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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000454/LER-1998-018, Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a1998-10-0909 October 1998 Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a ML20217A4471997-09-15015 September 1997 LER 97-S01-00:on 970815,unescorted Visitor Was in Protected Area.Caused by Badged Contractor Escort Who Did Not Comply W/Escort Duties.Nrc Took Control of Escort Duties 05000454/LER-1995-001, Informs That SER Issued Using LER 95-001 & Will Not Be Deemed as Ler.Lers 95-007 & 95-009 Will Not Be Used for Docket 50-454.LERs 95-003 Will Not Be Used for Docket 50-4551996-02-0505 February 1996 Informs That SER Issued Using LER 95-001 & Will Not Be Deemed as Ler.Lers 95-007 & 95-009 Will Not Be Used for Docket 50-454.LERs 95-003 Will Not Be Used for Docket 50-455 ML20076M2181994-10-27027 October 1994 Informs That LER Number 94-011 from Plant Will Not Be Used ML20076M2141994-10-27027 October 1994 Informs That LER Number 94-010 from Plant Will Not Be Used 05000455/LER-1993-005, Advises That LER 93-005 Will Not Be Used1993-10-27027 October 1993 Advises That LER 93-005 Will Not Be Used 05000454/LER-1985-1021993-08-0404 August 1993 LER 85-102-01:on 851231,determined That FW 1D Preheater Bypass Valve 1FW039D in Svc 18 Days W/O Proper Operational Testing.Caused by Procedural Deficiency.Byron Administrative Procedure Bap 330-1 Will Be revised.W/930806 Ltr 05000455/LER-1991-001, Advises That LER 91-001-00 Will Not Be Used1991-06-18018 June 1991 Advises That LER 91-001-00 Will Not Be Used 05000455/LER-1986-001, Errata to LER 86-001-00,incorporating Page 4 Inadvertently Omitted from Original LER Re Crosby Relief Valve JO-25WR1987-02-0606 February 1987 Errata to LER 86-001-00,incorporating Page 4 Inadvertently Omitted from Original LER Re Crosby Relief Valve JO-25WR ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 1998-10-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H5221999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Byron Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212B9261999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Byron Station,Units 1 & 2.With ML20210R3431999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Byron Station, Units 1 & 2.With ML20210E2251999-07-21021 July 1999 B1R09 ISI Summary Rept Spring 1999 Outage, 980309-990424 ML20209G1751999-07-0808 July 1999 SG Eddy Current Insp Rept,Cycle 9 Refueling Outage (B1R09) ML20207H7941999-06-30030 June 1999 Rev 0 to WCAP-15180, 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Comm Ed Byron Nuclear Power Station,Unit 1 Cycle 9 Startup Rept ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20202F6181998-12-31031 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20199E6371998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Byron Station,Units 1 & 2.With ML20202F6021998-12-31031 December 1998 Cycle 9 COLR in ITS Format & W(Z) Function ML20196K6731998-12-31031 December 1998 10CFR50.59 Summary Rept for 1998 ML20207H7731998-11-30030 November 1998 Rev 0 to WCAP-15125, Evaluation of Pressurized Thermal Shock for Byron,Unit 1 ML20207H8011998-11-30030 November 1998 Rev 0 to WCAP-15124, Byron Unit 1 Heatup & Cooldown Limit Curves for Normal Operation ML20198D1501998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195F8321998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Byron Nuclear Power Station,Units 1 & 2.With 05000454/LER-1998-018, Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a1998-10-0909 October 1998 Corrected LER 98-018-00:on 980912,inoperable Unit 1 DG Was Noted.Caused by Low Lube Oil Pressure Condition.Immediately Entered Into Lcoar for AC Sources TS 3.8.1.1,Action a ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154L5501998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20197C9051998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Byron Nuclear Power Station,Units 1 & 2.With ML20151Z9651998-08-31031 August 1998 Revised MOR for Aug 1998 for Byron Nuclear Power Station. Rept Now Includes Page 9 Which Was Omitted from Previously Issued Rept ML20238F6551998-08-28028 August 1998 SE Authorizing Licensee Request for Relief NR-20,Rev 1 & NR-25,Rev 0 Re Relief from Examination Requirement of Applicable ASME BPV Code,Section XI for First ISI Interval Exams ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B3361998-08-14014 August 1998 B2R07 ISI Summary Rept,Spring 1998 Outage, 961005-980518 ML20237B4841998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Byron Nuclear Power Station Units 1 & 2 1999-09-30
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LER-2085-102, |
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4542085102R00 - NRC Website |
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____ _____--
N CCmm:nw;;lth Edison 2
. Byron Nuclear Station
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O '- 4450 North German Church Road Byron, Illinois 61010 August 6, 1993 LTR: BYRON 93-0396 FILE: 3.03.0800 (1.10.0101)
U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
Dear Sir:
The Enclosed Supplemental Licensee Event Report from Byron Generating Station is being transmitted to you in accordance with the requirements of 10CFR50.73 (a) (2) (i) .
This report is number 85-102; Docket No. 50-454.
Sincerely, ft ,
/z
/ _-
G.K. Schwartz Station Manager Byron Nuclear Power Station GYS/DSK/ng
Enclosure:
Licensee Event Report No.85-102 Supplement 1 cc: J. Martfn, NRC Region III Administrator NRC Senior Resident Inspector INPO Record Center CECO Distribution List 1G0005 (9997R',WPfl072693 5)
T 9308170260 0804 PDR ADDCK 000454 8 S PDR @
LER Number 454:85-102-01 Title of Event: Missed ISI Surveillance due to Outace Procedure Deficiency Occurred: 12/31/85/ 114fL Date Time 1
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Acceptance by Station Review:
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1 Am / YbfA3 b.I /) $
OE Date TSS fate-i k j9/21/E2 l RAS Date OTHER Date
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Approved by: ///f / f l statioriha e Ddte/ ,
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i l- 19997Rin?R072693-1)
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LICENSEE EVENT REPORT (LER) l f ACluTT NAME DOCKET NUMBER PAGE l BYRON NUCLEAR POWER STAT 10N. Unit 1 0l5l0l0l0l4l5l4 1l0Fl0l3 TITLE i MISSED ISI SURVELLLANCE DUE TO DUTAGE PROCEDURE DEFICIENCY EVENT CATE LER NUMBER REPORT DATE OTHER F ACluTIES INVOLVED MONTH CAY YEAR YE AR 'SEC NUMBER REV!SION MONTH DAY YEAR f ACluTT NAMES DOCKET NUMBER (S) 4 NONE Ol5l0l0l0l l l 1l2 3l1 9 IS Bl5 -
1l0l2 -
Ol1 0lB 0l4 9l3 0l5l0l0l0l l l f THis REPORT IS SUBM:TTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (CHECK ONE OR MORE OF THE FOLLOWING)
DPERATING MODE j 73.71M 1 20.402[t) 20.405tel 50.71sX2Xiv) 20.409sXIXD 50.36(cM1) 50.73aX2iM 73.71tc)
POWER LEVEE CTHER (Specify m Abstract below Dl9l2 20.40ksX1Kii) 50.38tcX21 50.73sM2Nviil 20 *05te1Xia X 50.73sX2XD 50.73eX2XvsXA) 20.405fsW1Hnel 50.73aX2Xi) 50.73sX2xviiXBI 20.40kaN1xvi 50.73!aX2Xsil 50.73aK2Xx)
LICENSEE CONTACT FOR THIS LER NAME TELEPHONE NUMBER ;
ARE A CODE G. FR ANTZ, 0PER ATING DEPARTMENT EXT. 2992 8l1l5 2l3l4l~l5l4l4l1 COMPLETE ONE UNE FOR E ACH COMPONENT FAfLURE DESCR$ED IN TH!S REPORT CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER p PR S l
l 1 I I I I I I III II I I i1 1 I I I I I I I i1 I SUPPLEMENTAL REPORT EXPECTED EXPECTED MONTH CAT YEAR
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SU5M SSION I
] YES. Of yes. complete EXPECTED SUBM:SSION DATEl M NO DATE l { l ABSTR ACT (Lamt is 1400 spaces, is, appromenately fifteen smeltspace typewnften imes).
While in Mode 1 at 92% power, the System Engineer was asked to stroke time the 1D Feeduater Preheater Bypass Valve,1FWO39D, a containment isolation valve, following maintenance performed during a recent outage.
It was determined that the valve had been in service for 18 days, following the outage, without proper testing to l declare it operable. The appropriate Technical Specification Action Staternent was entered, power was reduced to 80% and the valve was successfully stroke timed. Because of the successful stroke time and back-up !
containment isolation throughout the 18 days, plant and public safety was never in jeopardy. A procedural i deficiency in the computerized outage tracking program allowed this testing requirement to go unnoticed. The procedural deficiency will be rectified.
l (9997R;WPRD72693 2)
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s LICENSEE EVENT REPORT (LER) TEXT CONTINUATION l F AtrJTY NAME DDCKET NUMBER LER NUMBER FAGE YEAR SED. WJMBER REVIS!DN
.l BYRON NUCLEAR POWER STATf0N j olSl0l0l0l4l5l4 sl5 -
1l0l2 ol1 ol2 0F ol3 f TEXT Energy industry identifzeten Srstem (DIS) cafes are adentifad m the test as ]XX]
A. PLANT CONDITIONS PRIOR TO EVENT:
MODE 1 - Power Ooeration Rx Power 92% RCS (AB] Temperature / Pressure 580oF B. DESCRIPTION OF EVENT:
On December 31,1985 at 1140 CST following maintenance, the System Engineer was asked to stroke time the !
1D Feedwater Preheater Bypass Valve,1FWO39D, a containment isolation valve IJM]. Upon inspection of the I completed work package calling out this test, it was determined that the valve to be tested had ben returned to ;
service and was in operation prior to the performance of this inservice Inspection required stroke time test . The i valve was immediately declared inoperable and the appropriate Tech 1ical Specification Actio.n Statement was I entered. A load reduction to 80% power was made where the vaWe was sucesssfully stroked and then returned i I
to service.
C. CAUSE OF EVENT: i The root cause of this incident was found to be a deficiency in the previous outage out of service program.
Throughout the outage, the Feedwater System ISJ) was taken out of service under a " blanket" out of service, i.e.
every component in the system was declared out of service. With the whole system out of service, work could be i done freely without additional out of services being processed. During the outage only work on the compt terized I outage list was to be performed under the blanket out of service. The computerized system was to track work to i be performed and testing required prior to unit start-up. This valve was not on the outage list. Its affect on mode I
change went undetected. There was no program in place to explicitly track Technical Specification / Mode change ,
required work if it did not appear on the outage list but was under the blanket out of service.
l D. SAFETY ANALYSIS: ,
l j The work was performed on this Borg-Wamer manufactured valve on December 7,1985. It was not properly )
tested and returned to service until December 31,1985. The applicable mode for which this valve must be '
operable was entered on December 13th. During the 18 days that this valve was in service, yet not tested, the Feedwater Regulating Valves and an inline check valve would have been provided Containment Isolation if it had j been required. The successful passing of the stroke time test on December 31st did indicate, however, that the i Preheater Bypass Valve would have been provided containment isolation even though it had not been previously !
tested. Because of the back-up isolation and the successful testing of the valve, it can be determined that at no point in time was plant or public safety jeopardized.
1 E. CORRECTIVE ACTIONS:
The corrective action to be taken to prevent reoccurrence will involve incorporation of all outage work in to the j computerized outage tracking program. A revision to Byron Administrative Procedure BAP 330-1, " Station Equipment Out-of-Service Procedure", will be processed to ensure that under the blanket out of service, no work ,
i can be performed on a safety-related piece of equipment unless the NWR number appears on the Out of Service l Form. The out of service may be used to track operability of the piece of safety-related equipment to prevent i declaring the equipment operable until all work is completed including all necessary testing.
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(9997R;WPR072693-3)
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- LICENSEE EVENT REPORT (LEll) TEXT CONTINUATION I
F ACIUTY NAME DOCKET NUMBER LER NUMBER FAGE TEAR SE(L NUMBER -REVISIDN BYRON NUCLEAR PDWER ETATION 0l5l0l0l0l4lEl4 8l5 1l0l2 l Dl1 0l3 0F 0l3 TEXT Ene sy industry identifcaten Sr:1em (Elfsi codes are identifed m the text s IXXI Justification for the change:
1 1). All outage related NWR's are now tracked by P-2, a computerized outage tracking program. Each NWR receives a three digit ccde that determines the mode in which the equipment is required to be operable. The outage coordinators track the status of these NWR's by use of a pre-sorted print-out listing all NWR's required for each mode.
2). Prior to each mode change, a Byron On-Site Review (BOSR) is held, at which time, all NWR's are reviewed for applicability to the assoc 4ted mode change. Any work not completed or not completely tested prior to the mode change is noied on the BOSR which is provided to the Shift Engineer prior to the mode change for review.
3). The QA Manual now allows out of services to be clear 3d prior to testing and approval for operation as long as the " Work Completed" section is signed. This is not often done with safety-related equipment, but the option does exist.
This event has never happened before at Byron Station. This report is in compliance with 10CFR50.73(a)(2)(i)(b).
This report will become required reading the Operating and Maintenance Department personnel.
F. PREVIOUS OCCURRENCES:
LER NUMBER TITLE NONE 1
G. COMPONENT FAILURE DATA:
MANUFACTURER NOMENCLATURE MODEL NUMBER MFG PART NUMBER NONE l
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l (9997R.WPR072E934:
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05000454/LER-1985-102 | LER 85-102-01:on 851231,determined That FW 1D Preheater Bypass Valve 1FW039D in Svc 18 Days W/O Proper Operational Testing.Caused by Procedural Deficiency.Byron Administrative Procedure Bap 330-1 Will Be revised.W/930806 Ltr | |
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