05000305/FIN-2011005-08
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Finding | |
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Title | Procedures for Reduced Inventory Operations were not Appropriate to Preclude Air Entrainment |
Description | The inspectors identified a finding of very low safety significance and associated NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure to establish procedures for reduced inventory operations that were appropriate to manage gas accumulation. Specifically, the procedures did not preclude air entrainment into the residual heat removal (RHR) and reactor coolant systems (RCSs). This finding was entered into the licensees corrective action program (CAP). The licensee\\\'s immediate corrective actions included calculating the instrument inaccuracies for RHR flow and refueling level instrument loops, referencing the level inaccuracies based on inactive flow in RCS loops in the associated procedures, evaluating levels, and updating the procedures with a new graph. The performance deficiency was determined to be more than minor because it was associated with the Initiating Event Cornerstone attribute of procedure quality, and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shut-down operations. Specifically, the failure to establish procedures for reduced inventory operations that were appropriate to preclude air entrainment did not limit the likelihood of events that result from adverse air entrainment into the RHR and RCSs. The finding screened as having very low safety significance (Green) because the Region III Senior Reactor Analysts determined that it reasonably met the safety functions of core heat removal, RCS inventory control, power availability, containment control, and reactivity control; and there had been no actual air entrainment problems that had occurred using the procedures. The finding has a cross-cutting aspect in the area of Problem Identification and Resolution because the licensee did not thoroughly evaluate relevant operating experience. Specifically, the licensees evaluation of gas-related issues in response to NRC Generic Letter (GL) 2008-01 was deficient in that it did not consider vortexing during reduced inventory operations. |
Site: | Kewaunee |
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Report | IR 05000305/2011005 Section 4OA5 |
Date counted | Dec 31, 2011 (2011Q4) |
Type: | NCV: Green |
cornerstone | Initiating Events |
Identified by: | NRC identified |
Inspection Procedure: | |
Inspectors (proximate) | D Mcneil R Winter K Riemer J Cassidy D Betancourt K Barclay N Feliz-Adomo M Jones J Beavers V Myers S Shah M Ziolkowski |
CCA | P.5, Operating Experience |
INPO aspect | CL.1 |
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Finding - Kewaunee - IR 05000305/2011005 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Kewaunee) @ 2011Q4
Self-Identified List (Kewaunee)
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