05000354/LER-2004-007

From kanterella
Jump to navigation Jump to search
LER-2004-007, Technical Specification Noncompliance - Radiation Effluent Monitor On North Plant Vent
Docket Numbersequential Revmonth Day Year Year Month Day Yearnumber No.
Event date: 8-19-2004
Report date: 10-18-2004
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
3542004007R00 - NRC Website

PLANT AND SYSTEM IDENTIFICATION

General Electric — Boiling Water Reactor (BWR/4) Radiation Monitoring System (RM/—)' * Energy Industry Identification System [EDS) codes and component function identifier codes appear as {SS/CCC}

IDENTIFICATION OF OCCURRENCE

Event Date: August 19, 2004 Discovery Date: August 24, 2004

CONDITIONS PRIOR TO OCCURRENCE

Hope Creek was in Operating Condition 1 (Power Operation), at the time of discovery. No other required structures, systems or components were inoperable at the start of this event that contributed to the event.

DESCRIPTION OF OCCURRENCE

On Tuesday August 24, 2004 at 1310 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.98455e-4 months <br />, while completing a weekly sample evolution on the North Plant Vent (NPV) radiation monitor {RM) skid, it was observed that the skid was not able to pass the system integrity vacuum test.

Upon investigation it was discovered that valve 1SPV-081, a sample test connection valve, had been inadvertently left open apparently during corrective maintenance that had been performed on August 19, 2004. With this valve open, the process flow path for the skid was effectively diluted as room air was drawn into the normal process flow from the North Plant Ventilation ductwork. The physical location of the valve left open on the skid was such that the high, mid and low noble gas monitors, iodine and particulate sampler would have been affected by this oversight. Technical Specification (TS) Section 3.3.7.5 for Accident Monitoring as well as Offsite Dose Calculation Manual (ODCM) Section 3.3.7.11 would have been applicable for the condition described. The preplanned alternate method of monitoring of periodic grab sampling and analysis of the effluent release stream was not established. This is contrary to the requirements of TS 3.3.7.5 and the ODCM.

Upon discovery the condition was rectified by closing the sample test connection valve and installing the end cap. The North Plant Vent radiation monitor system was then declared operable. Though alternate sampling capability was available, it was not recognized that it was required.

During the condition review it was determined that the valve was apparently left open while performing maintenance and calibration using Hope Creek NPV radiation monitor maintenance procedure HC.IC-CC.SP-0015 (Q), Process Radiation Monitoring. The work was managed under Workorder 50061401. The maintenance procedure requires that the test valve be fully closed following maintenance or sampling. Because the sample valve was found open this is a procedure noncompliance problem and not a system component failure.

This event is being reported in accordance with 10CFR50.73 (a) (2) (i) (B), Any event or condition which was prohibited by the plant's Technical Specifications. Also requirements of the Hope Creek ODCM section 3.3.7.11 were not complied with.

The cause of this occurrence was due to lack of procedure compliance. Specifically, procedure requirements to isolate the test connection by closing the valve and capping the test connection were not performed. In addition, verification of this activity was not performed.

PREVIOUS OCCURRENCES

A review of LERs for the two prior years at Hope Creek and Salem was performed to determine if similar events had occurred. There were 3 LERs reporting inoperable conditions involving the NPV radiation monitoring system but none were similar to that which caused this event. LER 354/03-009 which reported an inoperable condition of the high range monitoring capability of the NPV radiation monitoring condition was related to a nonconforming design condition. While that event did not involve procedure noncompliance it may have been prevented had a full system retest been performed following maintenance on the system.

SAFETY CONSEQUENCES AND IMPLICATIONS

There were no safety consequences associated with this event since it has been determined that during the period of inoperability there were no unplanned or uncontrolled releases from the NPV. During the period of inoperability, inline radiation detectors that monitor potential sources of airborne radioactivity exhausted to the NPV did not detect elevated levels. Had an elevated radiological effluent release occurred from the NPV, the vent sample would have been diluted, thus reducing the assessment capability. However, potential sources of airborne radioactivity that exit by way of the NPV are equipped with inline radiation detection duct monitors. Potential design basis accident sources are monitored by the reactor building ventilation monitoring system and the Filtration, Recirculation, Ventilation System (FRVS) which were not affected by this incident.

A review of this event determined that a Safety System Functional Failure (SSFF) as defined in Nuclear Energy Institute (NEI) 99-02 has not occurred.

CORRECTIVE ACTION

Corrective actions included:

  • Immediate closure of the sample test connection;
  • A vacuum test on the sampling system skid was performed to ensure system integrity;
  • Human performance issues being addressed in accordance with policies.

COMMITMENTS

This LER contains no Commitments.