05000354/FIN-2014002-05
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Finding | |
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Title | Failure to Maintain B.5.b Equipment in a State of Readiness to Support Mitigation Strategies per 10 CFR 50.54(hh)(2) |
Description | The inspectors identified a Green NCV of 10 CFR 50.54(hh)(2), Conditions of Licenses. Specifically, PSEG failed to adequately assess the functionality of the B.5.b portable gas generator on multiple occasions and implement adequate corrective actions in response to repeated failures of the B.5.b portable gas generator. This resulted in an unrecoverable and unavailable individual mitigating strategy associated with the remote operation of safety relief valves (SRV) with reactor pressure vessel (RPV) injection for approximately two and half months while the portable gas generator was unavailable. PSEGs corrective actions include repairing the B.5.b portable gas generator and returning it to an available, standby condition as well as performing a validation of all B.5.b equipment and associated mitigating strategies. The inspectors determined the performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). The inspectors determined that this finding was of very low safety significance using NRC IMC 0609, Appendix L, B.5.b Significance Determination Process, Table 2 - Significance Characterization, dated December 24, 2009, as specified for 10 CFR 50.54(hh) findings by IMC 0609, Attachment 4, Initial Characterization of Findings, dated June 19, 2012, because the finding affected the Mitigating Systems cornerstone while the plant was at power and resulted in an unrecoverable unavailability of an individual mitigating strategy. Specifically, because the B.5.b portable gas generator was not functional for approximately 2.5 months with no compensatory actions in place, the Remote Operation of SRVs with RPV Injection mitigation strategy per Hope Creek procedure HC.OP-AM.TSC-0024, Revision 8, was determined to be unrecoverable and unavailable during this time. The inspectors noted that the reactor core isolation cooling (RCIC) system remained functional during this time period and as such the finding did not represent an unrecoverable unavailability of multiple mitigating strategies such that injection to RPV could not have occurred. The inspectors determined that the contributing cause that provided the most insight into the performance deficiency was associated with the cross-cutting aspect of Problem Identification and Resolution, Evaluation, because PSEG failed to thoroughly evaluate equipment deficiencies related to the B.5.b portable gas generator to ensure that the resolutions addressed causes and extent of conditions commensurate with the B.5.b equipments safety significance. |
Site: | Hope Creek |
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Report | IR 05000354/2014002 Section 4OA2 |
Date counted | Mar 31, 2014 (2014Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | B Reyes E Burket H Nieh J Hawkins M Orr S Ibarrola |
Violation of: | 10 CFR 50.54 |
CCA | P.2, Evaluation |
INPO aspect | PI.2 |
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Finding - Hope Creek - IR 05000354/2014002 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Hope Creek) @ 2014Q1
Self-Identified List (Hope Creek)
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