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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000331/LER-1993-0061993-09-0909 September 1993 LER 93-006-00:on 930813,partial PCIS Group 3 Isolation Occurred Due to Inadequate Written & Verbal Communications. Event Will Be Reviewed by Engineering,Operations & Maint by 931201 to Stress Need for Good communications.W/930909 Ltr ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 05000331/LER-1983-027, /01T-0:on 830803,during Surveillance Required by Inoperable RCIC (LER 83-027),speed Indication for HPCI Turbine Failed.Caused by Faulty Turbine Magnetic Speed Pickup.Turbine Oil Sys Adjusted1983-08-17017 August 1983 /01T-0:on 830803,during Surveillance Required by Inoperable RCIC (LER 83-027),speed Indication for HPCI Turbine Failed.Caused by Faulty Turbine Magnetic Speed Pickup.Turbine Oil Sys Adjusted 05000331/LER-1981-016, Updated LER 81-016/01T-1:on 810421,lower Crankshaft Thrust Bearing 13 & Adjacent Bearing 12 Found Wiped on Journal Surface.Caused by High Temp.Crankshaft Thrust Bearings Replaced & Crankshaft Relapped1983-05-16016 May 1983 Updated LER 81-016/01T-1:on 810421,lower Crankshaft Thrust Bearing 13 & Adjacent Bearing 12 Found Wiped on Journal Surface.Caused by High Temp.Crankshaft Thrust Bearings Replaced & Crankshaft Relapped 05000331/LER-1981-015, Updated LER 81-015/01T-1:on 810421,lower Crankshaft 14 Bearing Found Wiped on Journal Surface Similar to Problem Identified on Diesel 1G-31.Caused by High Temp.Bearing Replaced & Crankshaft Relapped1983-05-16016 May 1983 Updated LER 81-015/01T-1:on 810421,lower Crankshaft 14 Bearing Found Wiped on Journal Surface Similar to Problem Identified on Diesel 1G-31.Caused by High Temp.Bearing Replaced & Crankshaft Relapped ML20148N5821978-06-30030 June 1978 /01T-0 on 780617:water Leak Found in Area of B Recirculation Sys N2A Inlet Nozzle Caused by Wall Crack in Nozzle Safe End.Lab Analysis Will Be Performed to Determine Cause of Cracking 1993-09-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H8991999-10-18018 October 1999 SER Approving Licensee Requests for Relief NDE-R001 (Part a & B),NDE-R027,NDE-028,NDE-R029,NDE-R030,NDE-R032 & NDE-R035. Relief Request NDE-036,denied & Relief Request NDE-R-034, Deemed Unnecessary NG-99-1415, Monthly Operating Rept for Sept 1999 for Daec.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Daec.With ML20212H2381999-09-22022 September 1999 Safety Evaluation Supporting Amend 228 to License DPR-49 NG-99-1226, Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Duane Arnold Energy Center.With NG-99-1115, Monthly Operating Rept for July 1999 for Daec.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Daec.With NG-99-0963, Monthly Operating Rept for June 1999 for Daec.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Daec.With ML20195G9901999-06-0909 June 1999 Safety Evaluation Supporting Amend 227 to License DPR-49 NG-99-0835, Monthly Operating Rept for May 1999 for Daec.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Daec.With ML20206N7551999-05-13013 May 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safey-Related Power-Operated Gate Valves NG-99-0682, Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Duane Arnold Energy Center.With NG-99-0530, Monthly Operating Rept for Mar 1999 for Daec.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Daec.With ML20207G0251999-03-0303 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety- Related MOVs at Duane Arnold & That Licensee Adequately Addressed Actions Requested in GL 96-05 NG-99-0330, Monthly Operating Rept for Feb 1999 for Daec.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Daec.With ML20202B4311999-01-26026 January 1999 Safety Evaluation Accepting Request for Approval to Use ASME Code Case N-508-1 in ISI Program for Duane Arnold Energy Ctr ML20202B3851999-01-26026 January 1999 Safety Evaluation Addressing Thermo-Lag Related Ampacity Derating Issues.Ampacity Derating Analysis Results Acceptable NG-99-0020, Monthly Operating Rept for Dec 1998 for Daec.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Daec.With ML20206N3211998-12-0707 December 1998 Final Part 21 Rept Re Piston Failure of MSIV Actuator at Daec.Rept Indicates That No Reportable Defect Exists,Per 10CFR21 NG-98-2010, Monthly Operating Rept for Nov 1998 for Daec.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Daec.With ML20196F9571998-11-24024 November 1998 Rev 20 to QA Program Description,Ufsar 17.2 for Daec NG-98-1875, Monthly Operating Rept for Oct 1998 for Daec.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Daec.With NG-98-1767, Cyclic Rept of Facility Changes,Tests & Experiments,Fire Plan & Commitment Changes,For Period from 970301-980930. with1998-09-30030 September 1998 Cyclic Rept of Facility Changes,Tests & Experiments,Fire Plan & Commitment Changes,For Period from 970301-980930. with NG-98-1717, Monthly Operating Rept for Sept 1998 for Daec.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Daec.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML20153B4141998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DAEC NG-98-1389, Monthly Operating Rept for July 1998 for DAEC1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DAEC ML20236X5321998-07-29029 July 1998 Safety Evaluation Re USI A-46 Program Implementation for Plant ML20236W0021998-07-29029 July 1998 Safety Evaluation Accepting Request for Relief NDE-R020 Re Third 10-yr ISI Interval of Plant,Per 10CFR50.55a(a)(3(i) ML20236S2541998-07-14014 July 1998 Special Rept 98-01:on 980629,diesel-driven Fire Pump Was Inoperable for Greater than Seven Days.Caused by Sheared Off Tie Rods on Accessory Drive End of Engine.Evaluated Condition,Procured Parts & Replaced Tie Rods ML20236R3251998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DAEC ML20249B5171998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DAEC ML20247P5651998-05-18018 May 1998 Part 21 Rept Re Model SA-A101 MSIV A' Actuator Showing Evidence of Internal Leakage,In Both Directions Past Pneumatic Piston.Situation Being Reviewed to Determine If Failure Could Pose Substantial Safety Hazard ML20247K1881998-05-0808 May 1998 Rev 0 to Cycle 16 COLR, for May 1998 ML20247H9381998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DAEC ML20217K7251998-04-16016 April 1998 Correction to SE of Relief Request MC-R001 Re Qualification Requirements for non-destructive Exam Personnel Performing Containment Insp ML20216J9171998-04-16016 April 1998 Safety Evaluation Accepting Relief Request MC-R001 for First 10-yr Interval of Containment Insp Program Per 10CFR50.55a (a)(3)(ii),per 971219 Request ML20217K0471998-04-0101 April 1998 Safety Evaluation Authorizing Proposed Alternative in Relief Request NDE-R004 for Plant Third 10-yr ISI Interval,Based on Finding That Compliance W/Code Would Result in Hardship W/O Compensating Increase in Level of Quality & Safety ML20217H8831998-04-0101 April 1998 Safety Evaluation Supporting Request for Relief for Third ISI Program ML20216F6791998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for DAEC NG-98-0650, Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Duane Arnold Energy Center ML20217F8841998-03-23023 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Program Plan Requests for Relief for Plant NG-98-0398, Monthly Operating Rept for Feb 1998 for DAEC1998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for DAEC ML20199L3481998-01-31031 January 1998 Rev 0 to Duane Arnold Energy Ctr Emergency Action Level (EAL) Technical Basis Document NG-98-0252, Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Duane Arnold Energy Center ML20249B3391997-12-31031 December 1997 Central Iowa Power Coopertive 1997 Annual Rept ML20249B3351997-12-31031 December 1997 1997 Annual Rept for Corn Belt Power Cooperative ML20249B3331997-12-31031 December 1997 1997 Annual Rept for Alliant Corporation NG-98-0017, Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center1997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Duane Arnold Energy Center NG-97-2118, Monthly Operating Rept for Nov 1997 for DAEC1997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DAEC ML20199J6841997-11-21021 November 1997 SER Approving Relief Requests to Second 10-year Inservice Inspection Interval for Duane Arnold Energy Center NG-97-1959, Monthly Operating Rept for Oct 1997 for DAEC1997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for DAEC 1999-09-30
[Table view] |
LER-2083-027, /01T-0:on 830803,during Surveillance Required by Inoperable RCIC (LER 83-027),speed Indication for HPCI Turbine Failed.Caused by Faulty Turbine Magnetic Speed Pickup.Turbine Oil Sys Adjusted |
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3312083027R00 - NRC Website |
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$ ,.. n i rable RCIC (See LER 83-0'27), it was found that the. speed indication for- I gi the HPCI turbine had failed. The testing of HPCI could not be completed 1 3 a ,,i i due to this problem. HPCI was declared inoperable and a shutdown wds ini ' _ l gi tiated in accordance with T.S. 3.5.E.3. Later on 8/3, PCIC was repaired I io ,7 l l and returned to service. The shutdown was terminated and a 7 day LC0 ant I m l ered IAW T.S. 3.5.D.2. No effect on health and safety of oublic. **
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Neurcaemeramen Daniel R. Kibler ,uoy g; 319-851-7306 ,
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, DUANE ARNOLD ENERGY CEHTER Iowa Electric Light! and Power Company
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Licensee Event Report - Supplemental Data x -
Docket No. 050-0331
. s L l.icensee Event Report Date: 8-17-83 l p2portableOccurrenceNo.: 83-028 Event Description and' Probable Consequences During normal operation, while conducting surveillance required by T.S. 4.5.E.2 for inoperable RCIC (see LER 83-027), it was found that the speed indication for the HPCI turbine had failed. The testing of HPCI could not be completed due to this problem. HPCI was declared inoperable and a shutdown was initiated in accordance with T.S. 3.5.E.3. Later on 8/3, RCIC was repaired and returned to service. The shutdown was terminated and a 7 day LC0 entered in accordance y'.with T.S. 3.5.D.2. ADS, CS and LPCI were operable throughout the HPCI and RCIC inoperable problems. No effect on health and safety of public.
Cause Description and Corrective Action
'The tirbine magnetic speed pickup was found to be faulty. The pickup was replaced.
When tie turbine was tested following the replacement of the speed pickup, speed contrd! was unstable. The turbine oil system was adjusted and the turbine retested.
Furthe'r adjustments were made to the turbine suction pressure indication and the tujbine speed circuits and the system tested satisfactorily. The 7-day LC0 was ended,on 3/6. Repetitive failures of HPCI during 1983 have been evaluated.
The evaluation determined failures to be non-related.
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Page 1 of I
w y-lowa Electric Light and Ibwer Company August 17, 1983 DAEC-83-674 Mr. Janes G. Keppler Regional Administrator Region III U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137
Subject:
Duane Arnold Energy Center Docket No. 50-331 Op. License DPR-49 Licensee Event Report No.83-028 (14-day)
Dear Mr. Keppler:
In accordance with Appendix A to Operating License DPR-49, Technical Specifications, Section 6.11.2.a(7), and dases for Duane Arnold Energy Center and Regulatory Guide 10.1, please find attached a copy of the subject Licensee Event Report.
Very truly yours, Daniel L. Mineck P1 ant Superintendent - Nuclear Duane Arnold Energy Center DLM/ DRK/pf l attachment cc: Document Control Desk U. S. Nuclear Regulatory Commission Washington, D. C. 20555 NRC Resident Inspector - DAEC File A-118a g)G a 9 Y
t
/y a Duane Arnold Energy Center. P.O. Box 351. Cedar Flapids, Iowa 52406 319!8517611
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05000331/LER-1983-001, Forwards LER 83-001/03L-0 | Forwards LER 83-001/03L-0 | | 05000331/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | 05000331/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | 05000331/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | 05000331/LER-1983-005, Forwards LER 83-005/03L-0 | Forwards LER 83-005/03L-0 | | 05000331/LER-1983-006, Forwards LER 83-006/03L-0 | Forwards LER 83-006/03L-0 | | 05000331/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | 05000331/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | 05000331/LER-1983-009, Forwards LER 83-009/03L-0 | Forwards LER 83-009/03L-0 | | 05000331/LER-1983-027, /01T-0:on 830803,during Surveillance Required by Inoperable RCIC (LER 83-027),speed Indication for HPCI Turbine Failed.Caused by Faulty Turbine Magnetic Speed Pickup.Turbine Oil Sys Adjusted | /01T-0:on 830803,during Surveillance Required by Inoperable RCIC (LER 83-027),speed Indication for HPCI Turbine Failed.Caused by Faulty Turbine Magnetic Speed Pickup.Turbine Oil Sys Adjusted | |
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