ENS 47337
ENS Event | |
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09:03 Aug 12, 2011 | |
Title | 60 Day Optional Telephone Notification for an Invalid Specified System Actuation |
Event Description | On August 12, 2011, while removing the Unit 2, Division II 24/48 volt DC Cabinet 2B from service for planned maintenance, Unit 2 secondary containment and partial Group II primary containment isolation signals were initiated upon disconnecting the battery with the following systems and components successfully started and actuated as designed:
- Unit 1 and 2 Standby Gas Treatment (SGT) systems automatically started - Complete actuation of Unit 2 secondary containment isolation devices in system 2T41 - Partial Group 2 primary containment isolation devices in systems in Division II associated with the 2D11, 2P33, and 2T48 systems. The procedure for rotating the affected battery chargers did not contain adequate direction to ensure the charger was functioning properly before disconnecting the associated battery in preparation for its replacement. This actuation was confirmed to be an invalid actuation as an unplanned response associated with this maintenance activity. Therefore, the event is not reportable under 10CFR50.72(b)(3)(iv), since it was not a valid actuation. In accordance with 10CFR50.73(a)(1) the option of reporting this event as a telephone notification within 60 days is being used. The event is reportable under 10CFR50.73(a)(2)(iv)(A) because the actuations were not planned and were not expected to occur. In this case the systems to which the requirements of 10CFR50.73(a)(2)(iv)(A) apply are general containment (primary and secondary) isolation signals as described in 10CFR50.73(a)(2)(iv)(B)(2) for the 'B' logic resulting in isolation of the associated valves on Unit 2, thereby affecting containment isolation valves in more than one system. Control room personnel restored the Unit 2, Division II 24/48 volt DC Cabinet 2B and the condition was cleared. The licensee notified the NRC Resident Inspector. |
Where | |
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Hatch Georgia (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1443.78 h60.158 days <br />8.594 weeks <br />1.978 months <br />) | |
Opened: | G. S. Griffis 12:50 Oct 11, 2011 |
NRC Officer: | Donald Norwood |
Last Updated: | Oct 11, 2011 |
47337 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (98 %) |
After | Power Operation (98 %) |
WEEKMONTHYEARENS 568972023-11-02T01:11:0002 November 2023 01:11:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60 Day Notification for an Invalid Specified System Actuation ENS 551882021-02-18T03:20:00018 February 2021 03:20:00 10 CFR 50.73(a)(1), Submit an LER Automatic Actuation of Group 2 Containment Isolation Logic ENS 551872021-02-13T03:23:00013 February 2021 03:23:00 10 CFR 50.73(a)(1), Submit an LER Automatic Actuation of Group I Containment Isolation Logic ENS 538172018-11-12T05:00:00012 November 2018 05:00:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 528182017-04-27T04:29:00027 April 2017 04:29:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to Failed Relay ENS 528032017-04-17T15:20:00017 April 2017 15:20:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid Specified System Actuation ENS 526852017-02-17T15:21:00017 February 2017 15:21:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid Specified System Actuation ENS 496412013-10-21T09:19:00021 October 2013 09:19:00 10 CFR 50.73(a)(1), Submit an LER 60 Optional Report - Invalid Partial Reactor Protection System Actuation ENS 490552013-03-24T14:09:00024 March 2013 14:09:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Hpci Suction Valves ENS 487212012-12-08T06:16:0008 December 2012 06:16:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephone Notification of Invalid System Actuation ENS 485652012-10-08T22:09:0008 October 2012 22:09:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid System Actuation ENS 483702012-08-06T01:25:0006 August 2012 01:25:00 10 CFR 50.73(a)(1), Submit an LER Rps Sub-Component Failure Caused Half Scram with Group 2 Pciv Actuation ENS 478592012-02-25T05:38:00025 February 2012 05:38:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Standby Gas Treatment Secondary Containment Isolation Valves (Scivs) ENS 473372011-08-12T09:03:00012 August 2011 09:03:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Telephone Notification for an Invalid Specified System Actuation ENS 461152010-05-29T12:49:00029 May 2010 12:49:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Primary Containment Isolation Valves Due to a Faulty Transistor ENS 459812010-04-16T23:15:00016 April 2010 23:15:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 458352010-02-23T14:50:00023 February 2010 14:50:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Standby Gas Treatment System ENS 432762007-02-25T08:58:00025 February 2007 08:58:00 10 CFR 50.73(a)(1), Submit an LER Invalid Secondary Containment Isolation ENS 424922006-02-28T06:50:00028 February 2006 06:50:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation Due to Work Instruction Error ENS 421102005-10-07T15:37:0007 October 2005 15:37:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 415902005-02-19T10:50:00019 February 2005 10:50:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Invalid Actuation of System Report. 2023-11-02T01:11:00 | |