ENS 43276
ENS Event | |
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08:58 Feb 25, 2007 | |
Title | Invalid Secondary Containment Isolation |
Event Description | The following information is provided as a 60 day telephone notification to NRC under 10 CFR 50.73(a)(1) in lieu of submitting a written LER to report a condition that resulted in an invalid actuation of the 10CFR50.73(a)(2)(iv)(B) [general containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves]. NUREG1022 Revision 2 identifies the information that needs to be reported as discussed below.
(a) The specific train(s) and system(s) that were actuated. This report is being made under 10CFR50.73(a)(2)(iv)(a). On February 25, 2007 at 3:58 AM EST Units 1 and 2 received an invalid full Secondary Containment Isolation. The following initiations and isolations were observed: All Fission Product Monitor Valves isolated, both Units' SBGT trains initiated and the reactor building ventilation supply and exhaust fans tripped and isolated, and the refueling floor ventilation supply and exhaust fans tripped and isolated. Operations personnel verified that all Secondary Containment isolations and initiations occurred as expected. The isolation was caused by a blown fuse. During investigation into the Secondary Containment isolation, fuse 1D11A-F14A in panel 1H11-P606 was found to be blown. After replacing this fuse, the isolation signal cleared and all related systems were returned to normal operation. Fuse 1D11A-F14A supplies the trip auxiliary units 1C51A-Z2A and 1C51A-Z2C. Loss of power to these units de-energizes several relays which are also deenergized as a result of a Refueling Floor Vent High Radiation signal which would actuate the same isolation logic and cause an SBGT initiation. (b) Whether each train actuation was complete or partial. The four Standby Gas Treatment (SBGT) fans auto started and both Unit One and Unit Two reactor building and refueling floor normal ventilation systems automatically shutdown and isolated. The SBGT initiation and the ventilation system shutdown were both complete actuations. (c) Whether or not the system started and functioned successfully. The above system functioned successfully. The licensee will inform the NRC Resident Inspector. |
Where | |
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Hatch ![]() Georgia (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+918.05 h38.252 days <br />5.465 weeks <br />1.258 months <br />) | |
Opened: | Jim Anderson 14:01 Apr 4, 2007 |
NRC Officer: | Pete Snyder |
Last Updated: | Apr 4, 2007 |
43276 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 568972023-11-02T01:11:0002 November 2023 01:11:00
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