05000352/FIN-2012004-04
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Finding | |
|---|---|
| Title | Failure to Establish and Perform Adequate Preventive Maintenance on 480VAC Load Center Power Transformers |
| Description | A self-revealing NCV of Limerick Technical Specification (TS) 6.8, Procedures and Programs, was identified for failure to establish and perform adequate preventive maintenance (PM) activities to routinely inspect the 480 volt-alternating current (VAC) load center power transformers. As a result, Limerick experienced a transformer related fault that could have been prevented by PM which resulted in a manual reactor scram of Unit 1 on July 18, 2012. Corrective actions implemented by Limerick as a result of this transformer failure included advancing the thermography window installation schedule to align with each transformers feeder breaker trip test calibration. Limerick also performed thermography inspections on the other load center transformers and developed corrective actions (Issue Report (IR) 1355930 and 1390033) to reinstitute the clean and inspect PM on all load center transformers at an increased frequency of 8 years vice 20 years. The finding was determined to be more than minor because it was associated with the Initiating Events cornerstone and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The finding was determined to be of very low safety significance because the finding caused a reactor trip but not the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. This finding was determined to have a cross-cutting aspect because, although the performance deficiency occurred more than three years ago, the performance characteristic associated with ineffective PM implementation continues to exist within Limericks PM program and is indicative of present performance. The cross-cutting aspect associated with this performance deficiency is in the Resources component of the Human Performance area because the licensee did not ensure that personnel, equipment, procedures and other resources were adequate to assure long term plant safety through maintenance and the minimization of long-standing equipment issues |
| Site: | Limerick |
|---|---|
| Report | IR 05000352/2012004 Section 4OA3 |
| Date counted | Sep 30, 2012 (2012Q3) |
| Type: | NCV: Green |
| cornerstone | Initiating Events |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71153 |
| Inspectors (proximate) | E Burket E Dipaolo J Hawkins J Laughlin P Krohn R Nimitz |
| CCA | H.6, Design Margins |
| INPO aspect | WP.2 |
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Finding - Limerick - IR 05000352/2012004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Limerick) @ 2012Q3
Self-Identified List (Limerick)
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