05000275/FIN-2008005-03
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Finding | |
|---|---|
| Title | Operation of 230 kV Offsite Power System Outside the Design Basis |
| Description | The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B, Criteria III, Design Control, after Pacific Gas and Electric failed to adequately translate the design basis for the 230 kV preferred offsite power system into specifications and procedures. Between November 3 and 7, 2008, the licensee operated with both units aligned to a single startup transformer. This created a situation where a dual unit trip or trip on one unit and accident on the other unit could result in loss of the preferred immediate offsite power source offsite power to both units. The finding is greater than minor because the Mitigating Systems Cornerstone design control attribute and objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences was affected. The inspectors used Inspection Manual Chapter 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, to analyze the significance of this finding. The inspectors concluded that the finding is a design deficiency that did result in loss of operability. However, the inspectors concluded the finding is of very low safety significance because the actual loss of safety function of the 230 kV offsite power system was less than the Technical Specification allowed outage time. The inspectors also concluded that the finding did not represent a loss of safety function for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The inspectors determined that this finding had a crosscutting aspect in the area of problem identification and resolution associated with the corrective action program component because Pacific Gas and Electric did not thoroughly evaluate the operability of the offsite power circuit prior to removing the Unit 2 startup transformer from service P.1(c). (Section 4OA2.5.2 |
| Site: | Diablo Canyon |
|---|---|
| Report | IR 05000275/2008005 Section 4OA2 |
| Date counted | Dec 31, 2008 (2008Q4) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71152 |
| Inspectors (proximate) | L Ricketson G Guerra M Brown M Peck P Elkmann V Gaddy M Runyan R Kellar A Fairbanks |
| CCA | P.2, Evaluation |
| INPO aspect | PI.2 |
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Finding - Diablo Canyon - IR 05000275/2008005 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Diablo Canyon) @ 2008Q4
Self-Identified List (Diablo Canyon)
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