05000445/FIN-2011004-03
From kanterella
Jump to navigation
Jump to search
Finding | |
|---|---|
| Title | Inadequate Supervision Causes Inadvertent Engineered Safety Features Actuation |
| Description | The inspectors reviewed a self-revealing noncited violation of Technical Specification 5.4.1.a for the failure of the unit supervisor to adequately maintain responsibility for the operation of Unit 1 and the supervision of operations personnel during preparations for a reactor startup. As a result, when an operator performed a trip of the main feedwater pump, the motor driven auxiliary feedwater pumps received an engineered safety features actuation and initiated full auxiliary feedwater flow to the steam generators. Operators throttled feedwater flow to prevent overfill of the steam generators and excessive cool down of the reactor coolant system. The licensee entered the finding into the corrective action program as Condition Report CR-2011-008052. The failure of the unit supervisor to maintain responsibility for the operation of Unit 1 and the supervision of operations personnel during preparations for a reactor startup was a performance deficiency and resulted in an unplanned engineered safety features actuation of the auxiliary feedwater pumps. The finding was more than minor because it was associated with the configuration control attribute of the initiating events cornerstone and affected the cornerstone objective, in that, it increased the likelihood of those events that upset plant stability. Using NRC Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, the finding was determined to be of very low safety significance because the finding did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating equipment would not be available. This finding has a human performance crosscutting aspect associated with decision making, in that, the unit supervisor failed to communicate the decision to install the auxiliary feedwater pump auto start fuses to all control room personnel |
| Site: | Comanche Peak |
|---|---|
| Report | IR 05000445/2011004 Section 1R20 |
| Date counted | Sep 30, 2011 (2011Q3) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71111.2 |
| Inspectors (proximate) | L Carson W Walker M Young M Bloodgood J Kramer S Hedger J Watkins M Williams |
| CCA | H.10, Bases for Decisions |
| INPO aspect | CO.2 |
| ' | |
Finding - Comanche Peak - IR 05000445/2011004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Comanche Peak) @ 2011Q3
Self-Identified List (Comanche Peak)
| ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||