05000265/LER-2003-005, Regarding Technical Specification Allowable Value Exceeded for Main Steam Flow Switches Due to Inadequate Drift Allowance Used in Setpoint Calculation

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Regarding Technical Specification Allowable Value Exceeded for Main Steam Flow Switches Due to Inadequate Drift Allowance Used in Setpoint Calculation
ML032671132
Person / Time
Site: Quad Cities 
Issue date: 09/15/2003
From: Tulon T
Exelon Nuclear
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
SVP-03-103 LER 03-005-00
Download: ML032671132 (4)


LER-2003-005, Regarding Technical Specification Allowable Value Exceeded for Main Steam Flow Switches Due to Inadequate Drift Allowance Used in Setpoint Calculation
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2652003005R00 - NRC Website

text

Exelon(

Exelon Generation Company, LLC Quad Cities Nuclear Power Station 22710 206'h Avenue North Cordova, IL 61242-9740 www.exeloncorp.com Nuclear September 15,2003 SVP-03-103 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Quad Cities Nuclear Power Station, Unit 2 Facility Operating License No. DPR-30 NRC Docket No. 50-265

Subject:

Licensee Event Report 265/03-005, "Technical Specification Allowable Value Exceeded for Main Steam Flow Switches due to Inadequate Drift Allowance used in Setpoint Calculation" Enclosed is Licensee Event Report (LER) 265/03-005, "Technical Specification Allowable Value Exceeded for Main Steam Flow Switches due to Inadequate Drift Allowance used in Setpoint Calculation,' for Quad Cities Nuclear Power Station, Unit 2.

This report is submitted in accordance with the requirements of the Code of Federal Regulations, Title 10, Part 50.73(a)(2)(i)(B), which requires reporting of any operation or condition which was prohibited by the plant's Technical Specifications.

Should you have any questions concerning this report, please contact Mr. W. J. Beck at (309) 227-2800.

Respectfully, Quad Cities Nuclear Power Station cc:

Regional Administrator - NRC Region IlIl NRC Senior Resident Inspector - Quad Cities Nuclear Power Station

Abstract

On July 17, 2003, at 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br />, during performance of the Unit 2 Division II Main Steam Line High Flow Switch Calibration and Functional Test, two main steam flow instruments were determined to have as-found setpoints that exceeded the Technical Specification (TS) Allowable Value.

The instruments were calibrated to be within the TS allowable range. A total of 16 switches, four per steam line, are installed on the Unit 2 Main Steam Lines. The switches feed into the Primary Containment Isolation System, with 'one out of two twice' logic.

The root cause of this event was the use of inadequate drift allowance in the associated setpoint calculation.

The safety significance of this event was minimal. The instruments would have provided the trip signal within the analytical values assumed in the accident analysis.

Corrective actions include a drift analysis and replacement of the instruments with an improved model.U.S. NUCLEAR REGULATORY COMMISSION (7-2001)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER (2)

ER NUMBER (6 PAGE (3)

YEAR SEQUENTIALI REVISION Quad Cities Nuclear Power Station Unit 2 05000265 NUMBER NUMBER 2003 005 00 2of3 (If more space Is required, use addiftonal copies of NRC Form 366A)(17)

PLANT AND SYSTEM IDENTIFICATION

General Electric - Boiling Water Reactor, 2957 Megawatts Thermal Rated Core Power Energy Industry Identification System (EIIS) codes are identified in the text as [XX].

EVENT IDENTIFICATION Technical Specification Allowable Value Exceeded for Main Steam Flow Switches due to Inadequate Drift Allowance used in Setpoint Calculation A.

CONDITION PRIOR TO EVENT

Unit: 2 Event Date: July 17, 2003 Event Time: 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br /> Reactor Mode: 1 Mode Name: Power Operation Power Level: 085%

Power Operation (1) - Mode switch in the RUN position with average reactor coolant temperature at any temperature.

B.

DESCRIPTION OF EVENT

On July 17, 2003, at 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br />, during performance of the Unit 2 Division II Main Steam Line High Flow Switch Calibration and Functional Test, two main steam (SB]

flow instruments [PS] were determined to have as-found setpoints that exceeded the Technical Specification (TS) Allowable Value.

The instruments were calibrated to be within the TS allowable range.

A total of 16 switches, four per steam line, are installed on the Unit 2 main steam lines. The switches feed into the Primary Containment Isolation System [JM], with "one out of two twice, logic.

C.

CAUSE OF EVENT

The root cause of this event was the use of inadequate drift allowance in engineering setpoint calculations.

The main steam flow switches were installed in February 2002.

Because the main steam flow switches were newly installed at the time the setpoint calculations were performed, there was no historical drift data available.

Therefore, the Technical Specification allowable value was calculated using the applicable calibration uncertainty values provided by the manufacturer along with an assumed drift term in accordance with procedural guidance. Based on the historical data that is now available, the drift that has been experienced exceeds the values assumed.

D.

SAFETY ANALYSIS

The safety significance of this event was minimal. Although the instruments were found to have setpoints outside the TS allowable values, the instruments would have provided the trip signal within the analytical values assumed in the accident analysis. Therefore, the safety function would have been met.

This event is beingU.S. NUCLEAR REGULATORY COMMISSION (7-2001)

LICENSEE EVENT REPORT (LER)

TEXT CONNUATION FACILITY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL I REVISION Quad Cities Nuclear Power Station Unit 2 05000265 I NUMBER NUMBER 2003 005 00 3 of 3 (If more space Is required, use additional copies of NRC Form 366A)(17) reported as operation prohibited by TS due to the fact that multiple instruments were found out of calibration during the same surveillance, providing sufficient evidence that the situation existed longer than allowed by TS.

E.

CORRECTIVE ACTIONS

Immediate Actions The main steam flow switches were recalibrated.

Corrective Actions to be Completed A drift analysis will be performed for the Unit I and Unit 2 main steam flow switches and current calibration frequencies will be evaluated.

Additional actions will be taken as appropriate based on this evaluation.

The Unit 1 and Unit 2 Barton main steam flow switches will be replaced with differential pressure transmitters.

F.

PREVIOUS OCCURREINES No instances of multiple main steam flow switches being outside of the Technical Specification Allowable Value were identified in the last two years.

However, there was one instance (not reportable) of a single main steam flow switch on Unit 1 where the as-found setpoint exceeded the Technical Specification Allowable Value.

G.

COMPONENT FAILURE DATA

The main steam flow switches are Barton Model 288A Differential Pressure Indicating Switches, with a setting range of 0 to 400 paid.