ENS 48370
ENS Event | |
---|---|
01:25 Aug 6, 2012 | |
Title | Rps Sub-Component Failure Caused Half Scram with Group 2 Pciv Actuation |
Event Description | On August 5, 2012, at 21:25 EDT, Unit 1 received a Reactor Auto SCRAM System 'A' Trip signal in the main control room. The annunciator was initially reset by operators, but the operating crew noted that some white SCRAM lights and some Group 2 PCIV indication lights were flickering in the control room. This anomaly coupled with the ability to reset the annunciated condition immediately indicated an issue with fluctuating voltage on the power supply for RPS [Reactor Protection System] 'A'. Approximately 30 seconds after the annunciator was reset, the 'A' RPS bus tripped, causing a half SCRAM in conjunction with the automatic actuation of the Standby Gas Treatment system (SGT) and isolation of PCIVs in multiple systems, both of which are normal responses to this loss of the 'A' RPS bus. The crew entered the appropriate abnormal operating procedures and confirmed the actuations automatically occurred as required given the loss of the RPS bus. They investigated the 'A' RPS Motor/Generator (M/G) set, placed the 'A' RPS bus on its alternate supply, reset the SGT and PCIV actuation logic, and returned the PCIVs to their normal position.
Upon investigation, the 'A' RPS M/G set was found running, but the Over Voltage Relay in the power monitoring cabinet was chattering. The field investigation team determined that the RPS trip was caused by the failure of its voltage regulator which was then replaced. The 'A' RPS M/G set was consequently returned to service as the primary RPS power source on August 6, 2012. Maintenance personnel subsequently determined that a voltage regulator subcomponent was defective. Because the malfunctioning subcomponent caused the loss of RPS 'A' as the initiating event rather than a valid SGT or PCIV actuation signal, the resulting actuation of SGT and the isolation of multiple PCIVs are considered invalid actuations. Based on that information, 10CFR50.73(a){2)(iv) allows this event to be reported via a telephone notification within 60 days instead of submitting a written LER. The licensee has notified the NRC Resident Inspector. |
Where | |
---|---|
Hatch Georgia (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1403.02 h58.459 days <br />8.351 weeks <br />1.922 months <br />) | |
Opened: | Kenny Hunter 12:26 Oct 3, 2012 |
NRC Officer: | John Knoke |
Last Updated: | Oct 3, 2012 |
48370 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 48370\u003C/a\u003E - \u003Ca href=\"/Hatch\" title=\"Hatch\"\u003EHatch\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003ERps Sub-Component Failure Caused Half Scram with Group 2 Pciv Actuation\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 48370 - Hatch\n","link":"","lat":31.93298888888889,"lon":-82.34381666666667,"icon":"/w/images/1/14/Southern_Nuclear_icon.png"}],"imageoverlays":null} | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (98 %) |
After | Power Operation (98 %) |
Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (98 %) |
After | Power Operation (98 %) |
WEEKMONTHYEARENS 568972023-11-02T01:11:0002 November 2023 01:11:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60 Day Notification for an Invalid Specified System Actuation ENS 551882021-02-18T03:20:00018 February 2021 03:20:00 10 CFR 50.73(a)(1), Submit an LER Automatic Actuation of Group 2 Containment Isolation Logic ENS 551872021-02-13T03:23:00013 February 2021 03:23:00 10 CFR 50.73(a)(1), Submit an LER Automatic Actuation of Group I Containment Isolation Logic ENS 538172018-11-12T05:00:00012 November 2018 05:00:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 528182017-04-27T04:29:00027 April 2017 04:29:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to Failed Relay ENS 528032017-04-17T15:20:00017 April 2017 15:20:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid Specified System Actuation ENS 526852017-02-17T15:21:00017 February 2017 15:21:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid Specified System Actuation ENS 496412013-10-21T09:19:00021 October 2013 09:19:00 10 CFR 50.73(a)(1), Submit an LER 60 Optional Report - Invalid Partial Reactor Protection System Actuation ENS 490552013-03-24T14:09:00024 March 2013 14:09:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Hpci Suction Valves ENS 487212012-12-08T06:16:0008 December 2012 06:16:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephone Notification of Invalid System Actuation ENS 485652012-10-08T22:09:0008 October 2012 22:09:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid System Actuation ENS 483702012-08-06T01:25:0006 August 2012 01:25:00 10 CFR 50.73(a)(1), Submit an LER Rps Sub-Component Failure Caused Half Scram with Group 2 Pciv Actuation ENS 478592012-02-25T05:38:00025 February 2012 05:38:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Standby Gas Treatment Secondary Containment Isolation Valves (Scivs) ENS 473372011-08-12T09:03:00012 August 2011 09:03:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Telephone Notification for an Invalid Specified System Actuation ENS 461152010-05-29T12:49:00029 May 2010 12:49:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Primary Containment Isolation Valves Due to a Faulty Transistor ENS 459812010-04-16T23:15:00016 April 2010 23:15:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 458352010-02-23T14:50:00023 February 2010 14:50:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Standby Gas Treatment System ENS 432762007-02-25T08:58:00025 February 2007 08:58:00 10 CFR 50.73(a)(1), Submit an LER Invalid Secondary Containment Isolation ENS 424922006-02-28T06:50:00028 February 2006 06:50:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation Due to Work Instruction Error ENS 421102005-10-07T15:37:0007 October 2005 15:37:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 415902005-02-19T10:50:00019 February 2005 10:50:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Invalid Actuation of System Report. 2023-11-02T01:11:00 | |