05000410/FIN-2017004-04
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Finding | |
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Title | Ineffective Correction Action Results in Failure of Instrument Air System |
Description | The inspectors documented a self-revealing Green finding (FIN) of CNG-CA-1.01-1000, Corrective Action Program, Revision 01100, because Nine Mile Point Nuclear Station (NMPNS) failed to implement corrective actions at NMPNS Unit 2 to remove and replace all un-annealed red brass piping for the instrument air system during the April 2008 refueling outage. Specifically, on July 13, 2017, Unit 2 experienced a rupture of un-annealed red brass instrument air pipe which resulted in a feedwater pump trip and a reactor recirculation pump runback to 49 percent. Exelons corrective actions for the July 13, 2017 failure of un-annealed red brass instrument air piping included wrapping the instrument air piping with a material that both supports the piping and prevents potential stress corrosion cracking. Exelon has developed work orders to replace the piping in the upcoming outage in spring 2018. Exelon also improved staff training for accountability and work checking to verify that generated work orders are completed and closed out. Exelon entered this issue into the corrective action program (CAP) as issue report (IR) 04031685, and performed a corrective action program evaluation (CAPE). This finding is more than minor because it is associated with the design control attribute of the Initiating Events cornerstone and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during power operations. Specifically, NMPNS staff failed to complete corrective actions to replace Unit 2 un-annealed red brass instrument air piping, which was susceptible to stress corrosion cracking, resulting in a feedwater pump trip and a reactor recirculation runback to 49 percent on July 13, 2017. The inspectors evaluated the finding using IMC 0609, Attachment 4, Initial Characterization of Findings, issued on October 7, 2016, and Exhibit 1 of IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, issued June 19, 2012. The inspectors determined that the finding was of very low safety significance (Green) because it did not result in the complete or partial loss of a support system that contributes to the likelihood of, or cause, an initiating event and affected mitigation equipment. The inspectors determined that this finding did not have a cross-cutting aspect because the performance deficiency occurred greater than 3 years ago; therefore, it is not considered to be indicative of current plant performance. |
Site: | Nine Mile Point |
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Report | IR 05000410/2017004 Section 4OA2 |
Date counted | Dec 31, 2017 (2017Q4) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | M Catts B Sienel P Presby M Patel K Mangan M Hardgrove J Bream F Arner R Rolph G Stock E Miller H Lynn |
INPO aspect | |
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Finding - Nine Mile Point - IR 05000410/2017004 | ||||||||||||||||||||||||||||||||||||||||||
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Finding List (Nine Mile Point) @ 2017Q4
Self-Identified List (Nine Mile Point)
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