05000296/LER-2012-002

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LER-2012-002, Main Steam Isolation Valve Leakage in Excess of Technical Specification Requirements
Docket Numbersequential Revmonth Day Year Year Month Day Yearnumber No N/A 05000
Event date: 04-07-2012
Report date: 06-06-2012
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2962012002R00 - NRC Website

I. PLANT CONDITION(S)

At the time of the event, Browns Ferry Nuclear Plant (BFN), Unit 3, was at zero percent power in Mode 3 during a planned shutdown for a refueling outage.

II. DESCRIPTION OF EVENT

A. Event

On April 8, 2012, at approximately 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br /> Central Daylight Time (CDT), during the performance of surveillance procedure 3-SR-3.6.1.3.10 (B-OUTBD), Primary Containment Local Leak Rate Test Main Steam Line B Outboard: Penetration X-7B, the 3B Outboard Main Steam Isolation Valve (MSIV) [SB] (3-FCV-001-0027) failed to meet the Technical Specification (TS) leak rate limit of 100 standard cubic feet per hour (scfh). On April 7, 2012, at approximately 0233 hours0.0027 days <br />0.0647 hours <br />3.852513e-4 weeks <br />8.86565e-5 months <br /> CDT, during an inspection walkdown, steam was found blowing from the packing on MSIV 3-FCV-001-0027; therefore, April 7, 2012, is considered the event date for this LER.

MSIV 3-FCV-001-0027 was considered to be inoperable for an indeterminate period of time. BFN, Unit 3, TS Limiting Condition for Operation (LCO) 3.6.1.3 requires each primary containment isolation valve, except reactor building-to-suppression chamber vacuum breakers, to be operable in reactor Modes 1, 2, and 3 and when associated instrumentation is required to be operable per LCO 3.3.6.1, "Primary Containment Isolation Instrumentation." With one or more penetration flow paths with MSIV leakage not within limits, Required Action D.1 requires leakage rate to be restored to within limit in 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. If the leakage rate cannot be restored to within limit in 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, Required Actions E.1 and E.2 require the unit to be placed in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in Mode 4 in 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Also, TS LCO 3.0.4 prohibits Mode changes when a LCO is not met except under certain conditions that were not applicable to this event.

Since MSIV 3-FCV-001-0027 failed to meet the TS leak rate limit and no specific time of failure was determined, it is probable that BFN, Unit 3, operated longer with an inoperable MSIV than allowed by the TS. In addition, due to MSIV 3-FCV-001-0027 failing to meet the leak rate limit and that no specific time of failure was determined, it is probable TS LCO 3.0.4 was not met for each applicable Mode change since the last recorded as-found MSIV 3-FCV-001-0027 leak rate test on March 28, 2010, when the leak rate was below 100 scfh.

B. Inoperable Structures, Components, or Systems that Contributed to the Event MSIV 3-FCV-001-0027 failed the as-found local leak rate test (LLRT).

C. Dates and Approximate Times of Major Occurrences November 29, 1995 Packing was installed on MSIV 3-FCV-001-0027.

March 20, 2006 A steam leak on MSIV 3-FCV-001-0027 was repaired by a re-torque without replacing any packing rings.

March 28, 2010 Recorded MSIV 3-FCV-001-0027 as-found leak rate of 0.0 scfh which was below the required TS limit of 100 scfh.

April 7, 2012, at 0233 hours0.0027 days <br />0.0647 hours <br />3.852513e-4 weeks <br />8.86565e-5 months <br /> CDT During an inspection walkdown, steam was found blowing from the packing on MSIV 3-FCV-001-0027.

April 8, 2012, at 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br /> CDT During the performance of surveillance procedure 3-SR-3.6.1.3.10 (B-OUTBD), recorded MSIV 3-FCV-001-0027 as-found leak rate of 781.09 which was above the required TS limit of 100 scfh.

April 29, 2012 MSIV 3-FCV-001-0027 was repacked and leak rate tested satisfactorily. Recorded as-left combined leak rate for "B" MSIVs was 11.4377 scfh.

D. Other Systems or Secondary Functions Affected

There were no other systems or secondary functions affected by this event.

E. Method of Discovery

This event was discovered during an inspection walkdown. It was determined that the resulting MSIV leak rate exceeded the required TS limits during the performance of surveillance procedure 3-SR-3.6.1.3.10 (B-OUTBD).

F. Operator Actions

There were no operator actions for this event.

G. Safety System Responses

There were no safety system responses for this event.

III. CAUSE OF THE EVENT

A. Immediate Cause

The immediate cause of the event was inadequate packing on MSIV 3-FCV-001-0027.

B. Root Cause

The cause of the event was an inadequate packing program at BFN. The current BFN implementing procedures are insufficient for maintaining valve packing to prevent packing failure.

C. Contributing Factors

There were no contributing factors for this event.

IV. ANALYSIS OF THE EVENT

The Tennessee Valley Authority (TVA) is submitting this report in accordance with 10 CFR 50.73(a)(2)(i)(B), any operation or condition prohibited by Technical Specifications.

On April 7, 2012, at approximately 0233 hours0.0027 days <br />0.0647 hours <br />3.852513e-4 weeks <br />8.86565e-5 months <br /> CDT, during an inspection walkdown, steam was found blowing from the packing on MSIV 3-FCV-001-0027.

On April 8, 2012, at approximately 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br /> CDT, during the performance of surveillance procedure 3-SR-3.6.1.3.10 (B-OUTBD), MSIV 3-FCV-001-0027 failed to meet the TS leak rate limit of 100 scfh representing a non-conformance with the valve's containment isolation function. The as-found leak rate was 781.09 scfh. MSIV 3-FCV-001-0027 did not have recent maintenance performed that could have contributed to the packing leak. It was determined, over time, that the packing preload is lost due to packing relaxation and that the current valve packing program does not give adequate guidance on when to reconsolidate and re-torque the valve packing or when to repack the valve. Therefore, the valve packing program was determined to be inadequate.

Extent of Condition The extent of condition applies to any valve that could result in a steam leak due to a degraded packing. The extent of condition will be addressed by identifying this population of valves and incorporating them into a new BFN valve packing program.

V. ASSESSMENT OF SAFETY CONSEQUENCES

The as-found leak rate for the MSIV 3-FCV-001-0027 was 781.09 scfh measured with 14 psig in the test volume and a water block on the inboard valve. The leak rate at the required full test pressure of 26 psig would have been higher. The leakage was noted as coming out of the packing of the MSIV 3-FCV-001-0027. The packing was re-torqued and the LLRT re-performed with the steam lines flooded. As a result, the leak rate was reduced to 241.8895 scfh with full test pressure in the test volume. When the steam lines were drained, the combined leakage for the "B" MSIVs (3-FCV-001-0026 and 3-FCV-001-0027) was 247.7594 scfh. Thus, the calculated leak rate for the 3-FCV-001-0026, "B" inboard MSIV, was determined to be 5.8699 scfh.

The minimum pathway leakage from the "B" main steam line was equal to 5.8699 scfh with the total MSIV minimum pathway leakage determined to be 11.1406 scfh, which is well within the design basis leakage of 150 scfh for all MSIVs (assumed in accident analysis). With one MSIV inoperable in a main steam line (i.e., 3-FCV-001-0027), the remaining operable MSIV in the main steam line (i.e., 3-FCV-001-0026) is capable of performing the main steam line isolation safety function. A review of operations logs for the time period between March 28, 2010, and April 7, 2012 (i.e., the date of entry into Mode 4 at the start of the BFN, Unit 3, refueling outage 15) indicated that the "B" inboard MSIV was operable and capable of maintaining MSIV leakage within limits whenever BFN, Unit 3, was in Mode 1, 2, or 3, during this time period. As a result, there was no loss of the main steam line isolation safety function during this time period.

Therefore, WA concluded that there was no significant reduction to the health and safety of the public for this event.

VI. CORRECTIVE ACTIONS - The corrective actions are being managed by TVA's corrective action program.

A. Immediate Corrective Actions

MSIV 3-FCV-001-0027 was repacked and applicable leak rate testing was performed satisfactorily.

B. Corrective Actions

Implement a new valve packing program at BFN.

VII. ADDITIONAL INFORMATION

A. Failed Components

The failed component was MSIV 3-FCV-001-0027. This component was manufactured by Atwood & Morrill Co., Inc. with a manufacturer model number of 20851-H-26.

B. Previous Similar Events

On December 9, 2011, during an initial drywell entry, BFN Unit 1 Recirculation Pump "B" Discharge Flow Control Valve, 1-FCV-068-0079, was discovered to have a packing leak. This event was identified in problem evaluation report (PER) 473637.

The cause of this leak was determined to be an inadequate packing program at BFN.

C. Additional Information

The corrective action document for this report is PER 533052.

D. Safety System Functional Failure Consideration

In accordance with NEI 99-02, this condition is not considered a safety system functional failure.

E. Scram With Complications Consideration

This condition did not include a scram.

VIII. COMMITMENTS

There are no commitments.