05000348/FIN-2011010-03
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Finding | |
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| Title | Failure to Provide Adequate Procedural Guidance for Controlling Steam Generator and Pressurizer Level During Loss of Air Events |
| Description | The team identified a non-cited violation (NCV) of Technical Specification (TS) 5.4, Procedures, for the licensees failure to provide adequate procedural guidance for controlling steam generator (SG) and pressurizer level during loss of instrument air events and Chemical and Volume Control System (CVCS) malfunctions. Specifically, the licensee failed to evaluate the capability of motor operated valves (MOVs) to be cycled as directed by abnormal operating procedures (AOPs). The licensee entered these issues into their Corrective Action Program (CAP) as Condition Reports (CRs) 355230, 355672 and 355695; performed DOEJ FRSNC326893-E001, Evaluate Cycling of Q1E21MOV8107, Q1E21MOV8107, and Q1E21MOV3764A through F; and implemented a standing order (S-2011-12) that restricted the cycling the of the MOVs until the procedures were revised. The failure to provide adequate procedural guidance for controlling SG and pressurizer level during loss of air events and CVCS malfunctions was a performance deficiency. The performance deficiency was more that minor because it was associated with the mitigating systems cornerstone attribute of equipment performance and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee directed the cycling of MOVs in AOPs without performing evaluations to provide assurance that the components would not fail as a result of the cycling operations and lead to a condition of inadequate SG and pressurizer level control. In accordance with NRC IMC 0609.04, Initial Screening and Characterization of Findings, the team used the mitigating systems column to perform a Phase 1 Significance Determination Process (SDP) screening and determined the finding to be of very low safety significance (Green) because it was not a design issue resulting in loss of function, did not represent an actual loss of a system safety function, did not result in exceeding a Technical Specification (TS) allowed outage time, and did not affect external event mitigation. A cross-cutting aspect was not identified because the finding did not represent current performance. |
| Site: | Farley |
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| Report | IR 05000348/2011010 Section 1R21 |
| Date counted | Dec 31, 2011 (2011Q4) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71111.21 |
| Inspectors (proximate) | D Jones M Shlyamberg S Sandal R Nease J Eargle P Wagner |
| INPO aspect | |
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Finding - Farley - IR 05000348/2011010 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Farley) @ 2011Q4
Self-Identified List (Farley)
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