05000316/LER-2006-003

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LER-2006-003, Inadvertent Emergency Core Cooling System Actuation During Testing
Docket Number 04 27 2006 2006 --0003 --000 06 23 06
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
3162006003R00 - NRC Website

Description of Event

On April 27, 2006, at 0207 hours0.0024 days <br />0.0575 hours <br />3.422619e-4 weeks <br />7.87635e-5 months <br />, while in MODE 5 and conducting activities to prepare for the performance of 2-IHP-4030-STP-180, "Prior to Startup (SU) Instrumentation Channel Operating Test and Trip Actuating device Operational Test," Donald C. Cook Nuclear Plant (CNP) Unit 2 received a main steam line low pressure safety injection (SI) signal on both trains. The following components automatically started:

Unit 2 west centrifugal charging pump (CCP) (on minimum flow recirculation path with injection path isolated for low temperature overpressure protection (LTOP) — no injection to reactor coolant system (RCS)) [BQ] Unit 2 south SI pump (on minimum flow recirculation path with injection path isolated for LTOP — no injection to RCS) [BQ] Unit 2 east residual heat removal (RHR) pump [BP] Unit 2 east component cooling water (CCW) pump [CC] Unit 2 CD emergency diesel generator (EDG) [EK] Both trains of Unit 2 control room pressurization [VI] Both trains of Unit 2 phase A containment isolation signal [JM] Both trains of Unit 1 control room pressurization fans [VI] Unit 1 east and west essential service water (ESW) pumps [BI] All equipment operated as designed. No injection to the RCS occurred due to LTOP system line-ups that were in effect.

general containment isolation, emergency core cooling system, and emergency AC electrical power systems.

On April 27, 2006, at 0918 hours0.0106 days <br />0.255 hours <br />0.00152 weeks <br />3.49299e-4 months <br />, Indiana Michigan Power Company (I&M), in accordance with the reporting requirements established in 10 CFR 50.72(b)(3)(iv)(A), completed its prompt notification of this event to the Nuclear Regulatory Commission Operations Center via the Emergency Notification System.

Analysis of Event

While conducting activities in preparation to perform required surveillance testing on Unit 2, maintenance personnel were attempting to clear several standing reactor trip signals on multiple channels using the newly installed reactor trip protection system bypass function. This resulted in an inadvertent SI on both trains due to the "Low Steam Line Pressure SI Block" having been removed with all Unit 2 steam generator pressures below the low pressure main steam line isolation and SI actuation set point of 500 psig. As designed, a main steam line isolation signal was generated; however, the main steam line isolation valves were already closed (the designated response position to low pressure steam line isolation signal) in support of system maintenance at the time of the event. As reported above, available Unit 2 emergency safety features equipment started, consisting of the Unit 2 CD EDG, the Unit 2 south SI pump, the Unit 2 west CCP, Unit 2 east RHR pump, and Unit 2 east CCW pump. Both trains of Unit 2 control room pressurization fans started and a Unit 2 phase "A" isolation occurred. Both trains of Unit 1 control room pressurization actuated and Unit 1 east and west ESW pumps automatically started (as designed) in response to the Unit 2 SI signal. Unit 2 was in MODE 5 at approximately 180 degrees F and 300 psig with the applicable Unit 2 LTOP controls and alignments in effect in a supporting alignment for Unit 2 Train B loss of offsite power/loss of coolant accident testing. The north (train A) SI pump was disabled in test and did not start. The south (train B) SI pump started, but did not inject because the discharge flow path was manually isolated for LTOP. The west (train B) CCP started, but did not inject because the discharge flow path was isolated for LTOP. Phase "A" Containment Isolation occurred as expected. At the time of the event, the AB EDG was out of service for planned maintenance. The pressurizer surge line (AB] temperature lowered from 412 degrees F to 205 degrees F and subsequently returned to 414 degrees F. This pressurizer surge line transient was evaluated and it was determined that the qualification of both the surge line and pressurizer were not impacted. No specific plant safety-related equipment OPERABILITY concerns were noted at the time and none were subsequently identified.

Events such as this represent a potential to challenge Unit 2 RCS integrity; however, all appropriate administrative and equipment controls were in place and there was no injection into the RCS as a result of this actuation, and thus no RCS integrity challenge. No additional equipment became unavailable as a result of this event. In that no additional plant equipment was made unavailable and no other equipment challenges occurred, there was no challenge to any key safety functions (i.e., shutdown cooling, inventory control, reactivity control, containment closure, electric power distribution, service water (CCW/ESW), and spent fuel pit cooling).

The impact to Unit 1 from a "shared PRA equipment" perspective was minimal in that the Unit 1 control room pressurization system started (not a PRA modeled system) and the stand-by ESW pumps auto-started from the Unit 2 SI. The extra operating ESW pumps did not affect either ESW system function or any related equipment availability. Thus, there was no significant risk impact to Unit 1 from this event.

Cause of Event

The root cause of the inadvertent SI actuation was the failure of instrument maintenance personnel to implement procedure use and adherence requirements when using a job order to bypass channels instead of using existing procedures to clear the standing reactor trip signals (formal procedures were available to address all of the standing trip signals that were observed for LTiTavg and SG level).

Corrective Actions

Immediate corrective actions included returning the bypass switches to their normal position, resetting the safety injection signal by reinstating the main steam line low pressure safety injection block, and restoring all actuated equipment to their pretest configuration. Additionally, the Plant Manager, Maintenance Manager, and Maintenance Instrumentation and Control Manager briefed the Instrumentation and Control personnel regarding this event and communicated expectations for remaining outage activities.

l&M will revise Procedure MHI-5000, "Conduct of Maintenance," to clarify procedure use and adherence requirements and expectations that a job order cannot be used to provide detailed instructions that manipulate plant components in order to establish initial conditions or bridge steps to support implementing procedures.

l&M will revise Procedure PMP-2291-PLN-001, 'Work Control Activity Planning Process," to clarify procedure use and adherence requirements and expectations that a job order cannot be used to provide detailed instructions that manipulate plant components in order to establish initial conditions or bridge steps to support implementing procedures.

l&M will utilize department communication, stand down, or all-hands meeting for the maintenance and work control departments to reinforce the requirements and expectations established in the above procedure revisions.

i&M will update initial and continuing training programs for Maintenance and Work Control personnel regarding procedure use and adherence guidance. Available video type training tools will be utilized to demonstrate expectations and provide examples for complying with procedure use and adherence, purpose and intent, place keeping, questioning attitude, and self checking.

l&M will establish and implement a procedure to provide instructions and limitations for using the channel bypass functions.

Previous Similar Events

None.