversely affect safety-related systems. BTP
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.~gite an Qofmmtrn7i to-rparagraph(1 );-required-that fixed setf-contained lighting consisting of fluorescent or sealed-1-lJ-ddWfnits with-individual-eightihoar--minimurr-batteiy power-supplies-should be-provided in-areas that must be manned for safe shutdown and for access and egress routes to and from all fire areas.
Contrary to the above requirements, the licensee failed to provide fixed self-contained lighting consisting of fluorescent or sealed-beam units with individual eight-hour-minimum battery power supplies in the location of the manual actions Identified above and listed in
_ Attachment 3. Because the licensee entered this finding into the corrective action-program-as -A t9 47,rfthlsviolation is-being ' reatbd as asn-NDVinaccordance with Section VL.A of the NRC's Enforcement Policy. This item is identified as NCV 50400/02-11-09, Failure to Provide Required Emergency Lighting for SSD Operator Actions.
.07 Cold Shutdown Repairs a.
Inspection Scope The team reviewed existing procedures and examined plant equipment to establish that the licensee had dedicated repair procedures, equipment, and materials to accomplish repairs of damaged components required for cold shutdown, that these components could be made operable, and that cold shutdown could be achieved within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The team examined cold shutdown repair equipment and replacement electrical power and control cables for systems needed to take the plant to cold shutdown following a large fire. The team evaluated the estimated manpower and the time required to perform post-fire repairs for reasonableness.
b.
Findincs No findings of significance were identified.
.08 Fire Barriers and Fire Area/Zone/Room Penetration Seals a.
InsDection ScoDe The team walked down the selected fire zones/areas to evaluate the adequacy of the fire resistance of barrier enclosure walls, ceilings, floors, and cable protection. This evaluation also included fire barrier penetration seals, fire doors, fire dampers, cable tray fire stops, and fire barrier partitions to ensure that at least one train of SSD equipment would be maintained free of fire damage from a single fire. The team observed the material condition and configuration of the installed fire barrier features and also reviewed construction details and supporting fire endurance tests for the installed fire barrier features. The team compared the observed fire barrier penetration seal
.configurations-to thekdesign-drawings and tested configurations. The team also compared the-penietratibifseal ratin-gs with tS tings-ftheburr in wihi r
thuy-were
installed. In addition, the team reviewed licensing documentation, engineering evaluations of Generic Letter 86-10 fire barrier features, and NFPA code deviations to
- - -verify-thatthe4ire-barrier-installations-met-design-requirements-andlicense commitments.
b.
Findings No findings of significance were identified.
.09 Fire Protection Systems. Features, and EguiDment a.
Insoection ScoDe The team reviewed flow diagrams, electrical schematic diagrams, periodic test procedures, engineering technical evaluations for NFPA code deviations, operational
--kalve-lineup procedures, and cable routing data for the power and control circuits of the motor-driven fire pump, the diesel-driven fire pump, and the fire protection water supply system yard mains. The review evaluated whether the common fire protection water delivery and supply components could be damaged or inhibited by fire-induced failures of electrical power supplies or control circuits and subsequent possible loss of fire water*
supply to the plant. Additionally, team members walked down the fire protection water supply system in selected fire areas to assess the adequacy of the system material condition, consistency of the as-built configuration with engineering drawings, and operability of the system in accordance with applicable administrative procedures and NFPA standards.
The team examined the adequacy of installed fire protection features in accordance with the fire area and system spatial separation and-design requirements In BTP CMEB 9.5-1.
The team walked down accessible portions of the fire detection and alarm systems In the selected fire areas to evaluate the engineering design and operation of the Installed configurations. The team also reviewed engineering drawings for fire detector spacing and locations in the four selected fire areas for consistency with the licensee's fire protection plan and the requirements in NFPA 72E.
The team also walked down the selected fire zones/areas with automatic sprinkler suppression systems installed to assure proper type, placement and spacing of the heads/nozzles and the lack of obstructions. The team examined vendor information, engineering evaluations for NFPA code deviations, and design calculations to verify that the required suppression system density for each protected area was available.
The team reviewed the adequacy of the design, installation and operation of the manual suppression standpipe and fire hose system for the selected fire areas. The team examined design calculations and evaluations to verify that the required fire hose water flow and sprinkler system density for each protected area were available. The team checked a sample of manual fire hose lengths to determine whether they would reach the SSD equipment. Additionally, the team observed placement of the fire hoses and extinguishers to assess consistency with the fire fighting pre-plan drawings.
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Findings
- CN~¶fdithryf significancevere-identif ied.
.10 Compensatory Measures a.
InsDection Scope The team reviewed the licensee's Fire Protection System Engineering Status Reviews which Identified each fire protection system's performance problems and regulatory issues. The team also reviewed the Fire Protection Out of Service Log generated for the last 18 months and associated compensatory measures. The review was performed to verify that the risk associated with removing fire protection and/or post4ire systems or components was properly assessed and adequate compensatory measures were
- 1mptemnred-irnac6ordance-withthe'ap'proved fire protection progratn.-r, fliw a-ce b.
Findings No findings of significance were identified.
4.
OTHER ACTIVMES (OA)
40A2 Identification and Resolution of Problems a.
Inspection Scope The team reviewed the corrective action program procedures and a selected sample of condition reports associated with the Harris FPP to verify that the licensee had an appropriate threshold for identifying Issues. The team also reviewed licensee audits and assessments of fire protection and safe shutdown. The team evaluated the effectiveness of the corrective actions for the identified issues.
b.
Findings The team found that licensee corrective actions for violation 50-400/02-08-01 regarding an inadequate fire barrier wall were Inadequate, in that the licensee's corrective actions for that violation contributed to three of the findings described above. However, because the net effect of corrective actions completed to date have significantly reduced the overall risk related to the finding, violation 50-400/02-08-01 is being closed at this time.
The team also found that licensee audits and self-assessments In the area of SSD were weak. The audits and self-assessments had not identified the types of findings that this inspection found. Contributing factors included a lack of attention to detail; for example, not tracing cable routings or walking down operator actions as was done In this inspection. In addition, the CP&L corporate Nuclear Assessment Section (NAS) audits of fire protection at Shearon Harris did not look at SSD. A Peer Report included In the November 2000 NAS audit of Shearon Harris fire protection stated: 'Harris NAS Fire Protection Program Audits of recent past have not included fire events safe shutdown within the scope of the audits due to a reliance on engineering self-assessments. It Is
the opinion of the auditor that the scope of future Harris NAS Fire Protection assessments should include fire events safe shutdown related documentation and activities." However, the team noted that subsequent NAS audits of Harris fire protection did not audit SSD.
The team noted that the licensee's initial corrective actions to the findings described in this report were timely and responsive. The licensee revised SSD procedures three times during the inspection, made a 10 CFR 50.72 report to the NRC, and stationed an additional SSD NLO.
40A6 Meetings Exit Meeting Summary The team presented the inspection results to you and members of your staff at the conclusion of the inspection on December 20, 2002. You acknowledged the findings presented. Proprietary information is not included In this inspection report.
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SUPPLEMENTAL INFORMATION Partial List of Persons Contacted Licer (a,-
D. Baksa, Supervisor, Equipment Pera J. Caves, Licensing Supervisor R. Duiqc~~, DPjctor of Site Operations M. Fletcher, Manager, Fire Protection Program P. Fulford, Superintendent, Design Engineering C. Georgeson, Supervisor, EI&C Design W. Gregory, Operations Fire Protection Specialist W. Gurganion, Manager, NAS T. Hobbs, Manager, Operations A. Khanpour, Manager, Engineering F. Lane,Jr, SeniorNuclear-Work-Maibagement;Speeiallt----
J. Laque, Manager, Maintenance T. Morton, Site Services Manager J. Scarola, Site Vice President B. Waldrep, Plant General Manager NRC J. Brady, Senior Resident Inspector, Shearon Harris H. Christensen, Deputy Director, Division of Reactor Safety (DRS), Region II (Rll)
C. Ogle, Chief, Engineering Branch 1, DRS, RI!
Items O~ened. Closed, and Discussed ODened 50-400/02-11-01 50-400/02-11-02 50-400/02-11-03 50-400/02-11-04 NCV NCV NCV NCV Failure to Protect Charging System MOV 1 CS-1 65, VCT Outlet to CSIPs, From Maloperation Due To a Fire (Section 1 R05.03.b.1)
Failure to Protect Component Cooling MOVs 1CC-251 and 1 CC-208, CC for RCP Seals, From Maloperation Due To a Fire (Section 1 R05.03.b.2)
Failure to Protect Charging System MOVs 1 CS-1 69, 1 CS-214, 1 CS-218, and I CS-21 9 From Maloperation Due To a Fire (Section 1 R05.03.b.3)
Failure to Protect Charging System MOVs 1 CS-1 66, 1 CS-168, and 1CS-217 From Maloperation Due To a Fire (Section 1 R05.03.b.4)
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50-400/02-11-05 50-400/02-11-06 URI NCV Reliance on Manual Actions in Place of Required Physical Separation or Protection From a Fire (Section 1 R05.04.b.1)
Fire SSD Operator Actions With Excessive Challenges (Section 1 R05.04.b.2)
50-400/02-11-07 NCV Too Many Fire SSD Actions for Operators to Perform
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50-400/02-11-08 50-400/02-11-09 NCV NCV Using the Boric Acid Tank Without Level Indication (Section 1 R05.04.b.4)
Failure to Provide Required Emergency Lighting for SSD Operator Actions (Section 1 R05.06.b)
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, s Closed 50-400/02-08-01 VIO Failure to Implement and Maintain NRC Approved Fire Protection Program Safe Shutdown System Separation Requirements (Section 40A2.b)
Discussed None Attachment 1