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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000457/LER-1993-0061993-08-26026 August 1993 LER 93-006-00:on 930727,2A RHR Pump Motor Bearing Oil Reservoir Unable to Be Drained,During Oil Change.Caused by Corrosion Particles Resulting from Previous Seal Leak.Rhr 2A Pump replaced.W/930826 Ltr 05000457/LER-1993-0041993-08-11011 August 1993 LER 93-004-00:on 930712,time Frame for Performing Core Normalization Surveillance Exceeded Due to Personnel Error. Commenced Performance of Required Surveillance.Surveillance Procedure Bwvs 1.1.1.2-1 Will Be revised.W/930811 Ltr 05000457/LER-1990-0101990-07-0303 July 1990 LER 90-010-00:on 900609,reactor Trip Occurred During Plant Startup from Low Steam Generator Water Level.Caused by Malfunctioning Bypass Feedwater Regulating Valve.Operator Training provided.W/900706 Ltr 05000457/LER-1990-0091990-07-0202 July 1990 LER 90-009-00:on 900604,pressures for Active & Standby Accumulators Identified to Be Below 4,800 Psig Required for Operability.Caused by Component Failure.Four Way Valve & Hydraulic Oil Filter Used for MSIV replaced.W/900629 Ltr 05000456/LER-1990-0081990-07-0202 July 1990 LER 90-008-00:on 900608,reactor Trip Occurred Due to High Flux Rate Signal from Power Range Nuclear Instrumentation. Caused by Voltage Transient,Resulting from Lightning Striking Containment.Power Supply reset.W/900629 Ltr 05000456/LER-1990-0071990-06-28028 June 1990 LER 90-007-00:on 900601,during Removal of Ohmmeter Probe, Operator Touched Probe to Exposed Terminal Point,Resulting in Automatic Start of Auxiliary Feedwater Pump 1A.Caused by Methodology Deficiency.Probes modified.W/900628 Ltr 05000457/LER-1990-0061990-06-18018 June 1990 LER 90-006-00:on 900521,containment Fuel Handling Incident Area Radiation Monitor Failed Automatic Checksource Test Due to Low Count Rate.Caused by Component Failure.Detector replaced.W/900618 Ltr 05000457/LER-1990-0051990-05-24024 May 1990 LER 90-005-00:on 900426,discovered That Diesel Generator 2A Starting Air Distribution Sys Tubing Crisscrossed to Cylinders 6L & 9L.Caused by Preservice Mfg Deficiency. Custom-routed Airlines replaced.W/900524 Ltr 05000457/LER-1990-0041990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillations Occurred Due to Defective Resistor.Caused by Failure of One Dropping Resistor in Governor Unit.Resistors replaced.W/900516 Ltr 05000456/LER-1988-012, Advises That LER 88-012-00 Withdrawn.Investigation Revealed That Operator Did Indicate That Room Temps Less than Tech Spec Limits1989-04-21021 April 1989 Advises That LER 88-012-00 Withdrawn.Investigation Revealed That Operator Did Indicate That Room Temps Less than Tech Spec Limits ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 1993-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20196A0721999-03-16016 March 1999 Cycle 8 COLR in ITS Format & W(Z) Function ML20207J4371999-03-0808 March 1999 ISI Outage Rept for A1R07 ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With ML20206U9011999-02-15015 February 1999 COLR for Braidwood Unit 2 Cycle 7. Page 1 0f 13 of Incoming Submittal Was Not Included BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20206U9081998-12-17017 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154D4401998-10-0202 October 1998 Safety Evaluation Authorizing Second 10-yr Interval ISI Program Request for Relief 12R-30 for Plant,Units 1 & 2 ML20155C2601998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Braidwood Generating Station,Units 1 & 2 ML20195F5911998-09-11011 September 1998 Special Rept:On 980812,addl Unseated Wires Were Discovered. Cause Is Unknown at Present Time.Util Evaluated Number of Unseated/Ineffective Wires & Determined Effect on Containment Structural Integrity.Commitments,Encl ML20196B3711998-09-0808 September 1998 Cycle 8 Operating Limits Rept (Olr) ML20151X6671998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Braidwood Generating Station,Units 1 & 2.With ML20238F3281998-08-31031 August 1998 SER Approving Second 10-year Interval Inservice Insp Program Request for Relief 12R-14 for Braidwood Station,Units 1 & 2 ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A1091998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Braidwood Generating Station,Unit 1 & 2 ML20236N7001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Braidwood Generating Station,Units 1 & 2 ML20198A0151998-06-18018 June 1998 10CFR50.59 Summary Rept 960619 Through 980618, Vols I & Ii,Consisting of Descriptions & SE Summaries for Changes to Procedural UFSAR Changes,Tests & Experiments & FP Rept.Without Fp,Rept ML20249A5451998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Braidwood Generating Station Units 1 & 2 ML20247F7711998-05-0808 May 1998 Special Rept:On 980403 & 980503 Seismic Monitoring Sys Was Declared Inoperable.Caused by 5-volt Power Supply & Regulator Card Failure.Imd & Sys Engineering Are Continuing to Identify & Resolve Problems So Sys Can Be Operable ML20247L7591998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Braidwood Generating Station,Units 1 & 2 ML20217K6331998-04-20020 April 1998 Safety Evaluation Accepting Methodology & Criteria Used in Generating Flaw Evaluation Charts for RPV of Braidwood IAW Section XI of ASME Code ML20216C6621998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Braidwood Generating Station,Units 1 & 2 1999-09-30
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/ \ Commonweshh Edison !
I4.'* .
i
/ Braldwood Nuclear Pow:r Stati;n
(
) Route #1. Box 84
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' ~ '
'/ Braceville, Illinois 60407 ,
L/ Telephone 815/458 2801 i
'l July 6,1990 3 BW/90-0694 1
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U. S. Nuclear Regulatory Commission Document Control Desk 1 Washington, D.C. 20555 1
Dear Sir:
The enclosed Licensee Event Report from Braldwood Generating Station is being transmitted to you in accordance with the requirements of '
10CFR50.73(a)(2)(lv) which requires a 30-day written report.
This report is number 90-010-00; Docket No. 50-457.
Very truly yours, L r R. E. Querlo l Station Manager -
i Braidwood Nuclear Station REQ /JDW/sjs (7126z) r l;
Enclosure:
Licensee Event Report No. 90-010-00 cc: NRC Region !!! Administrator i NRC Resident inspector l: INPO Record Center <
CECO Distribution List I
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! ilde (4) Reacter Trip During Plant $ tart tip Free Low $ teen Ger.arator Water level due to a Halfunctienlog Dypass feedwater Repulettog valve.
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. 20.402(b) , 20.405(c) _A., 10.73(a)(2)(iv) __,,, 73.71(b)
P0dCR 20.405(a)(1)(1) ___ 50.36(c)(1) 50.73(a)(2)(v) . _ , 73.71(c)
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A unit start up was in progress. Feedwater (FW) flow was being controlled in automatic by the Bypass FW R:pulating valves (BFRV). $teamline header pressure was being tontrolled in automatic by the $ lear Dumps. At 0030 on Sune 9,1990 a Reactor Operator (RO), who was monitoring the rw panel, observed that indicated level on the 2B Steam Generator ($G) had decreased to 35%. This was below the set point of 501.. The RO placed the co. troller in manual and increased the output to raise $G 1evel. 2B $G 1evel continued to decrease froe the
'shrid' etfeet of the cold FW. The Supervisor ($RO) directed the RO who was monitoring Reactor Control panel, to trithdra. cetrel rods to increase temperature and *$well" Le level. $G 1evel increased f roe an initisi value of 2fl% to 24%. .st 0039 the ef fects of the increase' heat input caused stearline pressure to increase which causid the $ tear Dump Valves to cycle. This created a level perturbation which caused the level in the 2B $G to decrease below the Reactor Trip 5et peint of 171 anf a Reactor trip occurred. The cause of the event was a malfunctioning BFFV which would stich during operation in the lower third of valve travel. The valve pac 6ing was 1:es;ned and valve travel was smooth and acceptable. Operator training will be provided, previous corrective actions are tot applicat.le. ;
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'A. tier.t Condittens Prior to tient:
tinitt Breldwood 2: Event Date: June 9. 1990: Event time: 0039; Mode! ? . I'c.er Operetten; b power: 15t; RC$ (ABe) Temperature / pressure: NOT/N0p; B. Description of twent:
I i
A unit start up was in progress in accordante with approved procedures. Rtatter power was at $1. and being increased to approelmately 15% in preparations fot Main Turbine start up, f ee=ater (rW) ($J) flo was being .
controlled in automatic by the Bypass fW Regulating Valves (BTRV). $ttamiine Header l'ressure ($B) was being l c;ntrolled in autoastic at 1092 psig by the $ team Dumps.
t At 0030 on June 9,1990 the Nuclear $tation Operator (N$0) (Licensed Reactor Operator) who was manitoring the FW panel, observed that indicated level on the 2B $tese Generator ($G) (09) had detressed to 35% narrow range ,
scale. This was significantly below the normal control set point of $0%. The N$0 observed that the output from the controller for the 2B $fRV indicated C. The N$0 placed the controller in manual and increased the entro11er output in an attempt to raise SG 1evel. 2B SG 1evel indicated 32% at this time and continued to decrease free the 'shrint* effect of the cold TW addition.
The Shif t Engineer ($t) (Licensed Senior Reactor Opetetor) directed the N$0 who was monitoring Reetter Control Panel, to withdraw control rods in an ef fort to increase temperature and *$well* the level in the
$Gs. The N30 withdrew the control rods and observed the resultant increases in RC$ temperature and $G 1evel. 4
$G 1evel increased free an initial value of 20% to 241. and reactor pc.er mas indicating 111..
At 0039 the effects of the increased heat input to the $Gs caused steamline pre;sure to increase. This !
caused the $ tram Dump valves, which were contro11tng in auto, to cycle. This created a level perturbation on the $G 1esel contro'. systee which caused the level in the 2B $G to decrease *oelo= the reactor Trip $et point of 17% and a Reactor trip occurred. The N$0s verified all avtomatic actions. All systems functioted as de signed. Stable conditions were immediately established.
The appropriate NRC notification via the (N$ phone systee was made at 0108 pursuant to 10CFR$0.72(b)(2)(ii).
This event is being reported pursuant to 10CFeh0.73(a)(2)(iv) . any event or condition that resulted in manual or automatic actuation of any [ngineered $t6fety festure, including the peetter protection $ystem, C. Cause of tvent:
i The root cause of this event was a malfunctioning valve. The malfunction of the El BrRV created a low level condition in the 2B $G. During the action to recover level, the addition of the cold FW combined with the cycling of the Steam Deps created a tendition that caused the Indicated level in the 2D $G to decrease below the Reactor trip set point. 1he sequence of events initiated by the malfunction of the 2B BFRV caused the cy:nt.
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D. Safety Analysis:
This event had no effect on the safety of the plant or the public. All systee's operated as designed.
A:siliary Fetdwater attuated at.) restored $G tevels as designed.
Under the worst case condition of a low $G 1evel occurring with the Unit operettop at 1001. Power there would still be no effett. The Engineered Safety feature Attuation System (t$F) would initiate a Reatter Trip, turbine Trip and Auriliary f eed= ster Actuation free either of the two redundant Trains of ($f both of which were operable and evaliable for this event.
L. Correttive Actions:
f reuble shooting was i.erfumed on both the instrument control loop for the 2B Bf RV arid the valve itself.
2F WOS20A. All portions of the control loop tested out satisf actorily. The valve emperiented sticking and jer6y motion when operated in the lower third of valve travel. The valve packing was loosened and valve travel was smooth and acceptable during additional testing. The valve has performed acceptably at maintaining $G level in automatic since making the pocling adjustment.
This event will be included it, the titensed Drerator Requalification Training program as part of the continuing ef fort to share experiente on level control of the Model D-5 $Gs during low power operation, this action will be tracked to completion by action itee 457-000-90-02601.
F, provious occurrences:
fl.ere have been previous occurrentes of t$F actuations as a result of level perturbations occurring on the Unit 2 Model 0-$ Steam Generators during low power opers'. tons. The corrective actions were implemented addressing both root and contributing causes, previous torrective actions are not applicable to this event.
G. Component Islivre Data:
!$4(1U1411ERI N98tElitEt Min. pari A fisher Controls Co. tevel Control valve 667-55-79 i
I l l 3044m(070290)4
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05000457/LER-1990-004 | LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillations Occurred Due to Defective Resistor.Caused by Failure of One Dropping Resistor in Governor Unit.Resistors replaced.W/900516 Ltr | | 05000457/LER-1990-005 | LER 90-005-00:on 900426,discovered That Diesel Generator 2A Starting Air Distribution Sys Tubing Crisscrossed to Cylinders 6L & 9L.Caused by Preservice Mfg Deficiency. Custom-routed Airlines replaced.W/900524 Ltr | | 05000457/LER-1990-006 | LER 90-006-00:on 900521,containment Fuel Handling Incident Area Radiation Monitor Failed Automatic Checksource Test Due to Low Count Rate.Caused by Component Failure.Detector replaced.W/900618 Ltr | | 05000456/LER-1990-007 | LER 90-007-00:on 900601,during Removal of Ohmmeter Probe, Operator Touched Probe to Exposed Terminal Point,Resulting in Automatic Start of Auxiliary Feedwater Pump 1A.Caused by Methodology Deficiency.Probes modified.W/900628 Ltr | | 05000456/LER-1990-008 | LER 90-008-00:on 900608,reactor Trip Occurred Due to High Flux Rate Signal from Power Range Nuclear Instrumentation. Caused by Voltage Transient,Resulting from Lightning Striking Containment.Power Supply reset.W/900629 Ltr | | 05000457/LER-1990-009 | LER 90-009-00:on 900604,pressures for Active & Standby Accumulators Identified to Be Below 4,800 Psig Required for Operability.Caused by Component Failure.Four Way Valve & Hydraulic Oil Filter Used for MSIV replaced.W/900629 Ltr | | 05000457/LER-1990-010 | LER 90-010-00:on 900609,reactor Trip Occurred During Plant Startup from Low Steam Generator Water Level.Caused by Malfunctioning Bypass Feedwater Regulating Valve.Operator Training provided.W/900706 Ltr | |
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