LER-1983-004, Forwards LER 83-004/03L-0.Detailed Event Analysis Submitted |
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T COOPER NUCLEAR STATION Nebraska Public Power District
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CNSS830308 April 29, 1983 h[@((h33 1
J MAY - 5 !983 u6 Mr. John T. Collins, Regional Administrator
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U. S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region IV 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76011
Dear Sir:
This report is submitted in accordance with Section 6.7.2.B.1 of the Technical Specifications for Cooper Nuclear Station and discusses a reportable occur-rence that was discovered on April 9, 1983.
A licensee report form is also enclosed.
Report No.:
50-298-83-04 Report Date:
April 29, 1983 Occurrence Date:
April 9, 1983 Facility:
Cooper Nuclear Station Brownville, Nebraska 68321 Identification of Occurrence:
A ccndition occurred which resulted in operation in a degraded mode as permitted by Section 3.1 of the Technical Specifications.
Conditions Prior to Occurrence:
The reactor was operating at a steady state power level of 87.8% of rated thermal power.
Description of Occurrence:
During the performance of Surveillance Procedure 6.1.4 (Main Steam Line Process Radiation Monitor Functional Tect), relay 917-5A-K7D failed to open its contacts when the relay was deenergized.
Designation of Apparent Cause of Occurrence:
The cause of the relay coil failure could not be determined.
Analysis et Occurrence:
Relay 917-5A-K7D is operated by two normally closed contacts from Main Steam Line Radiation channel "D" (17-251D).
One contact will open at a preset high radiation level and the second will open due to equipment inoperability.
If either contact opens, the relay will deenergize.
9 er 8305120433 830429
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PDR ADOCK 05000298 y
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s Mr. John T. Collins April 29, 1983 Page 2 The relay, in turn, operates a series pair of contacts in the Reactor Protection System (RPS) Auto-Scram Trip Logic "B2".
These contacts are two of approximately 36 which could deenergize "B2" Trip Logic, and pass a scram signal to open the "B" Trip System Scram Solenoid Valve for each Control Rod Drive (CRD).
Redundant Auto-Scram Trip Logic "Bl" perforns the same function of tripping the CRD Scram Solenoid Valves, independent of Trip Logic "B2".
A Manual Scram Trip Logic "B3" will also trip "B" system Scram Solenoid Valves.
The RPS system is conposed, in part, of two identical, independent trip systens, "A" and "B".
Each systen is a scries of sensors, relays, and contacts which open a Scram Solenoid Valve for each CRD.
There are two solenoid valvas, one controlled from Trip System "A" and the second fron Trip System "B", both of which must open to cause a scram. To initiate a scram, any one of the three trip logics in the "A" system and any one of the three "B" system trip logics must trip.
Relay 917-5A-K7D failed to open when deenergized during the performance of Surveillance Procedure 6.1.4.
The other trip logic systems were operable at the time of this occurrence.
The cause for the relay coil failure could not be determined.
This is the fourth failure of HFA relays at Cooper Nuclear Station. Thr first failure was not reportable, and the other two were reported in LERs 82-21 and 82-25.
This occurrence presented no adverse potential consequences from the standpoint of public health and safety.
Corrective Action
A "B" Group I isolation was placed in the trip condition as required per Technical Specifications. The relay coil was replaced and correct systen operation was verified.
Due to the increasing occurrence of GE Type HFA relay failures, all AC HFA relays will be tested during the Spring 1983 outage in an effort to identify potential failures.
Appropriate action will be taken on those found to be potentially defective.
A program is currently being formulated to replace all AC HFA relays.
Sincerely,
.M /
P. V. Thomason Acting Station Superintendent Cooper Nuclear Station PVT:RWK:cg Attach.
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| 05000298/LER-1983-001, Forwards LER 83-001/03L-0.Detailed Event Analysis Submitted | Forwards LER 83-001/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1983-001-03, /03L-0:on 830223,while Performing Surveillance Procedure 6.2.2.2.4,safety Relief Valve 71-C Failed to Transfer Alternate Power Source When Fuse Pulled.Caused by Bad Contact on Relay.Relay Control Wipe Adjusted | /03L-0:on 830223,while Performing Surveillance Procedure 6.2.2.2.4,safety Relief Valve 71-C Failed to Transfer Alternate Power Source When Fuse Pulled.Caused by Bad Contact on Relay.Relay Control Wipe Adjusted | | | 05000298/LER-1983-002-03, /03L-0:on 830218,source Range Monitor Rod Blocks Not Tested Prior to Hot Startup.Caused by Inadequate Procedures.Procedure 2.1.2 Revised | /03L-0:on 830218,source Range Monitor Rod Blocks Not Tested Prior to Hot Startup.Caused by Inadequate Procedures.Procedure 2.1.2 Revised | | | 05000298/LER-1983-002, Forwards LER 83-002/03L-0.Detailed Event Analysis Submitted | Forwards LER 83-002/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Submitted | Forwards LER 83-003/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1983-003-03, /03L-0:on 830403,indication & Control Power for Reactor Bldg Exhaust Valve HN-260MV Failed,Resulting in Valve Not Automatically Closing on Isolation Signal.Caused by Burned Out Lamp.Lamp & Fuse Replaced | /03L-0:on 830403,indication & Control Power for Reactor Bldg Exhaust Valve HN-260MV Failed,Resulting in Valve Not Automatically Closing on Isolation Signal.Caused by Burned Out Lamp.Lamp & Fuse Replaced | | | 05000298/LER-1983-004-03, /03L-0:on 830409,during Sp 6.1.4,contacts of Relay 917-5A-K7D Failed to Open.Cause Not Determined.Relay Coil Replaced & Proper Operation Verified.All Ac Hfa Relays on Essential Sys Will Be Tested During Spring 1983 Outage | /03L-0:on 830409,during Sp 6.1.4,contacts of Relay 917-5A-K7D Failed to Open.Cause Not Determined.Relay Coil Replaced & Proper Operation Verified.All Ac Hfa Relays on Essential Sys Will Be Tested During Spring 1983 Outage | | | 05000298/LER-1983-004, Forwards LER 83-004/03L-0.Detailed Event Analysis Submitted | Forwards LER 83-004/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1983-005-03, /03L-0:on 830505,scram Discharge Vol Drain Value CRD-CV-AOV33 Failed to Close Per Tech Specs.Caused by Grafoil Packing Working Between Valve Stem & Body.Valve Repacked | /03L-0:on 830505,scram Discharge Vol Drain Value CRD-CV-AOV33 Failed to Close Per Tech Specs.Caused by Grafoil Packing Working Between Valve Stem & Body.Valve Repacked | | | 05000298/LER-1983-006-03, /03L-0:on 830509,during Performance of Surveillance Procedure 6.3.10.9.1,four RHR Mechanical Snubbers Frozen.Caused by RHR Shutdown Cooling Creating Water Hammer & Overloading snubbers.w/830608 Ltr | /03L-0:on 830509,during Performance of Surveillance Procedure 6.3.10.9.1,four RHR Mechanical Snubbers Frozen.Caused by RHR Shutdown Cooling Creating Water Hammer & Overloading snubbers.w/830608 Ltr | | | 05000298/LER-1983-007-03, /03L-0:on 830518,during Refueling,Both Standby Gas Treatment Sys Diesel Generators Found Inoperable.Caused by Personnel Failure to Follow Tech Spec Requirements. 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