05000220/FIN-2017004-05
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Finding | |
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Title | Licensee-Identified Violation |
Description | The following violation of very low safety significance (Green) was identified by Exelon and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for being dispositioned as a NCV. Title 10 CFR 50.65(a)(4) requires, in part, ...the licensee shall assess and manage the increase in risk that may result from the proposed maintenance activities. Exelon procedure WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 001, Section 4.1.3, states to consider work activities that cause equipment to be unavailable (e.g., trains of systems) for assessment of risk under the requirements of 10 CFR 50.65(a)(4). Contrary to the above, on October 17, 2017, Exelon identified a discrepancy in PARAGON (risk software) that resulted in an improper risk assessment for the days planned work. Review and correction of the error resulted in an elevated risk condition of Yellow during Nine Mile Point Unit 1, 11 feedwater pump (FW) maintenance. This performance deficiency was determined to be more than minor because it adversely affected the human performance attribute of the Mitigating Systems cornerstone and affected cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, on October 17, 2017, Exelon identified a planned activity that resulted in an unplanned Yellow risk activity during planned maintenance of the 11 FW pump. In addition, IMC 0612, Appendix E, Examples of Minor Issues, under Section 7, Maintenance Rule, Example E for inadequate risk assessment states in part that a more-than-minor issue would put the plant into a higher licensee-established risk category. The finding was evaluated using IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process. The finding was determined to affect the overall plant risk with the 11 FW Pump being out of service for maintenance with PARAGON not elevating the overall plant risk from green to yellow. The risk deficit was elevated and determined to not be greater than 1E-6 event per year for Incremental Core Damage Probability Differential and not greater than 1E-7 events per year for Incremental Large Early Release Probability Differential. Therefore, the finding was determined to be of very low safety significance (Green). Exelon entered this issue into its CAP as IR 04064241. |
Site: | Nine Mile Point |
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Report | IR 05000220/2017004 Section 4OA7 |
Date counted | Dec 31, 2017 (2017Q4) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | |
Inspectors (proximate) | M Catts B Sienel P Presby M Patel K Mangan M Hardgrove J Bream F Arner R Rolph G Stock E Miller H Lynn |
Violation of: | 10 CFR 50.65 10 CFR 50.65(a)(4) |
INPO aspect | |
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Finding - Nine Mile Point - IR 05000220/2017004 | ||||||||||||||||||||||||||||||||||||||||||
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Finding List (Nine Mile Point) @ 2017Q4
Self-Identified List (Nine Mile Point)
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