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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000457/LER-1993-0061993-08-26026 August 1993 LER 93-006-00:on 930727,2A RHR Pump Motor Bearing Oil Reservoir Unable to Be Drained,During Oil Change.Caused by Corrosion Particles Resulting from Previous Seal Leak.Rhr 2A Pump replaced.W/930826 Ltr 05000457/LER-1993-0041993-08-11011 August 1993 LER 93-004-00:on 930712,time Frame for Performing Core Normalization Surveillance Exceeded Due to Personnel Error. Commenced Performance of Required Surveillance.Surveillance Procedure Bwvs 1.1.1.2-1 Will Be revised.W/930811 Ltr 05000457/LER-1990-0101990-07-0303 July 1990 LER 90-010-00:on 900609,reactor Trip Occurred During Plant Startup from Low Steam Generator Water Level.Caused by Malfunctioning Bypass Feedwater Regulating Valve.Operator Training provided.W/900706 Ltr 05000457/LER-1990-0091990-07-0202 July 1990 LER 90-009-00:on 900604,pressures for Active & Standby Accumulators Identified to Be Below 4,800 Psig Required for Operability.Caused by Component Failure.Four Way Valve & Hydraulic Oil Filter Used for MSIV replaced.W/900629 Ltr 05000456/LER-1990-0081990-07-0202 July 1990 LER 90-008-00:on 900608,reactor Trip Occurred Due to High Flux Rate Signal from Power Range Nuclear Instrumentation. Caused by Voltage Transient,Resulting from Lightning Striking Containment.Power Supply reset.W/900629 Ltr 05000456/LER-1990-0071990-06-28028 June 1990 LER 90-007-00:on 900601,during Removal of Ohmmeter Probe, Operator Touched Probe to Exposed Terminal Point,Resulting in Automatic Start of Auxiliary Feedwater Pump 1A.Caused by Methodology Deficiency.Probes modified.W/900628 Ltr 05000457/LER-1990-0061990-06-18018 June 1990 LER 90-006-00:on 900521,containment Fuel Handling Incident Area Radiation Monitor Failed Automatic Checksource Test Due to Low Count Rate.Caused by Component Failure.Detector replaced.W/900618 Ltr 05000457/LER-1990-0051990-05-24024 May 1990 LER 90-005-00:on 900426,discovered That Diesel Generator 2A Starting Air Distribution Sys Tubing Crisscrossed to Cylinders 6L & 9L.Caused by Preservice Mfg Deficiency. Custom-routed Airlines replaced.W/900524 Ltr 05000457/LER-1990-0041990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillations Occurred Due to Defective Resistor.Caused by Failure of One Dropping Resistor in Governor Unit.Resistors replaced.W/900516 Ltr 05000456/LER-1988-012, Advises That LER 88-012-00 Withdrawn.Investigation Revealed That Operator Did Indicate That Room Temps Less than Tech Spec Limits1989-04-21021 April 1989 Advises That LER 88-012-00 Withdrawn.Investigation Revealed That Operator Did Indicate That Room Temps Less than Tech Spec Limits ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 1993-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20196A0721999-03-16016 March 1999 Cycle 8 COLR in ITS Format & W(Z) Function ML20207J4371999-03-0808 March 1999 ISI Outage Rept for A1R07 ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With ML20206U9011999-02-15015 February 1999 COLR for Braidwood Unit 2 Cycle 7. Page 1 0f 13 of Incoming Submittal Was Not Included BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20206U9081998-12-17017 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154D4401998-10-0202 October 1998 Safety Evaluation Authorizing Second 10-yr Interval ISI Program Request for Relief 12R-30 for Plant,Units 1 & 2 ML20155C2601998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Braidwood Generating Station,Units 1 & 2 ML20195F5911998-09-11011 September 1998 Special Rept:On 980812,addl Unseated Wires Were Discovered. Cause Is Unknown at Present Time.Util Evaluated Number of Unseated/Ineffective Wires & Determined Effect on Containment Structural Integrity.Commitments,Encl ML20196B3711998-09-0808 September 1998 Cycle 8 Operating Limits Rept (Olr) ML20151X6671998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Braidwood Generating Station,Units 1 & 2.With ML20238F3281998-08-31031 August 1998 SER Approving Second 10-year Interval Inservice Insp Program Request for Relief 12R-14 for Braidwood Station,Units 1 & 2 ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A1091998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Braidwood Generating Station,Unit 1 & 2 ML20236N7001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Braidwood Generating Station,Units 1 & 2 ML20198A0151998-06-18018 June 1998 10CFR50.59 Summary Rept 960619 Through 980618, Vols I & Ii,Consisting of Descriptions & SE Summaries for Changes to Procedural UFSAR Changes,Tests & Experiments & FP Rept.Without Fp,Rept ML20249A5451998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Braidwood Generating Station Units 1 & 2 ML20247F7711998-05-0808 May 1998 Special Rept:On 980403 & 980503 Seismic Monitoring Sys Was Declared Inoperable.Caused by 5-volt Power Supply & Regulator Card Failure.Imd & Sys Engineering Are Continuing to Identify & Resolve Problems So Sys Can Be Operable ML20247L7591998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Braidwood Generating Station,Units 1 & 2 ML20217K6331998-04-20020 April 1998 Safety Evaluation Accepting Methodology & Criteria Used in Generating Flaw Evaluation Charts for RPV of Braidwood IAW Section XI of ASME Code ML20216C6621998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Braidwood Generating Station,Units 1 & 2 1999-09-30
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Commonweshh Edison
/ Braidwood Nucl :r Po:cr St: tion i
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/ Braceville, Illinois 60407 I
Telephone 81$/458-2801 i p
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i' , l June 29,1990 BW/90-0670 ;
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U. S. Nuclear Regulatory Commission I Document Control Desk j Washington, D.C. 20555 1 l
Dear Str:
l L The enclosed Licensee Event Report from Braldwood Generating ,
t Station is being transmitted to you in accordance with the requirements of 1 10CFR50.73(a)(2)(ll) which requires a 30-day written report. 1 This report is number 90-009-00: Docket No. 50-457. <
l Very truly yours, ]
[
. R. E. Querto 1 Station Manager l Braldwood Nuclear Station REQ /JDW/sjs ;
l (7126z). i
Enclosure:
Licensee Event Report No. 90-009-00 j i
! cc: NRC Region III Administrator NRC Resident Inspector [
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Hain $teamilne Isolation Valve Inoperable due to a Falled Four Way Hydrevilt Valve Jxt01 htt_i$L _ LLRJumi'tt 16L _ itter1Ditll)._ QA!!tLLeillitittl0xchtlLiti Sequential Revision Month Day Year .JatiblyjjattL 39.d tL1!udtrl11.
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AD$1RACT (Limit to 1400 spaces, i.e. approelmately fif teen single-space typewritten lines) (16)
At 0030 on June 4,1990, with unit 2 in mode 4, during a routtre ins;mtion of the 2A tiann Steaminne Inistion -
Valve (H$ly) It was identified that the pressures for the actl e anti standh accumu1Mors were 3&QO ps' d and 4600 psig tespectively. This was below the 4800 psig required ler operability. The M!!vs are not renun- u to be crerable in mode 4 At Approximately 0910 it was identified that the tause of the low accur...nor pressore was th) "N" four way hydraullt valve. The N velve had an tolernal lost which allowed hydra 9)(c fluid to Le perted to the reservoir. An evaluation was conducted to determint, tow the valve ucu?d have pertWed in its as feund
.tondition. It was tontivded that the valve would have been Intspeble of closure trae tha ;.:tive -accumulator.
There was adequate hydraulic fluid and pressure in the standby accumulator to ens ere 0% of atrote travel in the closed direction but it covid not be assured that 100% clovvre would be echiend. At44tienally, with the hydraulic leak on the N valve the air driven hydraulic pg distharge vould have been directed back to the reservoir instead of assisting with the final $t. of valvo r.losure. Ibe cause of the event was comsonent
-follure. The four way valve and the hydraulic oli fllter for the TA fl$1V were replar.e!, Slnre replaceme.it, the 2 A H$IV has performed satisf actorily. previous correct lvt octions are not appitcable.
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l A; 'p1:.nt Conditions prior to twent j
' I Unitt Braldwood 21 tvent Date! June 4. 1990; [ vent ilme: 0030 4 - Hot $hutdown; Rx powert 0%;
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zMode RC$ (AB) Temperature / pressuret 330 DtGRits f / 350 psig ;
Dhdiptionoftvent: I J ' Th;re were no systems or components innperable at the beginning of the event which contributed to the ;
. Severity of the event.
At 0030 on June 4.1990 during a routine inspection of the 2A Main Steamilne Isolation Valve (MSIV) ($B) it was identified that the pressures for the active and standby accumulators were 3400 pilg and 4600 psig t respectively. This was below the 4000 psig required for operability. The MSIVs are not required to be j
;perable in mode 4. The valve was classified as degraded equipment as a means for tracking and restoring to i i
op; table prior to entry into a mode where operability was required. Trouble shooting activities were immediately initiated. -:
At approntmately 0910 it was identified that the cause of the low accumulator pressure was the *N" four way hydraullt valve. The N valve had an internal leak which allowed hydraulic fluid to be ported to the !
! r servoir. The System Test Engineer (Sit) was requested to evaluate how the valve would have performed in this as found condition. Based on the results of this evaluation it was concluded that the valve would have m toen incapable of closure from the active accumulatot which Indicated 3400 psig. The $ft concluded that
'th;re was adequate hydraullt fluid and pressure in the standby accumulator to ensure 95% of stroke travel in
- the cloe,ed direction, but it could not be assured that 100% closure would be achieved. Additionally, with
-the hydraulic leak on.the N valve the air driven hydraulic pump discharge would have been directed back to th) reservoir Instead of assisting with the final 5% of valve closure. .j
< this event was conservatively classified as an event found while the reactor was shut down, that, had it been found while the reactos. was in operation, would have resulted in the Nuclear power plant, including its
, . principal saf ety barrlers, being seriously degraded. The appropriate NRC notification via the CNS phone system was made at 1150 pursuant to 10CrR50.72(b)(2HI).
l
,i This eventt is being reported pursuant to 10Cf R50.73(a)(2)(li) - any event or condition that resulted in the j
tondition of the nuclear power plant. including its principal safety barriers, being seriously degraded.
C. = C:use of tvent 1he root cause of this event was component failure. The defective four way valve wns removed and placed on a tist stand. During test operations leakage was evident and traced to poor sealing tetween the metal spool piece and it's mating thlmble. This was a metal to metal seal with a ground finish. Any small imperfection
,' sr dirt buildup on the faces would cause leakage. The hydraullt fluid was analyred and Indicated a very low particulate count. This would tend to indicate that the event was isolated.
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[lftXT Energy industry Identification $ystem (L!!$) codes are identified in the text as (XX) 8
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4 D. Safety Analysis: ,
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s This event had no effect on the safety of the plant or the public. The H$!V was not required.to be operable 'n ll
[p mod') 4. The M$1Vs for the three remaining steamilnes were operable and evallable had isolation been required, Und0t the worst case of this event occurring with a Unit at power and an actu61 HSIV isolation being required
,4 ~ there would still be no effect. The analyses of the postulated accidents which require steamline isolation assuae
! , the failure of ore H!!V to close, the conclusions of the analyses' indicates that for all cases the integrity of f, structures and components required to mitlpate this accident will be maintained, no Departure from Hucleate B2414ng will occur, and that any potential rad .. logical consequences would be within the guidelines of 10 Cf R
, 100. This is enveloped in section 1$ of the Updated final Safety Analysis Report.
L t, CCrrective Actions:
The four way valve was replaced. The hydraulic oil filter for the 2A M$1V was also replaced. $1nce replacement of ti.e filter and the valve, the hydraulic system of the 2 A HSIV has performed satisfactorily.
.w-
'F1 previous Occurrences:
There was a previous occurrences of an inoperable HSIV due to a failed four way solenold valve, n
LERJE - DYRJiot 1111e
'$0-4$6/ 88-024 20-1-08-25$ Inoperable H$1V dt.e to failure of H1 Four Way Solenoid valve.
The corrective actions were implemented addressing both root and contributing causes. previous corrective actions s, iare not appilcable to this event.
- G. Component failure Date:
MeDufAclurJtL. MQEtMlli.WLt- !i[o. Fati.Rg2
' Anchor Darling Valve Co. Four Way Hydraulle valve W19595
-(Teledyne Republic). (23304-7001-2852)
- 4. . ,.
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05000457/LER-1990-004 | LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillations Occurred Due to Defective Resistor.Caused by Failure of One Dropping Resistor in Governor Unit.Resistors replaced.W/900516 Ltr | | 05000457/LER-1990-005 | LER 90-005-00:on 900426,discovered That Diesel Generator 2A Starting Air Distribution Sys Tubing Crisscrossed to Cylinders 6L & 9L.Caused by Preservice Mfg Deficiency. Custom-routed Airlines replaced.W/900524 Ltr | | 05000457/LER-1990-006 | LER 90-006-00:on 900521,containment Fuel Handling Incident Area Radiation Monitor Failed Automatic Checksource Test Due to Low Count Rate.Caused by Component Failure.Detector replaced.W/900618 Ltr | | 05000456/LER-1990-007 | LER 90-007-00:on 900601,during Removal of Ohmmeter Probe, Operator Touched Probe to Exposed Terminal Point,Resulting in Automatic Start of Auxiliary Feedwater Pump 1A.Caused by Methodology Deficiency.Probes modified.W/900628 Ltr | | 05000456/LER-1990-008 | LER 90-008-00:on 900608,reactor Trip Occurred Due to High Flux Rate Signal from Power Range Nuclear Instrumentation. Caused by Voltage Transient,Resulting from Lightning Striking Containment.Power Supply reset.W/900629 Ltr | | 05000457/LER-1990-009 | LER 90-009-00:on 900604,pressures for Active & Standby Accumulators Identified to Be Below 4,800 Psig Required for Operability.Caused by Component Failure.Four Way Valve & Hydraulic Oil Filter Used for MSIV replaced.W/900629 Ltr | | 05000457/LER-1990-010 | LER 90-010-00:on 900609,reactor Trip Occurred During Plant Startup from Low Steam Generator Water Level.Caused by Malfunctioning Bypass Feedwater Regulating Valve.Operator Training provided.W/900706 Ltr | |
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