ENS 42492
ENS Event | |
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06:50 Feb 28, 2006 | |
Title | Invalid System Actuation Due to Work Instruction Error |
Event Description | General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves.
The following information is provided as a 60 day telephone notification to NRC under 10 CFR 50.73(a)(1) in lieu of submitting a written LER to report a condition that resulted in an invalid actuation of the 10CFR50.73(a)(2)(iv)(B) system checked above. NUREG1022 Revision 2 identifies the information that needs to be reported as discussed below. (a) The specific train(s) and system(s) that were actuated. This report is being made under 10CFR50.73(a)(2)(iv)(A). On February 28, 2006 at 02:50 EST the implementation of Work Order 1051442601, to perform a routine replacement of a relay 1C61-K86, called for lifting of wires related to the relay. During the evolution, the lifting of wires at CC-107 in panel 1 H11-P623 resulted in a daisy chain effect and the auto start of all four Standby Gas Treatment (SBGT) fans. Both the Unit One and Unit Two reactor building and refueling floor normal ventilation systems automatically shutdown and isolated. These actuations were a result of the loss of power to relay 1C61-K75. This relay initiates the logic for isolation of the reactor building and refueling floor ventilation and initiation of SBGT. Subsequent investigation determined that in order to prevent this daisy chain effect the wires should have been lifted at DDD-1 in panel 1H11-P623. This error was the result of inadequate work instructions. (b) Whether each train actuation was complete or partial. The four Standby Gas Treatment (SBGT) fans auto started and both Unit One and Unit Two reactor building and refueling floor normal ventilation systems automatically shutdown and isolated. The SBGT initiation and the ventilation system shutdown were both complete actuations. (c) Whether or not the system started and functioned successfully. The above systems functioned successfully. The licensee will notify the NRC Resident Inspector. |
Where | |
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Hatch Georgia (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1035.8 h43.158 days <br />6.165 weeks <br />1.419 months <br />) | |
Opened: | Alan Wolfe 09:38 Apr 12, 2006 |
NRC Officer: | Bill Huffman |
Last Updated: | Apr 12, 2006 |
42492 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 568972023-11-02T01:11:0002 November 2023 01:11:00
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