12-12-2005 | On July 25, 2005, with Unit 2 at approximately 100 percent power, Dresden Nuclear Power Station discovered during a vendor inspection of a Unit 2 Main Steam Target Rock Safety/RelietValve, that the valve's second stage disc and seat had steam cutting. This valve had been removed from Unit 2 service in November 2004 and subsequently did not pass its setpoint test on February 17, 2005. The valve lifted at approximately 1091 pounds per square inch gage which is lower than specified in Technical Specification 3.4.3, "Safety and Relief Valves," Allowed Value of 1135 pounds per square inch gage, plus or minus 11.4 pounds per square inch gage. The discovery of the steam , cutting of the valve's second stage disc and seat provided sufficient evidence for Dresden Nuclear Power StOon to conclude that the valve's setpoint did not meet its Technical Specification requirements while it was installed in the plant during 2004.
The apparent cause of the Target Rock Safety/Relief Valve low setpoint and steam cutting of its second stage disc and seat, was most likely caused by foreign Material (e.g., rust, crud) lodged between the valve's , , second stage seat and disc that was introduced into the valVe during in-plant testing with Reactor Coolant System steam in November 2003. A corrective action was previously implemented in November 2004 to eliminate the requirement for in-plant testing with Reactor Coolant System steam.
NRC FORM 366 (6-2004) PRINTED ON RECYCLED PAPER |
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Dresden Nuclear Power Station (DNPS) Unit 2 is a General Electric Company Boiling Water Reactor with a licensed maximum power level of 2957 megawatts thermal. The Energy Industry Identification System codes used in the text are identified as [XX].
A.� Plant Conditions Prior to Event:
Unit: 02� Event Date: 07-25-2005 Reactor Mode: 1� Mode Name: Power Operation Power Level: 100 percent Reactor Coolant System Pressure: 1000 psig
B. Description of Event:
On July 25, 2005, with Unit 2 at approximately 100 percent power, Dresden Nuclear Power Station (DNPS) discovered during a vendor disassembly inspection of a Unit 2 Main Steam Target Rock Safety/Relief Valve (S/RV) [V] that the valve's second stage disc and seat had steam cutting. This valve had been removed from Unit 2 in November 2004 and subsequently did not pass its setpoint test on February 17, 2005. The valve lifted at approximately 1091 pounds per square inch gage (psig) which is lower than specified in Technical Specification (TS) 3.4.3, "Safety and Relief Valves," Allowed Value of 1135 psig, plus or minus 11.4 psig.
This event is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B), "Any operation or condition which was prohibited by the plant's Technical Specifications." DNPS determined that the apparent cause of the February 17, 2005 setpoint test results indicated that the low setpoint condition existed while the valve was installed in Unit 2 and that the valve did not meet its TS requirements while it was installed in the plant during 2004.
C. Cause of Event:
The apparent cause of the Target Rock S/RV low setpoint and steam cutting of its second stage disc and seat, was most likely foreign material (e.g., rust, crud) lodged between the valve's second stage seat and disc that was introduced into the valve during in-plant testing' with Reactor Coolant System (RCS) steam in November 2003.
The Target Rock S/RV provides a dual' function. The S/RV can actuate in the safety mode or the relief mode. In the safety mode (i.e., when actuated by system presSure), the S/RV opens when the inlet steam pressure reaches a set lift pressure. In the relief mode (i.e., power actuated mode of operation), automatic or manual switch actuation energizes a solenoid valve that admits air to the air operator diaphragm and strokes the plunger which strokes the second stage disc that is located within the main disc body. Actuation of the plunger i allows pressure to be vented from the top of the main valve piston creating a differential pressure (d/p) across the main piston. This allows reactor system pressure to lift the main valve piston, which opens the main valve.
The Target Rock S/RV was initially tested and the setpoint verified at a vendor's shop with clean dry steam prior to being installed in Unit 2. The initial test records indicated that no valve seat leakage was identified. After the valve was installed in Unit 2 in November 2003, the valve was in-plant tested with RCS steam in accordance with TS Surveillance Requirements 3.4.3-2, 3.5.1-6 and 3.6.1.6-2.
The valve's tail pipe temperature was identified as being higher than normal during subsequent plant operation. A high tail pipe temperature is an indication that one or more of the valve's three stage seats (i.e., main stage seat, second stage seat and pilot valve seat) are leaking. A leaking main stage seat has little affect on the valve's safety mode setpoint, whereas a leaking second stage seat or pilot valve seat have greater potential to affect the safety mode setpoint.
The S/RV was removed from Unit 2 in November 2004. The S/RV was vendor tested on February 17, 2005 and the as-found setpoint was determined to be 1091 psig which is lower than specified in TS 3.4.3 Allowed Value of 1135 psig, plus or minus 11.4 psig. On July 25, 2005, the valve was inspected to obtain additional information to aid in determining the cause of setpoint failure. As part of the inspection, the pilot valve and second stage seat tightness were checked with nitrogen pressure and found to have high leakage. The valve internal components were then removed and inspected. The pilot valve seat and main stage seat generally looked to be in good condition. The second stage disc and seat had steam cutting. During the inspection, no foreign material was found in the second stage disc area due to the erosion that was done to the disc. DNPS concluded that:
- The steam cutting of the second stage seat and disc was the apparent cause of the setpoint test results on February 17, 2005,
- The steam cutting of the valve's second stage disc and seat had occurred during in-plant operation,
- The steam cutting was most likely caused by foreign material (e.g., rust, crud) lodged between the valve's second stage seat and disc that was introduced into the valve during in- plant testing with RCS steam in November 2003, and
- The length of in-plant operation to cause the observed steam cutting and its effect on the valve's setpoint exceeded the 14 day Allowed Outage Time of TS 3.4.3 for this valve.
Additionally, a Unit 3 S/RV that had a test result of 1119 psig in February 2005 was disassembled and inspected in July 2005 and no internal degradation was identified that could have caused the setpoint test results. It was concluded that the condition occurred at the time of discovery and was associated with setpoint drift.
DNPS had previously identified the potential detrimental effect on S/RVs from retesting the valves with RCS steam. On January 15, 2004, DNPS requested a revision to TS Surveillance Requirements 3.4.3-2, 3.5.1-6 and 3.6.1.6-2 that would eliminate the requirement to in-plant test the S/RVs with RCS steam. Thus, eliminating the potential introduction of foreign material (e.g., rust, crud) into the valve from the RCS. The NRC approved DNPS's request for the TS change on October 19. 2004.
DNPS implemented the TS change in November 2004.
In addition to the above event, the Target Rock S/RV's at DNPS have experienced additional testing issues. These issues occurred when the valves were subjected to the plus or minus 3 percent testing requirements of Section XI of the American Society of Mechanical Engineers Code. Since January 2000, three S/RVs from Units 2 and 3 have had test results ranging from 1116 psig to 1131 psig that were within the plus or minus 3 percent testing requirement and were attributed to setpoint drift. Also, in May 2004, a Target Rock S/RV had a test result of 1094 psig that was attributed to a groove in its bellows cap, which reduced the preload on the spring force.
Similarly, during the DNPS Unit 3 refueling outage in November 2004, four safety valves were removed from service and tested. The safety valves are Dresser valves, model number 3777QA.
One valve lifted outside the requirements of TS 3.4.3. The valve lifted 1.5 % low at 1231 psig instead of its setpoint of 1250 psig. An inspection of the valve did not identify any firm evidence for the low test results. It was concluded that the condition occurred at the time of discovery and was associated with setpoint drift.
D. Safety Analysis:
The safety significance of the event is minimal. The S/RV can actuate in the safety mode or the relief mode. The valve's safety mode function is to automatically actuate to prevent the over pressurization of the RCS. The steam cutting of the second stage seat and disc lowered the valve's setpoint. Thus, the steam cutting would not have prevented the valve from meeting its safety mode function of preventing RCS over pressurization. Additionally, the steam cutting did not lower the valve's setpoint significantly to cause a spurious actuation of the valve at normal RCS pressure. The steam cutting did not affect the relief mode of the S/RV. Therefore, the consequences of this event had minimal impact on the health and safety of the public and reactor safety.
E. Corrective Actions:
On January 15, 2004, DNPS requested a revision to TS Surveillance Requirements 3.4.3-2, 3.5.1-6 and 3.6.1.6-2 that would eliminate the requirement to retest the S/RVs with RCS steam. The NRC approved DNPS's request for the TS change on October 19. 2004. DNPS implemented the TS change in November 2004.
DNPS replaced the Target Rock S/RV in December 2004.
F. Previous Occurrences:
A review of DNPS Licensee Event Reports (LERs) for the last three years did not identify any similar events with the Target Rock S/RVs.
G. Component Failure Data:
Target Rock S/RV Model 67F
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05000328/LER-2005-001 | Unit 2 Reactor Trip Following Closure of Main Feedwater Upon Inadvertent Opening of Control Breakers | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000388/LER-2005-001 | DDegradation of Primary Coolant Pressure Boundary due to Recirculation Pump Discharge Valve Bonnet Vent Connection Weld Flaw | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000423/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000455/LER-2005-001 | Unit 2 Automatic Reactor Trip Due to Low Steam Generator Level resulting from a Software Fault on the Turbine Control Power Runback Feature | | 05000370/LER-2005-001 | Automatic Actuation of Motor Driven Auxiliary Feedwater Pumps During Outage | | 05000244/LER-2005-001 | Failure of ADFCS Power Supplies Results in Plant Trip | | 05000247/LER-2005-001 | 0Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by an Inoperable Auxiliary Component Cooling Water Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000529/LER-2005-001 | REACTOR HEAD VENT AXIAL INDICATIONS CAUSED BY DEGRADED ALLOY 600 COMPONENT | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000336/LER-2005-001 | | | 05000266/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000269/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000289/LER-2005-001 | | | 05000293/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000298/LER-2005-001 | Reactor Scram due to Reactor Level Transient and Inadvertent Rendering of High Pressure Coolant Injection Inoperable | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000331/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000315/LER-2005-001 | Reactor Trip Following Intermediate Range High Flux Signal | | 05000316/LER-2005-001 | Reactor Trip from RCP Bus Undervoltage Signal Complicated by Diesel Generator Output Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000317/LER-2005-001 | Main Feedwater Isolation Valve Inoperability Due to Handswitch Wiring | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000323/LER-2005-001 | TS 3.4.10 Not Met During Pressurizer Safety Valve Surveillance Testing Due to Random Lift Spread | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000333/LER-2005-001 | Inoperable Offsite Circuit In Excess of Technical Specifications Allowed Out of Service Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000352/LER-2005-001 | Loss Of Licensed Material In The Form Of A Radiation Detector Calibration Source | | 05000353/LER-2005-001 | Core Alterations Performed With Source Range Monitor Alarm Horn Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000362/LER-2005-001 | Emergency Diesel Generator (EDG) 3G003 Declared Inoperable Due to Loose Wiring Connection on Emergency Supply Fan | | 05000263/LER-2005-001 | | | 05000456/LER-2005-001 | Potential Technical Specification (TS) 3.9.4 Violation Due to Imprecise Original TS and TS Bases Wording | | 05000454/LER-2005-001 | Failed Technical Specification Ventilation Surveillance Requirements During Surveillance Requirement 3.0.3 Delay Period | | 05000282/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2005-001 | Plant in a Condition Prohibited by Technical Specifications due to Error Making Control Room Ventilation System Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000400/LER-2005-001 | Reactor Auxiliary Building Emergency Exhaust System Single Failure Vulnerability | | 05000395/LER-2005-001 | Emergency Diesel Generator Start and Load Due To A Loss Of Vital Bus | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2005-001 | RCS Pressure Boundary Leakage Due to Primary Water Stress Corrosion Cracking of a Pressurizer Heater Sleeve | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000305/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2005-001 | Reactor Coolant System Leakage Detection Instrumentation Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2005-002 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000255/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-002 | Missing Taper Pins on CCW Valve Cause Technical Specification Required Shutdown | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000370/LER-2005-002 | Ice Condenser Lower Inlet Door Failed Surveillance Testing | | 05000353/LER-2005-002 | High Pressure Coolant Injection System Inoperable due to a Degraded Control Power Fuse Clip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000263/LER-2005-002 | | | 05000454/LER-2005-002 | One of Two Trains of Hydrogen Recombiners Inoperable Longer Than Allowed by Technical Specifications Due to Inadequate Procedure | | 05000244/LER-2005-002 | Emergency Diesel Generator Start Resulting From Loss of Off-Site Power Circuit 751 | | 05000362/LER-2005-002 | Emergency Containment Cooling Inoperable for Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2005-002 | DTechnical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by Gas Intrusion from a Leaking Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000265/LER-2005-002 | Main Steam Relief Valve Actuator Degradation Due to Failure to Correct Vibration Levels Exceeding Equipment Design Capacities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000286/LER-2005-002 | • Entergy Nuclear Northeast Indian Point Energy Center 450 Broadway, GSB P.O. Box 249Entergy Buchanan. NY 10511-0249 Tel 914 734 6700 Fred Dacimo Site Vice President Administration July 5, 2005 Indian Point Unit No. 3 Docket Nos. 50-286 N L-05-078 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2005-002-00, "Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure." Dear Sir: The attached Licensee Event Report (LER) 2005-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2005-02478. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, 4F-/t R. Dacimo Vice President Indian Point Energy Center Docket No. 50-286 NL-05-078 Page 2 of 2 Attachment: LER-2005-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 3660 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request 50 hours.RReported lessons teamed are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 29555-0001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to Infocoilectsenrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection. 1. FACIUTY NAME 2. DOCKET NUMBER 3. PAGE INDIAN POINT 3 05000-286 10OF06 4. TITLE Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000287/LER-2005-002 | Unit 3 trip with ES actuation due to CRD Modification Deficiencies | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2005-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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