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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20217P3551999-10-22022 October 1999 LER 99-S01-00:on 990922,loaded 9mm Handgun Was Discovered on Truck Cargo Area of Vehicle Inside Protected Area.Caused by Inadequate Vehicle Search.Guidance in Procedures & Security Training to Address Multiple Vehicle Searches Was Provided 05000341/LER-1999-004, :on 990913,HPCI Sys Was Noted Inoperable.Caused by Failed HPCI Room Temp Switches.Replaced Temp Switches & HPCI Was Restored to Operable Status.With1999-10-13013 October 1999
- on 990913,HPCI Sys Was Noted Inoperable.Caused by Failed HPCI Room Temp Switches.Replaced Temp Switches & HPCI Was Restored to Operable Status.With
05000341/LER-1999-003, :on 990625,HPCI Sys Flow Controller Failed. Caused by Failure of Control Amplifier for Automatic HPCI Flow Control Loop.Replaced Control Amplifier Circuit Card. with1999-07-26026 July 1999
- on 990625,HPCI Sys Flow Controller Failed. Caused by Failure of Control Amplifier for Automatic HPCI Flow Control Loop.Replaced Control Amplifier Circuit Card. with
05000016/LER-1999-001, :on 990604,protected Area Access Was Found Unlocked.Caused by Human Error.Reinforced That Custodial Agent Issued Key Is Responsible for Ensuring That Protected Area Access Gate Is Locked1999-06-25025 June 1999
- on 990604,protected Area Access Was Found Unlocked.Caused by Human Error.Reinforced That Custodial Agent Issued Key Is Responsible for Ensuring That Protected Area Access Gate Is Locked
05000341/LER-1999-002, :on 990518,RRP Trip Resulted in Manual Reactor Scram.Caused by Previous Actions Taken to Minimize Risk for RRP Trip Were Not Effective.Preventive Maint Activity to Change RRP MG Set Brushes Has Been Revised.With1999-06-17017 June 1999
- on 990518,RRP Trip Resulted in Manual Reactor Scram.Caused by Previous Actions Taken to Minimize Risk for RRP Trip Were Not Effective.Preventive Maint Activity to Change RRP MG Set Brushes Has Been Revised.With
05000341/LER-1998-011, :on 981014,cracking in Silicone Fire Barrier Penetration Seal Occurred Due to High Temps.Caused by Inappropriate Translation of Vendor Matl Info Into Penetration Seal Design.With1998-11-13013 November 1998
- on 981014,cracking in Silicone Fire Barrier Penetration Seal Occurred Due to High Temps.Caused by Inappropriate Translation of Vendor Matl Info Into Penetration Seal Design.With
05000341/LER-1998-010, :on 981007,SRV as Found Settings Exceed TS Setpoint Tolerance Criteria.Caused by Oxide Bonding Between Pilot Valve Disc & Seat.All 15 Pilot Valve Assemblies Were Replaced.With1998-10-28028 October 1998
- on 981007,SRV as Found Settings Exceed TS Setpoint Tolerance Criteria.Caused by Oxide Bonding Between Pilot Valve Disc & Seat.All 15 Pilot Valve Assemblies Were Replaced.With
05000341/LER-1998-009, :on 980914,inadvertent Deenergization of Safety Bus 72F While Transferring from Alternate to Normal Power Resulted in ESF Actuations.Caused by Personnel Error. Operator Involved Was Counseled.With1998-10-0808 October 1998
- on 980914,inadvertent Deenergization of Safety Bus 72F While Transferring from Alternate to Normal Power Resulted in ESF Actuations.Caused by Personnel Error. Operator Involved Was Counseled.With
05000341/LER-1998-008, :on 980908,RHR/LPCI Sys Injection Line Inboard Isolation Check valve,E1100F050B,failed to Meet TS Leakage Criteria.Caused by Degraded Soft Seat.Subject Valve Was Refurbished with New Soft Seat1998-10-0808 October 1998
- on 980908,RHR/LPCI Sys Injection Line Inboard Isolation Check valve,E1100F050B,failed to Meet TS Leakage Criteria.Caused by Degraded Soft Seat.Subject Valve Was Refurbished with New Soft Seat
05000341/LER-1998-003, :on 980317,noted That Potential Drain Path to Hotwell or Condensate Return Tank Could Reduce CST Level. Caused by Inadequate Review of Dedicated Shutdown Sys.Will Continue Ongoing 10CFR50,App R Reassessment1998-04-16016 April 1998
- on 980317,noted That Potential Drain Path to Hotwell or Condensate Return Tank Could Reduce CST Level. Caused by Inadequate Review of Dedicated Shutdown Sys.Will Continue Ongoing 10CFR50,App R Reassessment
05000341/LER-1997-014, :on 971010,unsealed Electrical Penetrations Were Discovered in Auxiliary Bldg Wall Fire Rated Separation Barrier.Caused by Not Recognizing Significance of Four Inch Seismic Air Space.Hourly Fire Watch Established1998-04-0606 April 1998
- on 971010,unsealed Electrical Penetrations Were Discovered in Auxiliary Bldg Wall Fire Rated Separation Barrier.Caused by Not Recognizing Significance of Four Inch Seismic Air Space.Hourly Fire Watch Established
05000341/LER-1998-002, :on 980220,inadvertent Load Shed of ESF Bus 72E During Performance of Surveillance Test Resulting in ESF Actuations Occurred.Caused by Inadequate Procedure Rev. Power Was Restored to Affected Loads by 1344 Hrs on 9802201998-03-19019 March 1998
- on 980220,inadvertent Load Shed of ESF Bus 72E During Performance of Surveillance Test Resulting in ESF Actuations Occurred.Caused by Inadequate Procedure Rev. Power Was Restored to Affected Loads by 1344 Hrs on 980220
05000341/LER-1998-001, :on 980201,automatic Reactor Scram Occurred Due to Main Turbine Trip.Caused by Protective Relay Failure in 345 Kv Switchyard.Circuit Card Was Installed in 50BF Relay for CM Breaker in Jan 19971998-03-0303 March 1998
- on 980201,automatic Reactor Scram Occurred Due to Main Turbine Trip.Caused by Protective Relay Failure in 345 Kv Switchyard.Circuit Card Was Installed in 50BF Relay for CM Breaker in Jan 1997
05000341/LER-1997-014, :on 971010,turbine Bldg & Auxiliary Bldg Mezzanine Not Fully Meeting License Condition 2.C.9,was Discovered.Caused by Belief That Sealing Either End of Opening Met Sealing Requirements.Hourly Fire Watch Started1997-11-10010 November 1997
- on 971010,turbine Bldg & Auxiliary Bldg Mezzanine Not Fully Meeting License Condition 2.C.9,was Discovered.Caused by Belief That Sealing Either End of Opening Met Sealing Requirements.Hourly Fire Watch Started
05000341/LER-1997-013, :on 970619,HPCI Sys Isolation Valve Closed While Performing Surveillance.Caused by Apparent Spurious Closure of Relay Contact.Jumper Installed1997-07-21021 July 1997
- on 970619,HPCI Sys Isolation Valve Closed While Performing Surveillance.Caused by Apparent Spurious Closure of Relay Contact.Jumper Installed
05000341/LER-1997-010, :on 970504,HPCI Auxiliary Oil Pump Failed to Start.Caused by Failure of seal-in Contact in AOP Start Circuitry.Failed Auxiliary Contact Used for seal-in Purposes Has Been Replaced1997-06-0303 June 1997
- on 970504,HPCI Auxiliary Oil Pump Failed to Start.Caused by Failure of seal-in Contact in AOP Start Circuitry.Failed Auxiliary Contact Used for seal-in Purposes Has Been Replaced
05000341/LER-1997-016, :on 961016,ESF Actuation Occurred Due to Loss of Power to DC Bus.Caused by Inadequate Procedure.Test 2A-2 Battery Successfully Completed,Supervisors & Test Crew Counseled & Procedure Revised1997-04-29029 April 1997
- on 961016,ESF Actuation Occurred Due to Loss of Power to DC Bus.Caused by Inadequate Procedure.Test 2A-2 Battery Successfully Completed,Supervisors & Test Crew Counseled & Procedure Revised
05000341/LER-1997-006, :on 970320,response Time Testing Not in Conformance W/Ts Caused by Inadequate Review of TS During Safety Evaluation Development.Affected ECCS Actuation Instrumentation Channels Response Time Tested1997-04-21021 April 1997
- on 970320,response Time Testing Not in Conformance W/Ts Caused by Inadequate Review of TS During Safety Evaluation Development.Affected ECCS Actuation Instrumentation Channels Response Time Tested
05000341/LER-1996-020, :on 961203,loss of Shutdown Cooling Was Noted Due to ESF Actuation.Control Circuitry for Closure of Valve Investigated & All Connections Having Potential to de-energize Relay Checked1997-04-18018 April 1997
- on 961203,loss of Shutdown Cooling Was Noted Due to ESF Actuation.Control Circuitry for Closure of Valve Investigated & All Connections Having Potential to de-energize Relay Checked
05000341/LER-1997-017, :on 961025,multiple SRVs as-found Settings Were Outside of one-percent Tolerance Allowance Confirmed to Be corrosion-induced Bonding of Pilot Valve Disc & Seat.Pilots Replaced During Extended Fifth Refueling Outage1997-04-18018 April 1997
- on 961025,multiple SRVs as-found Settings Were Outside of one-percent Tolerance Allowance Confirmed to Be corrosion-induced Bonding of Pilot Valve Disc & Seat.Pilots Replaced During Extended Fifth Refueling Outage
05000341/LER-1996-024, :on 961228,automatic Reactor Scram Occurred Due to Perturbations in Reference Leg Backfill Sys While Placing Sys in Service.Procedures Revised1997-01-27027 January 1997
- on 961228,automatic Reactor Scram Occurred Due to Perturbations in Reference Leg Backfill Sys While Placing Sys in Service.Procedures Revised
05000341/LER-1996-021, :on 961204,automatic Reactor Scram on high-high Scram Discharge Volume During Shutdown Occurred. Caused by Personnel Error.Night Order Was Issued1996-12-30030 December 1996
- on 961204,automatic Reactor Scram on high-high Scram Discharge Volume During Shutdown Occurred. Caused by Personnel Error.Night Order Was Issued
05000341/LER-1996-019, :on 961119,inoperable Standby Feedwater Sys Flow Path for 10CFR50,App R Application Discovered.Caused by Inadequate Design Review of App R Dedicated Shutdown. Operating Procedures Revised1996-12-19019 December 1996
- on 961119,inoperable Standby Feedwater Sys Flow Path for 10CFR50,App R Application Discovered.Caused by Inadequate Design Review of App R Dedicated Shutdown. Operating Procedures Revised
05000341/LER-1996-016, :on 961016,ESFA Occurred Due to Loss of Power to DC Bus.Revised Surveillance Procedure & Reviewed Event in 1997 Cycle 1 Electrical Maint Requalification Training.W/1996-11-15015 November 1996
- on 961016,ESFA Occurred Due to Loss of Power to DC Bus.Revised Surveillance Procedure & Reviewed Event in 1997 Cycle 1 Electrical Maint Requalification Training.W/
05000341/LER-1996-008, :on 951213,one Megawatt Thermal Nonconservative Bias Found in Core Thermal Power Calculation.Caused by Heat Pump Seal Purge Flow Being Considered Insignificant During Original Heat Balance & Thermal Power Calculation1996-11-15015 November 1996
- on 951213,one Megawatt Thermal Nonconservative Bias Found in Core Thermal Power Calculation.Caused by Heat Pump Seal Purge Flow Being Considered Insignificant During Original Heat Balance & Thermal Power Calculation
05000341/LER-1996-012, :on 961003,engineered Safety Features Actuation of Primary Containment Isolation Valve B3100f014A Occurred. Caused by Personnel Error.Incident Was Discussed with I&C Personnel in Tailgate Meeting1996-11-0404 November 1996
- on 961003,engineered Safety Features Actuation of Primary Containment Isolation Valve B3100f014A Occurred. Caused by Personnel Error.Incident Was Discussed with I&C Personnel in Tailgate Meeting
05000341/LER-1996-014, :on 961004,Div 2 UHS cross-connect Valve de-energized.Caused by Loose Set Screw on Valve Operator Spline bushing.Cross-connect Path Established & Valves Will Also Be Modified W/Set Screw Recess1996-11-0404 November 1996
- on 961004,Div 2 UHS cross-connect Valve de-energized.Caused by Loose Set Screw on Valve Operator Spline bushing.Cross-connect Path Established & Valves Will Also Be Modified W/Set Screw Recess
05000341/LER-1996-011, :on 960928,ESF Actuation of Torus to Drywell Vacuum Breaker Occurred.Caused by Lack of Awareness on Part of Operator.Rhr Sys Operating Procedures Revised1996-10-28028 October 1996
- on 960928,ESF Actuation of Torus to Drywell Vacuum Breaker Occurred.Caused by Lack of Awareness on Part of Operator.Rhr Sys Operating Procedures Revised
05000341/LER-1996-009, :on 960526,ESF Actuation Occurred.Caused by Plant Operator Attempting to Replace Burned Out Indicating Bulb,Cracked Socket Separated Completely,Resulting in Short Circuit.Lamp Socket Wires Taped1996-06-21021 June 1996
- on 960526,ESF Actuation Occurred.Caused by Plant Operator Attempting to Replace Burned Out Indicating Bulb,Cracked Socket Separated Completely,Resulting in Short Circuit.Lamp Socket Wires Taped
05000341/LER-1996-006, :on 960324,missed ASME Section 11 Required Surveillance Insp.Caused by Inadequate Review of Change in Inservice Testing Program.Check Valve Inspected & Relief Request VR-48 Revised1996-05-28028 May 1996
- on 960324,missed ASME Section 11 Required Surveillance Insp.Caused by Inadequate Review of Change in Inservice Testing Program.Check Valve Inspected & Relief Request VR-48 Revised
05000341/LER-1996-007, :on 960419,RCIC Sys Declared Inoperable Due to Turbine Shaft Gland Leakage.Caused by Steam Leakage Past Seat of RCIC Turbine Steam Admission Valve1996-05-20020 May 1996
- on 960419,RCIC Sys Declared Inoperable Due to Turbine Shaft Gland Leakage.Caused by Steam Leakage Past Seat of RCIC Turbine Steam Admission Valve
05000341/LER-1996-005, :on 960327,EECW Sys Declared Inoperable & TS Required Shutdown Commenced Due to Design Issue.Design Mod Implemented to Provide safety-related make-up Sources for make-up Water & Nitrogen to EECW Mut1996-04-26026 April 1996
- on 960327,EECW Sys Declared Inoperable & TS Required Shutdown Commenced Due to Design Issue.Design Mod Implemented to Provide safety-related make-up Sources for make-up Water & Nitrogen to EECW Mut
05000341/LER-1996-004, :on 960310,high Particulate Levels Found in EDG 11 Fuel Oil.Caused by Draining Day Tank Into Bottom of FOST Day Before Maint Creating Turbulence Near Sampling Point. Changed Out Fuel Oil in FOST for EDG 11 W/Fresh Fuel Oil1996-04-0909 April 1996
- on 960310,high Particulate Levels Found in EDG 11 Fuel Oil.Caused by Draining Day Tank Into Bottom of FOST Day Before Maint Creating Turbulence Near Sampling Point. Changed Out Fuel Oil in FOST for EDG 11 W/Fresh Fuel Oil
05000341/LER-1996-002, :on 960207,ESFA of Torus to Drywell Vacuum Breaker Occurred Due to Personnel Error.Enhanced TRS Procedure to Improve Human Factors Aspect of Using Procedure1996-03-0707 March 1996
- on 960207,ESFA of Torus to Drywell Vacuum Breaker Occurred Due to Personnel Error.Enhanced TRS Procedure to Improve Human Factors Aspect of Using Procedure
05000341/LER-1995-003, :on 950228,unusual Event Declared & Terminated When Mode Switch Placed in Shutdown Completing Plant shut- Down in Accordance W/Tss.Caused by Gradual Draining Down of Div 2 Rwl.Performed Verification of Valves1995-03-29029 March 1995
- on 950228,unusual Event Declared & Terminated When Mode Switch Placed in Shutdown Completing Plant shut- Down in Accordance W/Tss.Caused by Gradual Draining Down of Div 2 Rwl.Performed Verification of Valves
05000341/LER-1995-002, :on 950216,RCIC Turbine Exhaust Line Vacuum Outboard Isolation Valve E51-F062 Closed Due to Personnel Error.Relay E51K63 Replaced & Surveillance Procedure 44.020.235 Reperformed1995-03-17017 March 1995
- on 950216,RCIC Turbine Exhaust Line Vacuum Outboard Isolation Valve E51-F062 Closed Due to Personnel Error.Relay E51K63 Replaced & Surveillance Procedure 44.020.235 Reperformed
05000341/LER-1994-011, :on 941123,erratic Indication Observed for Intermediate Range Monitor E During Testing of SRM C. Caused by Personnel Low Sensitivity of Significance.Screws Replaced & Tightened as Necessary1995-01-11011 January 1995
- on 941123,erratic Indication Observed for Intermediate Range Monitor E During Testing of SRM C. Caused by Personnel Low Sensitivity of Significance.Screws Replaced & Tightened as Necessary
05000341/LER-1994-010, :on 941111,unplanned Automatic Isolation of Shutdown Cooling Occurred Due to Inadequate Review Prior to Authorizing I&C Surveillance.Individuals Involved in Event Counseled1994-12-12012 December 1994
- on 941111,unplanned Automatic Isolation of Shutdown Cooling Occurred Due to Inadequate Review Prior to Authorizing I&C Surveillance.Individuals Involved in Event Counseled
05000341/LER-1994-008, :on 941108,unrecognized Entry Into TS Action Statements Occurred.Caused by Poor Communication Among Entire Shift Team.Individuals Involved Counseled on Need to Specifically Review Applicable TS1994-12-0808 December 1994
- on 941108,unrecognized Entry Into TS Action Statements Occurred.Caused by Poor Communication Among Entire Shift Team.Individuals Involved Counseled on Need to Specifically Review Applicable TS
05000341/LER-1994-007, :on 941031,control Ctr HVAC Duct Hanger Improperly Installed.Caused by Engineering Design Change Process Error.Edp 26868 Revised to Have South Structural Channel Welded to Adjacent Structural Channels1994-11-30030 November 1994
- on 941031,control Ctr HVAC Duct Hanger Improperly Installed.Caused by Engineering Design Change Process Error.Edp 26868 Revised to Have South Structural Channel Welded to Adjacent Structural Channels
05000341/LER-1994-003, :on 941020,identified Inadequate Logic Functional Tests.Caused by Procedural Deficiencies. Undervoltage Calibr & Logic Functional Tests Revised for 4160 Volt Buses 64B,65E,64C & 65F1994-11-30030 November 1994
- on 941020,identified Inadequate Logic Functional Tests.Caused by Procedural Deficiencies. Undervoltage Calibr & Logic Functional Tests Revised for 4160 Volt Buses 64B,65E,64C & 65F
05000341/LER-1994-009, :on 941110,unplanned Primary Containment Isolation of Torus Water Mgt Sys Occurred.Caused by Poor Communications & Failure to Adequately Monitor & Control Pump Out of Drywell Equipment Drain Sump1994-11-10010 November 1994
- on 941110,unplanned Primary Containment Isolation of Torus Water Mgt Sys Occurred.Caused by Poor Communications & Failure to Adequately Monitor & Control Pump Out of Drywell Equipment Drain Sump
05000341/LER-1994-006, :on 940903,discovered That SRMs & IRMs Inoperable During Core Alterations.Caused by Cable Connectors Becoming Separated Due to Stress.Procedure 82.000.04 Will Be Modified1994-10-0303 October 1994
- on 940903,discovered That SRMs & IRMs Inoperable During Core Alterations.Caused by Cable Connectors Becoming Separated Due to Stress.Procedure 82.000.04 Will Be Modified
05000341/LER-1994-005, :on 940826,power Was Interrupted to Portion of Supply Shutoff Sys Control Logic Causing Actuations of Engineered Safety Feature Sys.Caused by Procedural Weakness. Procedures Revised1994-09-26026 September 1994
- on 940826,power Was Interrupted to Portion of Supply Shutoff Sys Control Logic Causing Actuations of Engineered Safety Feature Sys.Caused by Procedural Weakness. Procedures Revised
05000341/LER-1994-004, :on 940822,discovered That Isolation Valves May Not Be Capable of Performing Their Function.Caused by Inadequate Control of Valve Actuator Settings.Controls Will Be Place to Ensure Settings Are Maintained1994-09-21021 September 1994
- on 940822,discovered That Isolation Valves May Not Be Capable of Performing Their Function.Caused by Inadequate Control of Valve Actuator Settings.Controls Will Be Place to Ensure Settings Are Maintained
05000341/LER-1994-002, :on 940714,fifteen SRV Pilot Assemblies Were Removed During Fourth Refueling Outage.Caused by SRV Setpoint Pressure Upward Drift.All Fifteen SRV Pilot Assemblies Have Been Replaced1994-08-15015 August 1994
- on 940714,fifteen SRV Pilot Assemblies Were Removed During Fourth Refueling Outage.Caused by SRV Setpoint Pressure Upward Drift.All Fifteen SRV Pilot Assemblies Have Been Replaced
05000341/LER-1993-014, :on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was Conducted1994-04-25025 April 1994
- on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was Conducted
05000341/LER-1993-015, On 931226,valve B3105-F031B, B Loop Pump Discharge Valve,Failed to Fully Close.Caused by Broken Wires in Valve Yoke.Wiring Replaced1994-04-21021 April 1994 On 931226,valve B3105-F031B, B Loop Pump Discharge Valve,Failed to Fully Close.Caused by Broken Wires in Valve Yoke.Wiring Replaced 05000341/LER-1994-001, :on 940127,loss of Div I Power Occurred Due to Weather & Breaker Failure.Power Restored to Div I Utilizing Fermi-Custer & Fermi-Luzon Lines1994-02-28028 February 1994
- on 940127,loss of Div I Power Occurred Due to Weather & Breaker Failure.Power Restored to Div I Utilizing Fermi-Custer & Fermi-Luzon Lines
05000341/LER-1993-013, :on 930917,manual Reactor Scram Occurred Due to Failure to Follow Established Work Control Practices. Administered Discipline Per Plant Policy1993-10-18018 October 1993
- on 930917,manual Reactor Scram Occurred Due to Failure to Follow Established Work Control Practices. Administered Discipline Per Plant Policy
1999-07-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N4381999-10-25025 October 1999 Safety Evaluation Supporting Amend 17 to License DPR-9 ML20217P3551999-10-22022 October 1999 LER 99-S01-00:on 990922,loaded 9mm Handgun Was Discovered on Truck Cargo Area of Vehicle Inside Protected Area.Caused by Inadequate Vehicle Search.Guidance in Procedures & Security Training to Address Multiple Vehicle Searches Was Provided ML20217M7121999-10-19019 October 1999 Safety Evaluation Supporting Amend 135 to License NPF-43 05000341/LER-1999-004, :on 990913,HPCI Sys Was Noted Inoperable.Caused by Failed HPCI Room Temp Switches.Replaced Temp Switches & HPCI Was Restored to Operable Status.With1999-10-13013 October 1999
- on 990913,HPCI Sys Was Noted Inoperable.Caused by Failed HPCI Room Temp Switches.Replaced Temp Switches & HPCI Was Restored to Operable Status.With
NRC-99-0095, Monthly Operating Rept for Sept 1999 for Fermi 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Fermi 2.With NRC-99-0067, Monthly Operating Rept for Aug 1999 for Fermi 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Fermi 2.With NRC-99-0065, Monthly Operating Rept for July 1999 for Fermi 2.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Fermi 2.With 05000341/LER-1999-003, :on 990625,HPCI Sys Flow Controller Failed. Caused by Failure of Control Amplifier for Automatic HPCI Flow Control Loop.Replaced Control Amplifier Circuit Card. with1999-07-26026 July 1999
- on 990625,HPCI Sys Flow Controller Failed. Caused by Failure of Control Amplifier for Automatic HPCI Flow Control Loop.Replaced Control Amplifier Circuit Card. with
NRC-99-0088, Detroit Edison Co Enrico Fermi Atomic Power Plant,Unit 1 Annual Rept for Period 980701-990630. with1999-06-30030 June 1999 Detroit Edison Co Enrico Fermi Atomic Power Plant,Unit 1 Annual Rept for Period 980701-990630. with NRC-99-0064, Monthly Operating Rept for June 1999 for Fermi 2.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Fermi 2.With 05000016/LER-1999-001, :on 990604,protected Area Access Was Found Unlocked.Caused by Human Error.Reinforced That Custodial Agent Issued Key Is Responsible for Ensuring That Protected Area Access Gate Is Locked1999-06-25025 June 1999
- on 990604,protected Area Access Was Found Unlocked.Caused by Human Error.Reinforced That Custodial Agent Issued Key Is Responsible for Ensuring That Protected Area Access Gate Is Locked
05000341/LER-1999-002, :on 990518,RRP Trip Resulted in Manual Reactor Scram.Caused by Previous Actions Taken to Minimize Risk for RRP Trip Were Not Effective.Preventive Maint Activity to Change RRP MG Set Brushes Has Been Revised.With1999-06-17017 June 1999
- on 990518,RRP Trip Resulted in Manual Reactor Scram.Caused by Previous Actions Taken to Minimize Risk for RRP Trip Were Not Effective.Preventive Maint Activity to Change RRP MG Set Brushes Has Been Revised.With
NRC-99-0062, Monthly Operating Rept for May 1999 for Fermi 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Fermi 2.With ML20207A8901999-05-25025 May 1999 Safety Evaluation Supporting Amend 133 to License NPF-43 ML20206J9301999-05-10010 May 1999 SER Concluding That Util Adequately Addressed Actions Requested in GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Powered-Operated Gate Valves ML20206G5081999-05-0505 May 1999 Safety Evaluation Approving Request for Relief PR-8,Rev 2 on Basis That Licensee Committed to Meet All Related Requirements of ASME OM-6 Std & PR-12 on Basis That Proposed Alternative Will Provide Acceptable Level of Safety NRC-99-0022, Monthly Operating Rept for Apr 1999 for Fermi 2.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Fermi 2.With ML20205Q7141999-04-15015 April 1999 Safety Evaluation Supporting Amend 16 to License DPR-9 ML20205P9721999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Fermi 2 ML20204E0371999-03-17017 March 1999 Safety Evaluation Accepting Licensee Request for NRC Approval of Alternative Rv Weld Exam,Per Provisions of 10CFR50.55a(a)(3)(i) & 10CFR50.55a(g)(6)(ii)(A)(5) for Plant,Unit 2 for 40-month Period ML20207F9951999-03-0303 March 1999 Safety Evaluation Supporting Amend 132 to License NPF-43 ML20204D0361999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Fermi 2 ML20203F8441999-02-0808 February 1999 Safety Evaluation Supporting Amend 130 to License NPF-43 ML20203F8651999-02-0808 February 1999 Safety Evaluation Supporting Amend 131 to License NPF-43 ML20198S3341999-01-0606 January 1999 Safety Evaluation Supporting Amend 15 to License DPR-9 NRC-99-0021, 1998 Annual Financial Rept for Detroit Edison Co. with1998-12-31031 December 1998 1998 Annual Financial Rept for Detroit Edison Co. with NRC-99-0005, Monthly Operating Rept for Dec 1998 for Fermi 2.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Fermi 2.With ML20207B7491998-12-31031 December 1998 1998 Annual Operating Rept for Fermi 2 ML20205Q9621998-12-31031 December 1998 Revised Monthly Operating Rept for Dec 1998 for Fermi 2 NRC-98-0153, Monthly Operating Rept for Nov 1998 for Fermi 2.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Fermi 2.With 05000341/LER-1998-011, :on 981014,cracking in Silicone Fire Barrier Penetration Seal Occurred Due to High Temps.Caused by Inappropriate Translation of Vendor Matl Info Into Penetration Seal Design.With1998-11-13013 November 1998
- on 981014,cracking in Silicone Fire Barrier Penetration Seal Occurred Due to High Temps.Caused by Inappropriate Translation of Vendor Matl Info Into Penetration Seal Design.With
NRC-98-0160, Monthly Operating Rept for Oct 1998 for Fermi 2.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Fermi 2.With 05000341/LER-1998-010, :on 981007,SRV as Found Settings Exceed TS Setpoint Tolerance Criteria.Caused by Oxide Bonding Between Pilot Valve Disc & Seat.All 15 Pilot Valve Assemblies Were Replaced.With1998-10-28028 October 1998
- on 981007,SRV as Found Settings Exceed TS Setpoint Tolerance Criteria.Caused by Oxide Bonding Between Pilot Valve Disc & Seat.All 15 Pilot Valve Assemblies Were Replaced.With
ML20154R2331998-10-21021 October 1998 Safety Evaluation Supporting Amend 13 to License DPR-9 ML20154L1031998-10-14014 October 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode 05000341/LER-1998-009, :on 980914,inadvertent Deenergization of Safety Bus 72F While Transferring from Alternate to Normal Power Resulted in ESF Actuations.Caused by Personnel Error. Operator Involved Was Counseled.With1998-10-0808 October 1998
- on 980914,inadvertent Deenergization of Safety Bus 72F While Transferring from Alternate to Normal Power Resulted in ESF Actuations.Caused by Personnel Error. Operator Involved Was Counseled.With
05000341/LER-1998-008, :on 980908,RHR/LPCI Sys Injection Line Inboard Isolation Check valve,E1100F050B,failed to Meet TS Leakage Criteria.Caused by Degraded Soft Seat.Subject Valve Was Refurbished with New Soft Seat1998-10-0808 October 1998
- on 980908,RHR/LPCI Sys Injection Line Inboard Isolation Check valve,E1100F050B,failed to Meet TS Leakage Criteria.Caused by Degraded Soft Seat.Subject Valve Was Refurbished with New Soft Seat
NRC-98-0139, Monthly Operating Rept for Sept 1998 for Fermi,Unit 2.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Fermi,Unit 2.With ML20154H8161998-09-30030 September 1998 Rev 0 to COLR Cycle 7 for Fermi 2 ML20153B8811998-09-18018 September 1998 Safety Evaluation Accepting Request for Relief from Certain Requirements of ASME Boiler & Pressure Vessel Code,Section Xi,For Plant,Unit 2 ML20153C4781998-09-16016 September 1998 Safety Evaluation Supporting Amend 128 to License NPF-43 ML20151X0651998-09-11011 September 1998 Safety Evaluation Re Inservice Testing Program Relief Request VR-63 for Plant NRC-98-0111, Monthly Operating Rept for Aug 1998 for Fermi 2.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Fermi 2.With ML20153B7921998-08-31031 August 1998 Rev 0 to Fermi 1 Sar ML20237E1171998-08-25025 August 1998 Safety Evaluation Accepting Licensee Relief Requests for First 10-yr Interval Inservice Insp Nondestructive Exam Program ML20237E2071998-08-25025 August 1998 Safety Evaluation Supporting Amend 126 to License NPF-43 ML20237E1751998-08-25025 August 1998 Safety Evaluation Supporting Amend 127 to License NPF-43 ML20237C5571998-08-20020 August 1998 Safety Evaluation Supporting Amend 125 to License NPF-43 ML20236X8611998-08-0505 August 1998 SER Related to Revised Feedwater Nozzle Analysis to Facility Operating License NPF-43,Enrico Fermi Nuclear Power Plant, Unit 2 ML20237D1491998-08-0404 August 1998 Safety Evaluation Supporting Amend 124 to License NPF-43 1999-09-30
[Table view] |
text
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On January 4 1988, the Average Power Range Monitor (APRM) setdown trips were found outside the Technical Spec i f ic a t io n allowances.
This was due to an inadequacy in the calibration procedure of the APRM fixed neutron flux upscale trip.
They were recalibrated upon discovery.
The APRM calibration procedure is being revised.
Additionally, it has been recognized that piscing the mode switch la the refuel position to perform required Source Range (SRMs) and Intermediate Range, Monitors (IRMe) functional cests was in technical violation of Technical Specifications 3.3.1 and 3.3.7.6.
Also not placing a Reactor Protective System trip system in the trip condition prior to 3 IRM channels per trip system having their testing completed was also a technical violation despite all control rods being fully inserted.
Performance of a full functional test requires the mode switch be in refuel since the rod block function cannot be verified with the mode switch in shutdown.
The SRMs and IRMs are not required to be operable during Operational Condition 1 so this situation becomes a problem following a plant shutdown.
A Technical Specification change will be submitted.
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Initial Plant Conditions
Operational Condition:
4 (Cold Shutdown) l Reactor Power:
0%
Reactor Pressure:
O psig Reactor Temperature:
approximately 150 degrees Fahrenheit Description of Occurrence:
On January 4, 1988 at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />, the Average Power Range Monitors (APRM) functional tests were performed.
As a result of these tests, it was determined that the APRM setdown trip was at approximately 34 percent of rated thermal power.
Technical Specification 2.2.1 Table 2.2.1-1 lists the allovable values to be less than or equal to 20 percent of rated thermal power.
Upon completing the functional tests, calibration procedures were issued to correct the setpoints.
While the APRM setdown trip is not required to be o p e r ab l e l
in Operational Condition 4 an investigation of the l
possibility that the trip was out of tolerance vb il e the plant was in Operational Conditions 2 or 3 was made.
The inve s tiga tion d e termined that the out of tolerance condition had existed since December 27, 1987.
At that point in time the plant was in Operational Condition 1.
During the scram and subsequent shutdown, the plant was in Operational Condition 3 from 1852 hours0.0214 days <br />0.514 hours <br />0.00306 weeks <br />7.04686e-4 months <br /> on December 31, 1987 till 0920 hours0.0106 days <br />0.256 hours <br />0.00152 weeks <br />3.5006e-4 months <br /> on January 1, 1988.
Since the condition of the ApRM setdown trip was not known, the action required by the Technical Specification, locking the mode switch in shutdown within one hour, and placing a trip system in the trip condition vere not taken.
The mode switch was placed in the refuel position from 2039 to 2143 on December 31, 1987.
Additionally, it has been determined actions taken in testing the Source Range Monitors ( S RM s ) and Intermediate Range Monitors (IRMs) following the December 31, 1987 scram were in technical violation of Technical Specifications 3.3.1 and 3.3.7.6.
At the time of the December 31, 1987 scram (see Licensee Event Report 87-056), the IRMs, the SRMs and the Average Power Range Monitors (APRMs) setdown trips were outside their surveillance frequency since all had expired vbile the plant was in Operational Condition 1.
These monitors are not required to be operable in Operational Condition 1.
At the time of the scram, 1852 hours0.0214 days <br />0.514 hours <br />0.00306 weeks <br />7.04686e-4 months <br />, the plant entered Operational Condition 3.
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==w.mn Since the IRHs and APRHs were outside the surveillance frequency, Specification 3.3.1 technically required a trip system be placed in the trip condition, despite all control rods being fully inserted.
This was not done.
At 2039 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.758395e-4 months <br />, the mode switch was placed in the refuel position to support the performance of surveillances.
This was in technical violation of Technical Specifications 3.3.1 and 3.3.7.6 which require the mode switch to be in the shutdown position if the required number of monitor channels are not operable.
The mode switch was returned to the shutdown position and locked at 2143 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.154115e-4 months <br />.
At 2245 hours0.026 days <br />0.624 hours <br />0.00371 weeks <br />8.542225e-4 months <br /> the functional test of SRM Channel B was performed excluding the rod block interlocks.
The rod block intetlocks cannot be tested with the mode switch in the shutdown position.
On January 1, 1988 at 0920 bours, the plant entered Operational Condition 4.
Several surveillances were performed on this day to verify the operability of SRH Channel A and the Division II 1RMs exclusive of their rod block interlocks.
On January 2, 1988 the SRM Channel C functional test was performed exclusive of the rod blocks.
The mode switch was placed in the refuel position at 0302 hours0.0035 days <br />0.0839 hours <br />4.993386e-4 weeks <br />1.14911e-4 months <br /> in order to test the rod block interlocks for the SRHs.
The mode switch was left in the refuel position until 0645 hours0.00747 days <br />0.179 hours <br />0.00107 weeks <br />2.454225e-4 months <br /> on January 3, 1988.
During this time, SRM Channel D had been verified to be fully operable.
On January 3,
1988 after the identification of possible noncompliance with the Technical Specifications, the mode switch was placed in the shutdown position at 0645 and at 0715 hours0.00828 days <br />0.199 hours <br />0.00118 weeks <br />2.720575e-4 months <br />, Reactor Protection System Channel A was placed in the tripped condition as required by Technical S pec i f ic a t io n s 3.3.1.
The functional and calibration tests for the Division I IRMs were completed exclusive of the rod block interlocks.
At 1716 hours0.0199 days <br />0.477 hours <br />0.00284 weeks <br />6.52938e-4 months <br /> the mode switch was returned to the refuel position to verify the remaining rod block interlocks.
The trip condition was reset as necessary to complete the IRH functional tests.
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Cause of Event
The out of tolerance condition of the APRM setdown trip was due to an inadequate procedure.
Because of the relationship of the fixed neutron flux upscale trip and the setdown trip, adjustment of the neutron flux upscale trip on December 27, 1987 vhile in Operational Condition 1 affected the setdown trip setpoint.
At the time the work was done, the relationship was not recognized.
The technical violation of action statements associated with SRM and IRM operability requirements oc cur r ed as a result of plant personnel attempting to perform required surveillance tests in their entirety, including rod block functions, and lack of practicality in Technical Specification Table 1.2 and Section 3.3.1.
Analysis of Event
None of these deficiencies reduced the safety of the public or the plant.
The plant successfully shut down during the time the violations of the Technical Spec ifica tions occurred.
In the event the scram had not occurred, the APRM setdown trip would have been checked as required by Technical Specification 3.3.1 after entering Operational Condition 2 or actions in compliaace with the Technical Specification would have been required.
Corrective Actions
The APRM setdown trip was adjusted to be within the Technical Specification range.
The APRM calibration procedures are being r ev is ed to verify / adjust the setdown trip when the fixed neutron flux upscale trip is adjusted.
These will be approved by March 1988.
Urgent Required Reading was issued to shift personnel on January 6, 1988 to clarify the requirement to maintain the reactor mode switch in SHUTDOWN until portions of surveillances are completed to allow required SRM and IRM functions to be declared operable upon entry into Operational Condition 3 or 4.
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,w s m4 won A Technical Specification change request is being prepared to add notes to Table 1.2, "0PERATIONAL CONDITIONS".
These notes would define when a mode switch may be moved to the refuel position for performance of surveillance tests.
This change vill be submitted by April 30, 1988.
A Technical Specification change vill also be proposed by June 30, 1988 eliminating the need to place trip systems in the trip condition during plant shutdown.
In the future, channel functional tests vill be perfomed on the SRMs and IRMs while in Operational Conditions 1 and 2, with the exception of the rod block function, which cannot be performed unless the plant is shutdown.
Procedure changes to allow this to be accomplished vill be completed by Ma.ch 31, 1988.
Previous Similar Events
In Licensee Event Report 85-062, inoperability of IRM Channels B and D was reported.
This was due to failure to complete the weekly channel functional test within the required frequency while in Cold Shutdown.
A failure to test the rod block function was described in Licensee Event Report 86-022.
This was due to inadequate procedures.
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February 2, 1988 NRC-88-0016 U.
S.
Nuclear Regulatory Commission Attention:
Document Control Desk Washington, D.C.
20555
Reference:
Fermi 2 NRC Docket No. 50-341 Facility Operating License No. NPF-43
Subject:
Licensee Event Report (LER) No. 88-001-00 Please find enclosed LER No. 88-001-00, dated February 2, 1988, for a reportable event that occurred on January 3, 1988.
A copy of this LER is also being sent to the l
Regional Administrator. USNRC Region III.
If you have any questions, please contact Patricia Anthony at (313) 586-1617.
Sincerely, f
W.
S.
Orser Vice President Nuclear Operations Enclosure NRC Forms 366, 366A cci A.
B. Davis J.
R.
Eckert l
l E.
G.
Greenaan W.
G.
Rogers J. J.
Stefano Wayne County Emergency Management Division
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05000341/LER-1988-001, :on 880103,APRM Setdown Trips Found Outside Tech Spec Allowances.Caused by Inadequate Procedure.Aprm Setdown Trip Adjusted to Be within Tech Spec Range & Calibr Procedures Being Revised |
- on 880103,APRM Setdown Trips Found Outside Tech Spec Allowances.Caused by Inadequate Procedure.Aprm Setdown Trip Adjusted to Be within Tech Spec Range & Calibr Procedures Being Revised
| | 05000341/LER-1988-005, :on 880111,reactor Pressure Exceeded 150 Psig W/O HPSI Sys or RCIC Sys in Standby Lineup.Caused by Personnel Error.Individual Disciplined,Per Company Policy & Mgt Discussed Event W/Shift Supervisors |
- on 880111,reactor Pressure Exceeded 150 Psig W/O HPSI Sys or RCIC Sys in Standby Lineup.Caused by Personnel Error.Individual Disciplined,Per Company Policy & Mgt Discussed Event W/Shift Supervisors
| | 05000341/LER-1988-006, :on 880229,unexpected Loss of RHR Shutdown Cooling Experienced After Transfer of Reactor Protection Sys B Power Supply.Appears That Operator Failed to Reset Valve Closure Logic After Transfer.Procedure Revised |
- on 880229,unexpected Loss of RHR Shutdown Cooling Experienced After Transfer of Reactor Protection Sys B Power Supply.Appears That Operator Failed to Reset Valve Closure Logic After Transfer.Procedure Revised
| | 05000341/LER-1988-007, :on 880214,deenergized Radiation Monitor Caused Control Ctr HVAC to Shift to Recirculation Mode.Caused by Improper Review of Sys Functions Prior to Performing Work. Personnel Involved Counseled on Event |
- on 880214,deenergized Radiation Monitor Caused Control Ctr HVAC to Shift to Recirculation Mode.Caused by Improper Review of Sys Functions Prior to Performing Work. Personnel Involved Counseled on Event
| | 05000341/LER-1988-008, :on 880229,determination Made During Local Leak Rate Testing That Combined Leakage Limits Exceeded.Caused by Normal Degradation of Valve Components &/Or Contaminants on Valve Seats.Valves Cleaned,Reworked & Retested |
- on 880229,determination Made During Local Leak Rate Testing That Combined Leakage Limits Exceeded.Caused by Normal Degradation of Valve Components &/Or Contaminants on Valve Seats.Valves Cleaned,Reworked & Retested
| | 05000341/LER-1988-009, :on 880311,nine Safety Relief Valves Failed Pressure Surveillance Test.Cause of Failure Under Review by Site & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Cleaned |
- on 880311,nine Safety Relief Valves Failed Pressure Surveillance Test.Cause of Failure Under Review by Site & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Cleaned
| | 05000341/LER-1988-010, :on 880310,turbine Bldg Stationary Particulate, Iodine & Noble Gas Radiation Monitor Lost Power.Caused by Failure of Operations Personnel to Comply W/Requirement of Abnormal line-up Sheet |
- on 880310,turbine Bldg Stationary Particulate, Iodine & Noble Gas Radiation Monitor Lost Power.Caused by Failure of Operations Personnel to Comply W/Requirement of Abnormal line-up Sheet
| | 05000341/LER-1988-011, :on 880313,failure to Perform Shiftly Surveillance within Required Time Occurred.Caused by Failure to Designate Person to Perform Surveillance When Personnel Reassigned.Requirement Added |
- on 880313,failure to Perform Shiftly Surveillance within Required Time Occurred.Caused by Failure to Designate Person to Perform Surveillance When Personnel Reassigned.Requirement Added
| | 05000341/LER-1988-012, :on 880316,rack Isolation Valve for Reactor Protection Sys Channel C Drywell Pressure Instrument Found Closed.Caused by Failure to Fully Open Valve After 861016 Surveillance.Procedure 23.137 Revised |
- on 880316,rack Isolation Valve for Reactor Protection Sys Channel C Drywell Pressure Instrument Found Closed.Caused by Failure to Fully Open Valve After 861016 Surveillance.Procedure 23.137 Revised
| | 05000341/LER-1988-013, :on 880318,shutdown Cooling Was Lost Due to Closure of Suction Isolation Valve & Subsequent Tripping of RHR Pump.Caused by Procedural Inadequacies & Personnel Error.Sys Operating Procedures Will Be Revised |
- on 880318,shutdown Cooling Was Lost Due to Closure of Suction Isolation Valve & Subsequent Tripping of RHR Pump.Caused by Procedural Inadequacies & Personnel Error.Sys Operating Procedures Will Be Revised
| | 05000341/LER-1988-014, :on 880320,Div I Emergency Diesel Generators Inadvertently Started.Caused by Procedural Error.Revs Issued Which Corrected Sequence of Steps |
- on 880320,Div I Emergency Diesel Generators Inadvertently Started.Caused by Procedural Error.Revs Issued Which Corrected Sequence of Steps
| | 05000341/LER-1988-016, :on 880420,closure of RHR Shutdown Cooling Outboard Isolation Valve Occurred.Caused by Failure of Agastat Relay A71B-K75.Relay & Fuse Replaced & Tested & Valve Returned to Normal Operation |
- on 880420,closure of RHR Shutdown Cooling Outboard Isolation Valve Occurred.Caused by Failure of Agastat Relay A71B-K75.Relay & Fuse Replaced & Tested & Valve Returned to Normal Operation
| | 05000341/LER-1988-017, :on 880427,control Ctr HVAC Shifted to Recirculation Mode Due to de-energization of Local Panel. Caused by Short in Panel When Burned Indicator Lamp Removed from Panel.Subj Lamp & Opened Fuse Replaced |
- on 880427,control Ctr HVAC Shifted to Recirculation Mode Due to de-energization of Local Panel. Caused by Short in Panel When Burned Indicator Lamp Removed from Panel.Subj Lamp & Opened Fuse Replaced
| | 05000341/LER-1988-018, :on 880503,operator Failed to Perform Shiftly Surveillance within Allowable Time.Caused by Personnel Error.Counselling Provided & Personnel Involved Disciplined |
- on 880503,operator Failed to Perform Shiftly Surveillance within Allowable Time.Caused by Personnel Error.Counselling Provided & Personnel Involved Disciplined
| | 05000341/LER-1988-019, :on 880507,offsite Power to Div 1 Interrupted When CRD Pump a Tripped on Loss of Power.Caused by Raccoon Climbing Sys Svc Transformer.Gravel Brought in to Bring Grade Above Fence Line |
- on 880507,offsite Power to Div 1 Interrupted When CRD Pump a Tripped on Loss of Power.Caused by Raccoon Climbing Sys Svc Transformer.Gravel Brought in to Bring Grade Above Fence Line
| | 05000341/LER-1988-020, :on 880508,incorrect HPCI Surveillance Test Procedure Performed Causing Reactor Scram.Procedure Intended to Be Performed in Cold Shutdown or Refueling Condition. Procedure 24.202.04 Revised |
- on 880508,incorrect HPCI Surveillance Test Procedure Performed Causing Reactor Scram.Procedure Intended to Be Performed in Cold Shutdown or Refueling Condition. Procedure 24.202.04 Revised
| | 05000341/LER-1988-021, :on 880510,reactor Protection Sys High Pressure Scram Occurred 18 After Closure of Both Main Steam Bypass Valves.Caused by Faulty Relay.Relay Replaced.Mod to Alter Comparator Trip Circuits Planned |
- on 880510,reactor Protection Sys High Pressure Scram Occurred 18 After Closure of Both Main Steam Bypass Valves.Caused by Faulty Relay.Relay Replaced.Mod to Alter Comparator Trip Circuits Planned
| | 05000341/LER-1988-022, :on 880613,Div 2 Emergency Diesel Generators & Core Spray Pumps Actuated.Most Likely Caused by Personnel Error.Program Will Be Developed to Perform Periodic Audits of Personnel During Surveillance Procedure |
- on 880613,Div 2 Emergency Diesel Generators & Core Spray Pumps Actuated.Most Likely Caused by Personnel Error.Program Will Be Developed to Perform Periodic Audits of Personnel During Surveillance Procedure
| | 05000341/LER-1988-023, :on 880528 & 0713,RWCU Sys Manually Isolated by Operator Action.Caused by Separate Instrument Line Compression Failures.Instrument Lines Repaired & RWCU Sys Operating Procedures Revised |
- on 880528 & 0713,RWCU Sys Manually Isolated by Operator Action.Caused by Separate Instrument Line Compression Failures.Instrument Lines Repaired & RWCU Sys Operating Procedures Revised
| | 05000341/LER-1988-024, :on 880705,isolation of HPCI During Performance of Functional Test Occurred.Caused by Personnel Error. Surveillance Successfully Performed on Same Day & Accountability Meeting Held W/Individual |
- on 880705,isolation of HPCI During Performance of Functional Test Occurred.Caused by Personnel Error. Surveillance Successfully Performed on Same Day & Accountability Meeting Held W/Individual
| | 05000341/LER-1988-025, :on 880719,breaker Tripped & Reactor Protection Sys Trip Sys B de-energized.Caused by Personnel Mishap.Event Will Be Included in Maint News Ltr & in Instrumentation & Controls Training Program |
- on 880719,breaker Tripped & Reactor Protection Sys Trip Sys B de-energized.Caused by Personnel Mishap.Event Will Be Included in Maint News Ltr & in Instrumentation & Controls Training Program
| | 05000341/LER-1988-026, :on 880723,unit Shut Down.Caused by Leakage in Valves E51-F007 & G33-F100 Which Developed Following Stroking of Valves While Plant in Operation.Stems on Valves Replaced & Valves Repacked |
- on 880723,unit Shut Down.Caused by Leakage in Valves E51-F007 & G33-F100 Which Developed Following Stroking of Valves While Plant in Operation.Stems on Valves Replaced & Valves Repacked
| | 05000341/LER-1988-027, :on 880726,technician Accidentally Shorted Across Two Terminals Which Actuated Div I of Emergency Equipment Cooling Water & Emergency Equipment Svc Water Sys. Caused by Personnel Error.Technician Counseled |
- on 880726,technician Accidentally Shorted Across Two Terminals Which Actuated Div I of Emergency Equipment Cooling Water & Emergency Equipment Svc Water Sys. Caused by Personnel Error.Technician Counseled
| | 05000341/LER-1988-028, :on 880726,HPCI Pump Discharge Inboard Isolation Valve Failed to Open.Caused by Grounded Contactor Coil at Valve Torque Switch by Heater Bracket.Heater Assembly & Nine Other Valves Removed |
- on 880726,HPCI Pump Discharge Inboard Isolation Valve Failed to Open.Caused by Grounded Contactor Coil at Valve Torque Switch by Heater Bracket.Heater Assembly & Nine Other Valves Removed
| | 05000341/LER-1988-029, :on 880802,24 Hydraulic Control Unit Scram Inlet & Oulet Valves Opened Due to Deenergization of Associated Stated Valves.Caused by Improper Termination of Cable.Reactor Protection Sys Logic Reset |
- on 880802,24 Hydraulic Control Unit Scram Inlet & Oulet Valves Opened Due to Deenergization of Associated Stated Valves.Caused by Improper Termination of Cable.Reactor Protection Sys Logic Reset
| | 05000341/LER-1988-030, :on 880813,main Turbine on High Vibration of Bearings 8 & 9 Tripped.Caused When General Svc Water Flow Control Valve to Main Turbine Generator Lube Oil Coolers Failed Open.Failed Valve Repaired |
- on 880813,main Turbine on High Vibration of Bearings 8 & 9 Tripped.Caused When General Svc Water Flow Control Valve to Main Turbine Generator Lube Oil Coolers Failed Open.Failed Valve Repaired
| | 05000341/LER-1988-031, :on 880815,accelerated Valve Stroke Time Testing of HPCI Discharge Isolation Valve E41-F067 Not Performed as Required.Caused by Personnel Error.Individual Involved Counseled |
- on 880815,accelerated Valve Stroke Time Testing of HPCI Discharge Isolation Valve E41-F067 Not Performed as Required.Caused by Personnel Error.Individual Involved Counseled
| | 05000341/LER-1988-032, :on 880820 & 28,recirculation Pump B Discharge Valve Failed to Close.Caused by Torque Switch Being Set at Incorrect Value & Improperly Installed.Program That Controls Torque Switch Settings Will Be Improved |
- on 880820 & 28,recirculation Pump B Discharge Valve Failed to Close.Caused by Torque Switch Being Set at Incorrect Value & Improperly Installed.Program That Controls Torque Switch Settings Will Be Improved
| | 05000341/LER-1988-033, :on 880822,RWCU Sys & Outboard Isolation Valves Automatically Closed Upon Receipt of High Differential Flow Isolation Signal.Caused by Steam Voiding in Sys at Pump Discharge Flow Element |
- on 880822,RWCU Sys & Outboard Isolation Valves Automatically Closed Upon Receipt of High Differential Flow Isolation Signal.Caused by Steam Voiding in Sys at Pump Discharge Flow Element
| | 05000341/LER-1988-034, :on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits Replaced |
- on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits Replaced
| | 05000341/LER-1988-035, :on 881004,automatic Scram Signal Generated During Shutdown.Caused by Control Room Operator Failure to Follow Procedures When Resetting Manual Scram Signal. Operator Counselled |
- on 881004,automatic Scram Signal Generated During Shutdown.Caused by Control Room Operator Failure to Follow Procedures When Resetting Manual Scram Signal. Operator Counselled
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