05000341/LER-1998-001, :on 980201,automatic Reactor Scram Occurred Due to Main Turbine Trip.Caused by Protective Relay Failure in 345 Kv Switchyard.Circuit Card Was Installed in 50BF Relay for CM Breaker in Jan 1997

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:on 980201,automatic Reactor Scram Occurred Due to Main Turbine Trip.Caused by Protective Relay Failure in 345 Kv Switchyard.Circuit Card Was Installed in 50BF Relay for CM Breaker in Jan 1997
ML20217Q050
Person / Time
Site: Fermi 
Issue date: 03/03/1998
From: Gipson D, Harsley K
DETROIT EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
CON-NRC-98-0020, CON-NRC-98-20 LER-98-001, LER-98-1, NUDOCS 9803110334
Download: ML20217Q050 (7)


LER-1998-001, on 980201,automatic Reactor Scram Occurred Due to Main Turbine Trip.Caused by Protective Relay Failure in 345 Kv Switchyard.Circuit Card Was Installed in 50BF Relay for CM Breaker in Jan 1997
Event date:
Report date:
3411998001R00 - NRC Website

text

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Douglis R. Gipson Senior Vice President, Nuclear Generation Ferm! 2 6400 North Dixie liwy, Newport, Michigan 48166 Tel: 313.586.5201 Fat 313.586A172 Detroit Edison 10CFR50.73 3

March 3,1998

,JRC-98-0020 U. S. Nuclear Regulatory Commission Atta: Document Control Desk Washington, D. C. 20555

References:

Fermi 2 NRC Docket No. 50-341 NRC License No. NPF-43

Subject:

Licensee Event Report (LER) No.98-001 1

Pursuant to 10CFR50.73, Detroit Edison is submitting the enclosed LER No. 9841.

This LER addresses an automatic reactor scram due to a main turbine trip caused by protective relay failure in the 345 kV switchyard.

1 The following commitment is being made in this letter:

A long-term action plan will be developed by May 1,1998 for the 345 kV switchyard that will provide assurance that configuration is maintained on the 345 kV switchyard and relaying house equipment.

Ifyou have any questions, please contact Kimberly Harsley at (734) 586-1255.

Sincerely,

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A. B. Beach i

B. L. Burgess G. A. Harris A. J. Kugler M. V. Yudasz, Jr.

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Wayne County Emergency Management Division 9003110334 980303 PDR ADOCK 05000341 8

PDR A DTE Energy Company

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Automatic Reactor Scram due to Main Turbine Trip FVENT DATE M) i ER NUMBER (6)

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ABSTRACT (16)

On February 1,1998, the plant experienced a Reactor Protection System (RPS) actuation due to a Turbine i

Control Valve Fast Closure and the reactor scrammed at 0918 hours0.0106 days <br />0.255 hours <br />0.00152 weeks <br />3.49299e-4 months <br />. The Turbine Control Valve Fast Closure was initiated when generator output breakers CM and CF opened resulting in a turbine load reject. The turbine load reject was initiated when the outside rounds Nuclear Power Plant Operator (NPPO) actuated the test reset switch for the Brownstown 3 "B" relaying panel in the 345 kV relay house. In addition to circuit brea).ers CM and CF, circuit breaker CT opened and Brownstown - Fermi 3 Line de-energized. The 345 kV buses emained energized through the DM and DF breakers, the redundant off-site power source. All control rods fully inserted into the core. Reactor Pressure Vessel (RPV) level decreased below the Level 3 setpoint resulting in a Nuclear Steam Supply Shutoff System (NSSSS) Group 4,13, and 15 isolation signals.

Two degraded conditions existed on the Brownstown 3 "B" relay scheme. A circuit card was installed in the 50BF relay for the CM breaker in January 1997. The card that was installed in the relay had a latching resistor that should have been removed prior to installation. Secondly, an intemal failure of the 95 (SRU) relay created and passed a voltage spike of sufficient amplitude and duration to pick up the breaker failure relay.

Corrective actions included replacement of the 50BF (SBFU) relay to eliminate the undesirable latching circuit and replacement of the 95 (SRU) relay to eliminate the stray high output signal.

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Initial Plant Condition:

OperationCondition:

1 (Power Operation)

ReactorPower:

96 Percent ReactorPressure:

1022 psig ReactorTemperature:

540 degrees Fahrenheit Descriptionof the Event On February 1,1998, at 0918 hours0.0106 days <br />0.255 hours <br />0.00152 weeks <br />3.49299e-4 months <br />, the outside ro' aids Nuclear Power Plant Operator (NPPO) actuated the test reset switch for the Brownstown 3 "B" relaying panel in the 345 kV relay house. The test is part of a routine alarm functional test that is performed daily by operations. The plant experienced a reactor scram as a result of RPS actuation due to a Turbine Contn el Valve Fast Closure that was initiated when generator output circuit breakers CM [BKR] and CF [BKR] opened resulting in a turbine load reject. In addition to breakers CM [BKR] and CF [BKR), breaker CT [BKR] opened and Brownstown 3 line de-energized.The 345 kV buses remained energized through the DM and DF breakers,the redundant off-site power source. All control rods fully inserted into the core. The tarbine bypass valves opened in response to the turbine trip and controlled reactor pressure. Reactor pressure peaked at 1080 psig and no Safety Relief Valves (SRV) lifted during the transient.

Reactor Pressure Vessel (RPV) level decreased to 119 inches. Post scram feedwaterlogic initiated and reactor feedpump speed decreased to approximately2100 rpm. The Startup Level Control Valve (SULCV) shifted to automatic. The General Electric Transient Analysis Recoroer System (GETARS) data showed the SULCV received an open signal and fully opened. RPV level did not increase until the South reactor feedpump was placed in manual and speed was increased by the operators in accordance with Abnormal Operating Procedure (AOP) 20.000.21. The SULCV modulated normally in response to the level increase and operators continued to maintain RPV levelwith the SULCV.

A reactor vessel law water level condition (Level 3) occurred as part of the event resulting in Nuclear Steam Supply Shutoff System (NSSSS) Group 4 (Residual Heat Removal Shutdown Cooling),13 (Drywell Sump),

and 15 (Traversing in-core probe system) isolation signals. Group 13 valves were the only valves open at the time of the scram and the valves isolated as required.

The reactor scram was reset at 0939 on February 1,1998, and a four-hour notification of the reactor protection system actuation was made to the NRC pursuant to 10CFR50.72(b)(2)(ii)at 1230 hours0.0142 days <br />0.342 hours <br />0.00203 weeks <br />4.68015e-4 months <br />.

Plant response and resultant reactor trip was normal with the exception of turbine response to the load rejection. An automatic turbine trip is initiated by the opening of the output breakers which is expected to limit turbine generatoracceleration to approximately 110 percent speed. Actual speed reached was 124 percent. This overspeed is attributed to abnormally slow closure of #2 Lcw Pressure Stop Valve (LPSV)

[ISV) and #2 Low Pressure Intercept Valve (LPIV) [FCV].

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Cause of the Event

The scram was initiated by the breaker failure relay 50BF (SBFU) [RLY]. A breaker failure circuit card was installed in the relay for the CM breaker. The breaker failure circuit card had a resistorin the circuit which caused the relay to be susceptible to actuation when exposed to a voltage spike of adequate duration. The card was installed in the CM breaker 50BF relay in January 1997.

Two degraded conditions existed on the Brownstown 3 "B" relay scheme. The first was the breaker failure relay 50BF, and the second was an internal failure of the 95 (SRU) [RLY] relay. Investigative testing revealed that when the test reset switch is operated, the alarm relay coils within the Type SRU [RLY] output relay is first energized,then de-energized,resultingin an inductive" kick" or surge voltage. The test reset switch produced a periodic transient voltage of sufficient magnitude and duration to generate an output on the breaker failure initiate board of the Type SRU [RLY] relay. This output by itself would not cause a breaker trip. The breaker failure initiate output of the Type SRU [R.LY] relay satisfies one of two required inputs to the Type SBFU [RLY] breaker failure relay for position CM [BKR]. The other required input is a current level detector that picks up at 1200 primary amps, which was satisfied due to machine and line loading at the time. These two inputs would normally need to be present for 5.5 cycles (approximately 92 milliseconds)to produce a trip output and pick up the breaker failure trip string. However,because a modificationhad not been made to the Type SBFU [RLY] relay, an initiate signal of approximately 8 milliseconds in duration would be sufficient to produce a trip output. Had the modification to the 50BF [RLY] relay been completed, the voltage spike would not have been of sufficient duration (greater than 92 milliseconds)to have caused the trip regardless of the 95 (SRU) [RLY] relay equipment failure; therefore, the cause of the plant scram was the unmodified breaker f;ilure relay 50BF circuit card installation.

The circuit card in the 50BF [RLY] relay for the CM [BKR] breaker should have been modified to remove the 1stching resistor prior to installation. Following the event, the circuit was visually inspected and it was verified that the installed card had not been modified as required. This card was installed in January 1997.

Maintenance activities on protective relaying equipment in the 345 kV [FK] and 120 kV [FK] switchyards are performed by Corporate Equipment Performance and Predictive Maintenance (EPPM) personnel under a Fermi work request. Fermi maintains oversight of EPPM personnel. Material control, maintenance and configuration control for relaying equipmentin the switchyards are performed by Corporate EPPM. An interim work control process has been developed that will provide assurance that configuration will be maintained on the relaying equipment until a long-term action plan is developed.

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onalysis of the Event:

The Main Turbine Generator (MTG) [TG) tripped while operating at 96 percent power as a result of the turbine load reject. An evaluation of the event to determine the cause of the overspeed was performed and it was concluded that the #2 LPIV [FCV) and #2 LPSV [ISV] did not close in the proper time to prevent the rnain turbine speed from reaching 2234 rpm (124 percent).

Under wrmal conditions,the fast valve closure mode initiates the closure of the High Pressure (HP) Turbine Stop Valves (TSVs), High Pressure Turbine Control Valves (TCVs) and the LPSV and LPIV valves. The HP valves are designed to close in less that 220 milliseconds and the Low Pressure (LP) valves in less than one second. The LP valve closure time allows the energy in the HP turbine and Moisture Separator Reheaters (MSRs) to be bled ofTin such a fashion as to not add to the overspeed of the coupled rotor train. Even with the unit valves functioning normally the rotor may accelerate between 7 and 10 percent following trip initiation.

Following the turbine load reject, turbine speed increased abnormally. Both the electrical and mechanical overspeed trip devices initiated. All of the HPCV and HPSV valves closed as designed; however, the Sequence of Events Recorder (SOER) indicated that the #2 LPIV [FCV] and #2 LPSV [ISV) did not close within their specifiedtime.

Investigationinto the Main Turbine 124 percent overspeed revealed that the #2 LPIV [FCV] and #2 LPSV [ISV] valves did not close in the proper time to prevent main turbine speed from reaching 2234 rpm. The most probable cause of the valves sluggish response is increased friction, binding, of the roller bearings. The #2 LPIV [FCV] binding of the roller bearings was most likely due to corrosion causing the valve not to function properly. S ubsequent lubrication of the roller bearings and repeated successful stroke time testing provides confidence that the #2 LPIV [FCV] will perform its intended function during a main turbine trip.

The #2 LPSV [ISV] had two problems that contributed to the valve's sluggish response, increased friction, most likely due to corrosion,of the roller bearings and the unitized actuator dump valve being out of adjustment. Lubrication of the roller bearings and adjustment to the dump valve were required to assure proper valve operation.

Additional testing of the remaining ten LP valves indicated that the #1 LPSV [ISV) had not closed in the required time. The unitized actuator dump valve was readjusted and was stroke tested with an acceptable time.

In addition to the valve stroke times being verified for each LP valve to close in ! css than one second, roller bearings were lubricated on all 12 LPIV and LPSV valves.

The investigationinto the LP valve failures concluded that exercising the valves more frequently should prevent valve binding reoccurrence. The frequency of LP valve testing was increased from quarterly to bi-weekly and LP valve performance and vendor recommendationswill be used to determine valve testing frequencies for the remainder of this cycle and future cycles.

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6 An evaluation team, which included the System Engineering Organization, Engineering Support Organization, and the turbine generatormanufacturers, General Electric and GEC - Alsthom, was assembled to evaluate the turbine event. The evahiation included an analysis of the generator rotor retaining rings to determine the stress levels at 124 percent. The calculations performed on the retaining rings concluded that the yield strength for the retaining rings was 108 ksi, which was well below the GEC designlimit of 145 ksi. A rotor train vibration profile was diagnosed before and during the turbine trip and the analysis revealed no mechanical damage to the rotor train. Even at turbine speeds from 218 to 222 percent the design strength of the LP turbine blades would not be exceeded. Based on this evaluation,it was concluded that no damage to the rotor train occurred due to the opening of the CM [BRK] and CF [BKR] breakers and the HP turbine and LP turbines and generator components were not affected by the 124 percent overspeed.

No additional abnormalities to the plant scram response were noted and Emergency Operating Procedures (EOPs) and Abnormal Operating Procedures (AOPs) were implemented with no noted problems or identified areas for proceduralimprovement.

Corrective Actions

Corrective actions included the replacement of the 50BF (SBFU) relay to eliminate the latching resistor, and replacement of the 95 (SRU) relay to eliminate the stray high output signal. Plant walk-down verification on the 345 kV r: laying equip ment that required modification prior to installation was also performed.

Components that were identified to have incorrect configurations were corrected prior to restart on February 14,1998.

The interim work control process for all work associated with the 345 kV switchyard and relay house will be conducted undct control of Fermi Maintenance Supenision with support by Corporate Energy Marketing and Distribution (EM&D), the Engineering Support Organization,and System Projects and Engineering Supenision during work planning, execution, testing, and paperwork close-out. Parts installed in these systems will have the responsible EM&D organization provide written verification of their applicability for configuration control with a review of the written verification by Fermi's Plant Support Engineerin3. Thir interim work control process will remain in effect until a long term corrective action plan is developed. A long-term action plan will be developed by May 1,1998 for the 345 kV switchyard that will provide assurance that configurationis maintained on the 345 kV switchyard and relaying house equipment.

The frequency of LP valve testing was increased from quarterly to bi-weekly and LP valve performance and vendor recommendations will be used to determine valve testing frequencies for the remainder of this cycle and future cycles.

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Additionalinformation:

l A. FailedComponents.

l Component:

  1. 2 Low Pressure Stop Valve (N3021-F0128) -

Description

IsolationValve Manufacturer:

GEC Alsthom TypeNumber:

Style 7 Component:

  1. 2 Low PressureInterceptValve (N3021-F013B)

Description

Flow ControlValve Manufacturer:

GEC Alsthom Type Number:

Style 6 1

Component:

  1. 1 Low Pressure Stop Valve (N3021-F012A) l

Description

IsolationValve Manufacturer:

GEC Alsthom.

Type Number:

Style 7 Component:

95 (SRU) Relay

Description

Trippingrelay Manufacturer:

ABB Style Number:

205C260A17 1

B. Previous LERs on SimilarProblems None