05000354/FIN-2013003-01
From kanterella
Jump to navigation
Jump to search
Finding | |
|---|---|
| Title | Inadequate Preventive Maintenance Replacement Schedule for Agastat Control Relays |
| Description | A self-revealing Green NCV of Technical Specifications (TS) 6.8.1, Procedures, was identified because PSEG failed to establish an appropriate preventive maintenance (PM) schedule for Tyco/Agastat General Purpose (GP) control relays. Specifically, the evaluation PSEG performed to revise the relay replacement periodicity from 22 years to 40 years neither adequately addressed available relay references nor all applicable failure mechanisms. As a result, high pressure coolant injection (HPCI) failed to respond to logic system actuation signals during surveillance testing on April 8, 2013. PSEGs immediate corrective actions included replacing failed relays and placing the issues in the corrective action program (CAP). Additionally, PSEG plans to revise the replacement frequency and to replace other Tyco/Agastat GP control relays of high safety significance, as identified in their extent of condition review. This finding was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure of a control relay caused the HPCI system to fail to automatically actuate during testing, and the HPCI system was unexpectedly declared inoperable. The inspectors evaluated the finding in accordance with IMC 0609, Significance Determination Process, issued June 2, 2011, and determined the finding is of very low safety significance (Green) following a detailed risk evaluation. No cross-cutting aspect was assigned to this finding because PSEG decisions made with regard to evaluating the PM replacement periodicity were made more than 3 years ago and a PM Ownership Committee has since been created to review PM change evaluations; therefore, this performance deficiency is not reflective of current plant performance. |
| Site: | Hope Creek |
|---|---|
| Report | IR 05000354/2013003 Section 4OA3 |
| Date counted | Sep 30, 2013 (2013Q3) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71153 |
| Inspectors (proximate) | R Fuhrmeister R Barkley G Dentel R Nimitz F Bower D Dodson S Ibarrola S Hammann D Lawyer G Bjorkman |
| Violation of: | Technical Specification - Procedures Technical Specification |
| INPO aspect | |
| ' | |
Finding - Hope Creek - IR 05000354/2013003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||
|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Hope Creek) @ 2013Q3
Self-Identified List (Hope Creek)
| |||||||||||||||||||||||||||||||||||||||||||||||||||||||