05000275/FIN-2016301-01
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Finding | |
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Title | Insufficient Procedural Direction Contained Within Procedure EOP E-2, Faulted Steam Generator Isolation |
Description | The examiners identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings. Specifically, Procedure EOP E-2, Faulted Steam Generator Isolation, does not contain sufficient procedural direction for isolating auxiliary feedwater flow to a faulted steam generator in the event that auxiliary feedwater control valves cannot be closed from the control room. Procedure EOP E-2, Appendix HH, Isolated Faulted Steam Generator, Step 1.d, and its associated column, Response Not Obtained, does not ensure that a faulted steam generator would remain isolated under all conditions. The Response Not Obtained column permits operators to either locally close auxiliary feedwater control valves OR secure the auxiliary feedwater pump feeding the faulted steam generator. However, due to the absence of pull-to-lock or hard stop switches for the auxiliary feedwater pumps, the possibility exists for an automatic restart of an auxiliary feedwater pump and a re-initiation of feedwater to a faulted steam generator. The failure to ensure that Procedure EOP E-2 contained sufficient direction to isolate a faulted steam generator when auxiliary feedwater flow control valves cannot be closed from the control room was a performance deficiency. This performance deficiency was of more than minor safety significance because it was associated with the procedure quality attribute of the Barrier Integrity cornerstone (reactor coolant system and containment) and adversely affected the cornerstone objective of providing reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, the re-initiation of feedwater to an isolated, faulted steam generator has the potential to adversely affect the reactor coolant system barrier by causing an additional unintended cooldown of the reactor coolant system, increased potential for pressurized thermal shock, and thermal stress to the steam generator u-tubes. Additionally, the containment barrier would be affected by the reinitiation of feedwater to a steam line break within containment. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the team determined that the finding required a detailed risk evaluation due to the potential to affect the reactor coolant system boundary. A senior reactor analyst performed a bounding detailed risk evaluation and estimated the maximum increase in core damage frequency to be 5.9E-8/year, and therefore the finding was determined to be of very low safety significance (Green). This increase in core damage frequency was mitigated by the low probability of multiple equipment failures in the auxiliary feedwater system when combined with the low initiating event frequency of a faulted steam generator. Because the violation was of very low safety significance (Green) and the issue was entered into the licensees corrective action program as Notification 50847218, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the Enforcement Policy: NCV 05000275/2016301;05000323/2016301-01, Insufficient Procedural Direction Contained Within E-2, Faulted Steam Generator Isolation. This finding has a crosscutting aspect in the area of human performance associated with resources because the organization did not ensure procedures are available and adequate to support nuclear safety (H.1). |
Site: | Diablo Canyon |
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Report | IR 05000275/2016301 Section 4OA5 |
Date counted | Jun 30, 2016 (2016Q2) |
Type: | NCV: Green |
cornerstone | Barrier Integrity |
Identified by: | NRC identified |
Inspection Procedure: | |
Inspectors (proximate) | B Larson C Cowdrey D Deese M Bloodgood M Kennard T Farina V Gaddy |
Violation of: | 10 CFR 50 Appendix B Criterion V |
CCA | H.1, Resources |
INPO aspect | LA.1 |
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Finding - Diablo Canyon - IR 05000275/2016301 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Diablo Canyon) @ 2016Q2
Self-Identified List (Diablo Canyon)
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