05000414/LER-2001-003

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LER-2001-003, Electrical fault in reactor coolant pump motor stator causes automatic reactor trip, autostart of emergency diesel generator, and autostart of auxiliary feedwater.
Catawba Nuclear Station, Unit 2
Event date: 12-07-2001
Report date: 02-04-2002
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
4142001003R00 - NRC Website

BACKGROUND

Catawba Nuclear Station Unit 2 is a four loop Westinghouse pressurized water reactor [EIIS: RCT]. Each reactor coolant pump (RCP) motor [EIIS:

MO] is provided power from the 6900VAC normal auxiliary power system [EIIS: EA]. The 6900VAC normal auxiliary power system distributes power to unit auxiliaries required during normal operation and serves as the preferred power supply to the 4160VAC essential auxiliary power system [EIIS: EB] through a 6900/4160VAC transformer [EIIS: XFMR].

The 6900VAC system consists of four switchgear assemblies [EIIS:

SWGR] of the split-bus design. One section of each switchgear assembly (cubicles 1-6) supplies one RCP motor and serves as part of the preferred power supply to the 4160VAC essential auxiliary power system as indicated below:

6900VAC switchgear 2TA - 6900VAC switchgear 2TB - 6900VAC switchgear 2TC - 6900VAC switchgear 2TD - Normal source for 4160VAC switchgear 2ETA Alternate source for 4160VAC switchgear 2ETB Alternate source for 4160VAC switchgear 2ETA Normal source for 4160VAC switchgear 2ETB The other section of each switchgear assembly (cubicles 8-16) supplies balance-of-plant loads such as the condenser circulating water pump motors.

The 6900VAC feeder breakers to RCP motors and 4160VAC essential switchgear have protective relying for differential current [EIIS:

61] and ground fault [EIIS: 64].

Each of the four 6900VAC switchgear assemblies supplies power to its associated RCP motor via an additional separate and independent 6900VAC switchgear assembly. These additional switchgear assemblies are provided for RCP motor electrical penetration [EIIS:

PEN] protection and are located in the auxiliary building.

Each train of the 4160VAC essential auxiliary power system is also provided with a separate and independent emergency diesel generator (EDG) [EIIS: DG] to supply the class lE loads required to safely shutdown the unit following a design basis accident.

Each of the redundant 4160VAC essential buses is provided with undervoltage protection to monitor bus voltage with three under voltage relays [EIIS: 27] which are utilized in a two-out-of-three logic scheme. Upon a loss of voltage on the 4160VAC essential bus, this relaying actuates the load sequencer [EIIS: EK]. The sequencer starts the associated EDG, load sheds the essential bus, powers the bus from the EDG, and sequences on the required loads.

Plant conditions immediately prior to this event were: reactor power 100% in MODE 1, turbine load 1230 Mwe, reactor coolant system [EIIS: AB] Tavg 587.2 degrees F., reactor coolant system pressure 2231 psig, reactor coolant system boron concentration 1196 ppm, and cycle burnup 45.0 effective full power days. There were no systems, structures, or components out of service at the time of this event that contributed to the event.

This event is being reported under 10CFR50.73(a)(2)(iv)(A) (any event or operation that resulted in manual or automatic actuation of a safety system).

EVENT DESCRIPTION

(Dates and times are approximate) 12/7/2001 2350 � A phase to ground fault occurred in the stator of the 2D RCP motor.

Protective relaying automatically opened the 6900VAC breaker supplying power to the 2D RCP motor.

Protective relaying automatically opened the 6900VAC breaker supplying power to the 2ETB 4160VAC essential bus.

A unit 2 reactor trip occurred because of low RCS flow in the 2D loop with power >P8 (49%).

Operations entered procedure EP/2/A/5000/E-0 "Reactor Trip or Safety Injection".

The 2B EDG automatically started and supplied power to the 2ETB 4160VAC essential bus. All loads required for this situation were automatically sequenced on as designed. This included the 2B motor-driven auxiliary feedwater pump and the turbine driven auxiliary feedwater pump. Operations entered procedure AP/2/A/5000/007 "Loss of Normal Power".

The 2A motor-driven auxiliary feedwater pump automatically started because of lo lo level in the 2D steam generator. The lo lo level was expected as a result of shrink caused by reverse flow in that loop when the RCP tripped.

An automatic main feedwater isolation occurred as a result of the reactor trip and lo T-ave as designed.

12/8/2001 0050 � Stable no-load conditions were established with the unit in MODE 3.

12/8/2001 0152 � Required 4-hour notification to the NRC was made.

12/8/2001 0200 � A plant recovery team was formed to investigate the reactor trip.

12/8/2001 0252 � Essential bus 2ETB was realigned to an offsite power supply and the 2B EDG was shut down.

12/8/2001 2151 � Electrical testing was completed on the 2D RCP motor and it was determined that the ground was internal to the motor on the Z phase. The decision was made to replace the motor with the available spare.

12/9/2001 0256 � A cooldown of Unit 2 to MODE 5 was commenced to allow replacement of the RCP motor.

12/19/2001 Testing and calibration of protective relaying associated with the two 6900VAC feeder breakers that tripped was completed. An evaluation of the results concluded that all relaying functioned as designed and within established setpoints and allowable tolerances.

12/22/2001 0856 � Unit 2 was placed on line.

12/23/2001 1034 � Unit 2 returned to 100% power.

CAUSAL FACTORS

To determine the source of the ground fault, testing was performed on the circuit from the 6900VAC RCP motor breaker through the RCP motor stator. Testing performed included phase-to-phase and phase-to ground measurements of the cables, electrical penetration, and the stator windings of 2D RCP motor.

Winding resistance was measured at 0.091 ohms from X-to-Y, Y-to-Z, and X-to-Z phases. This indicated that there was no open circuit between the safety breaker and the motor windings. This also confirmed that there were no high impedance connections within the circuit.

Impedance measurements at 1 kHz identified a change in Z-phase capacitance to ground.

Z-phase insulation resistance (phase-to-ground) was only 284 Kohms with an applied voltage of 1 kVDC. This is unacceptable (well below the IEEE 43 acceptance criteria) and was the source of the ground fault.

Preliminary inspection after disassembly of the motor revealed a "turn- to-turn" failure of a single coil. The damaged coil is on the line end of the stator core and appears to be the first coil in the Z-phase (T3) coil group. A possible cause of failure is a manufacturing defect of the magnet wire.

The motor was rewound by the original equipment manufacturer in 1998 and had been in service for less than 3 years. The stator is being shipped back to the original equipment manufacturer for further investigation and analysis.

The RCP motors are included in the Catawba preventive maintenance program. The motor parameters are monitored during operation and refurbished motors are periodically installed based on performance monitoring and trending. This practice is to improve system reliability and prevent unexpected failures during plant operation.

This practice has been in effect for many years.

An investigation was conducted into the cause for the trip of the 6900VAC feeder breaker that supplies power to essential switchgear 2ETB. It was determined that the breaker was tripped by the actuation of the ground fault relay. The ground fault relay operates on the principle that a balanced three-phase load current will result in zero current to the relay. Given that the RCP motor stator failure resulted in a large fault current, it was concluded that this produced an imbalance in the 6900VAC system that exceeded the setpoint of this ground fault relaying and the relay operated as designed.

There have been two other reactor trips within the previous 36 months. One was the result of a degraded electrical connector of the turbine electrical trip solenoid valve. The other was caused by inadequate oversight of a modification to the turbine building roof. Corrective actions for these previous events would not have prevented this event. This event is not a recurring event.

CORRECTIVE ACTIONS

Subsequent:

1. The failed 2D RCP motor was replaced with a refurbished spare.

2. The testing and calibration of protective relaying associated with the two 6900VAC feeder breakers that tripped was performed.

An evaluation of the results concluded that all relaying functioned as designed and within established setpoints and allowable tolerances.

Planned:

1. Results of the inspection of the failed RCP motor stator by the vendor will be reviewed to identify any additional actions.

SAFETY ANALYSIS

The conditional core damage probability (CCDP) of this event has been evaluated using the PRA. This reactor trip was complicated by the resulting loss of power to the operating essential 4160VAC train. However, plant systems worked as designed as the EDG started and re-powered the bus. The other train of essential power was not affected. Operators restored off-site power to the bus in about 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. Based on operations simulations and plant walkdowns of the scenario, it was concluded that off-site power could have been restored in less than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> had it been required. Therefore, the CCDP for the event being evaluated is on the order of 5.4E-07.

This value is less than the accident sequence precursor threshold of 1.0E-06.

The dominant core damage sequences associated with this event would have containment safeguards systems available which included hydrogen igniters and containment air return fans. These types of sequences contribute insignificantly to the large early release frequency (LERF) which is dominated by ISLOCA and seismic initiating events. Therefore, this event is judged to have no significance with respect to LERF for Catawba.

This event was not a Safety System Functional Failure. The health and safety of the public were not affected by this event. There were no radiological events or consequences associated with this event.