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05000483/LER-2022-002, Forward LER 2022-002-00 for Callaway Plant, Unit 1, Containment Spray and Cooling Systems, and a Condition Which Could Have Prevented Fulfillment of the Safety Function of the Containment Spray System (Letter Only)Callaway18 August 2022Forward LER 2022-002-00 for Callaway Plant, Unit 1, Containment Spray and Cooling Systems, and a Condition Which Could Have Prevented Fulfillment of the Safety Function of the Containment Spray System (Letter Only)
05000306/LER-2017-003Prairie Island11 January 2018Both Containment SEa) Pump Control Switches in Pull-out in Mode 4
LER 17-003-00 for Prairie Island Nuclear Generating Plant, Unit 2 Regarding Both Containment Spray Pump Control Switches in Pull-Out in Mode 4

On November 12, 2017 at 2119, a Control Room board walkdown discovered that both of the Unit 2 Containment Spray Pump control switches had been left in pull-out, when operators transitioned Unit 2 from Mode 5 to Mode 4. With the control switches in pull-out, the pumps would not automatically start as required. Technical Specification (Tech Specs) 3.0.3 was entered as a result of not complying with Technical Specification 3.6.5, Containment Spray and Cooling systems, which required both trains of Containment Spray to be Operable while in Mode 4. This event is reportable under 10 CFR 50.73(a)(2)(i)(B), Condition Prohibited by Technical Specification and 10 CFR 50.73(a)(2)(v)(D), Event or Condition that Could Have Prevented Fulfillment of a Safety Function.

The root cause determined that Surveillance Procedure SP 2099, Unit 2 Main Steam Isolation Valve Logic Test, was not adequately designed to account for outage schedule variation. Contributing causes included that the Unit 2 Startup to Mode 4 procedure does not contain adequate process barriers such that plant configuration meets Technical Specification requirements for Mode 4 entry. Operations personnel failed to uphold standards for panel walkdown requirements.

Corrective actions include revising SP 2099, Unit 2 Main Steam Isolation Valve Logic Test to include steps to reposition Containment Spray Switches to the "as found" configuration and revise Unit 2 start-up procedure to add additional HOLD to have the Shift Manager perform Control Board Walkdown to verify equipment required in Mode 4 is aligned and Operable.

Develop and implement an operations improvement plan specifically targeted to improve Operator standards in the performance of Control Board Walkdowns.

05000306/LER-2017-001Prairie Island2 May 2016
29 November 2017
23 Containment Fan Coil Unit Operability
LER 17-001-00 for Prairie Island, Unit 2, Regarding 23 Containment Fan Coil Unit Operability

From May 2, 2016 to May 6, 2016, when B Train 122 Control Room Chiller (CRC) was out-of-service (OOS) per Technical Specifications (Tech Specs) 3.7.11 Condition A, Unit 2 A Train 23 Containment Fan Coil Unit (FCU) was OOS. According to revision 41 of site procedure C18.1, "Engineered Safeguards Equipment Support Systems," Bus 16 load sequencer and Bus 121 were inoperable when 122 CRC was OOS. Bus 121 supports B Train Diesel Driven Cooling Water Pump and Unit 2 B Train containment cooling (22/24 FCUs). So both trains of containment FCUs were OOS at the same time for approximately 35.6 hours. This would have required entry into LCO 3.0.3 putting Unit 2 in MODE 3 within 7 hours, this did not occur. This event is reportable under 10 CFR 50.73(a)(2)(i)(B), Operation or Condition Prohibited by Tech Specs.

The cause was that the Senior Reactor operators failed to utilize Human Performance Tools (Verification/Validation and Procedure Use/Adherence) when assessing the Tech Specs impact to Unit 2 for applying LCO 3.0.6 when 122 CRC was taken OOS.

Corrective actions include independent assessment of shared system LCO's for each unit, revising the LCO database, established a standard for LCO 3.0.6 log entries, and revising the safety function determination program to be more user friendly.

05000390/LER-2017-012Watts Bar23 October 2017Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications
LER 17-012-00 for Watts Bar, Unit 1, Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications

On August 23. 2017. Watts Bar Nuclear Plant (WBN) identified that procedures 1-E-1 and 2-E-1, Loss of Reactor or Secondary Coolant, contained steps to manually open 1-FCV-67-458 in the event of a Train A or B power failure.

Opening 1-FCV-67-458 would result in the crosstie of Essential Raw Cooling Water (ERCW) Headers 2A and 1B, which would lead to providing flow to equipment not operating due to the loss of a train of power. On October 6. 2017.

it was determined that for certain time periods, if a design basis accident had occurred on Unit 2 with a loss of offsite power concurrent with a train failure and with 1-FCV-67-458 opened, inadequate ERCW flow would have been available to remove decay heat after transfer to cold leg recirculation. This condition only affected operability of ERCW Train A. This is reportable as a condition prohibited by Technical Specification 3.7.8.

The issue associated with this incorrect procedural step to cross-tie the ERCW trains in 1-E-1 and 2-E-1 was addressed as part of actions to resolve an ERCW design and procedure issue documented in Licensee Event Report (LER) 390-2017-009. This report, while related, identifies an issue that was not addressed in the prior LER. The cause was determined to be the incorrect application of a cross tie requirement associated with 10 CFR 50 Appendix R. Corrective action will be to include engineering in the review of procedures affected by complex design changes.

NRC FORM 355 ;:;4-217' APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001. or by e-mail to NEOB-10202. (3150-0104), Office of Management and Budget. Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number. the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

05000247/LER-2015-001Indian Point11 August 2015
29 August 2017
Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for Containment
LER 15-001-02 for Indian Point, Unit 2, Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for Containment

On August 11, 2015, during operator investigations inside the reactor containment building, a through wall leak was discovered on the 24 Fan Cooler Unit (FCU) motor cooler service water (SW) return line. The leak was in a 2 inch copper-nickel pipe near a brazed joint upstream of containment penetration SS. The leak was located within the ASME Section XI Code ISI Class 3 boundary and estimated to be approximately 2 gpm.

Since the pipe flaw was through wall and was located within the ASME Section XI boundary, it exceeds the flaw allowable limits provided per IWC-3000.

The weld leak was evaluated and determined to meet the structural requirements of ASME Code Case N-513-3.

The condition was determined to have no impact on SW cooling safety function or adverse impact on piping structural integrity. The pipe is considered a closed loop system inside containment and required to meet containment integrity.

An engineering evaluation was performed to determine the potential air leakage out of containment based on the observed SW leakage into containment.

This evaluation concluded that the leaking defect could result in post-LOCA air leakage out of containment in excess of that allowed by Technical Specification 3.6.1 (Containment) which requires leakage rates to comply with 10 CFR 50, Appendix J.

The direct cause was corrosion. The apparent cause was the length of time to implement a modification to replace the FCU motor cooler copper-nickel piping identified in 2009 per the SW mitigation strategy.

An engineered clamp was installed over the pipe defect. The pipe and affected elbow were replaced in accordance with the requirements of ASME Section XI Code during the spring refueling outage in 2016. A modification to replace piping will be processed for funding. The event had no significant effect on public health and safety.

05000416/LER-2017-006Grand Gulf29 August 2017Completion of Grand Gulf Nuclear Station Shutdown Required By Technical Specifications Because Of An Inoperable A Residual Heat Removal Pump

On August 22, 2017 at 2321 hours central daylight time, Grand Gulf Nuclear Station entered Technical Specification (TS) conditions for three Limiting Condition for Operations (LCOs) not met due to Residual Heat Removal 'A' (RHR A) being declared inoperable. Entergy Operations Inc. (Entergy) made the decision to shut down the plant based on the results of troubleshooting performed on the RHR A pump. The A RHR pump TS differential pressure was out of specification (low) and could not be returned to acceptable limits.

Grand Gulf Nuclear Station initiated plant shutdown required by Technical Specifications 3.5.1, 3.6.1.7, and 3.6.2.3 at 1200 hours CDT on August 29, 2017, due to expected restoration of RHR A exceeding the completion time of 7 days prior to restoring Operability. The shutdown was completed and entry into MODE 3 occurred at 2217 hours CDT on August 29, 2017. The cause is under investigation and this LER will be supplemented upon completion of the causal analysis. Corrective Actions included the replacement of the A RHR pump and the successful retesting of the. A RHR pump and restoration of the pump to operable status. This condition is reportable as a completion of a plant shutdown required by the TS.

(4-2017) 366A U.S. NUCLEAR REGULATORY COMMISSION

CONTINUATION SHEET

(See NUREG-1022, R.3 for instruction and guidance for completing this form htio://www.nrcoovireadino-rm/dcc-collectionenureosistafffsr1022;r31 APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/31/2020 Reported lessons learned are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

Grand Gulf Nuclear Station, Unit 1 05000 416

3. LER NUMBER

Description On August 22, 2017 at 2321 hours central daylight time (CDT), Grand Gulf Nuclear Station entered Technical Specification (TS) conditions for three Limiting Condition for Operations (LCOs) not met due to Residual Heat Removal (BO) 'A' (RHR A) being declared inoperable.

LCOs not met:

1) TS 3.5.1 for one low pressure ECCS injection/spray subsystem.

2) TS 3.6.1.7 for one RHR containment spray subsystem, and 3) TS 3.6.2.3 for one RHR suppression pool cooling subsystem.

Entergy Operations Inc. (Entergy) made the decision to shut down the plant based on the results of troubleshooting performed on the RHR A pump. Grand Gulf Nuclear Station initiated plant shutdown required by Technical Specifications 3.5.1, 3.6.1.7, and 3.6.2.3 at 1200 hours CDT on August 29, 2017, due to expected restoration of RHR A exceeding the TS completion time of 7 days prior to restoring Operability. The shutdown was completed and entry into MODE 3 occurred at 2217 hours CDT on August 29, 2017.

REPORTABILITY

Entergy completed Event Notification 52936 notifying the Nuclear Regulatory Commission of the commencement of a plant shutdown in accordance with 10CFR50.72(b)(2)(i), due to the anticipated inability to complete the required A RHR Pump repairs prior to exceeding the TS LCO time limits.

The completion of the shutdown reported in Event Notification 52936 is reportable in accordance with 10CFR50.73(a)(2)(i)(A), the completion of any nuclear plant shutdown required by the plant's Technical Specifications. LCOs not met:

1) TS 3.5.1 for one low pressure ECCS (BO) injection/spray subsystem.

2) TS 3.6.1.7 for one RHR containment spray subsystem, and 3) TS 3.6.2.3 for one RHR suppression pool cooling subsystem.

CAUSE

The A RHR pump TS differential pressure was out of specification (low) and could not be returned to acceptable limits prior to exceeding the 7 day limiting condition for operation time.

The A RHR pump was shipped to a vendor for the determination of the cause of the A RHR pump being out of specification limits. This causal analysis is not anticipated to be completed prior to the 60 day report time for this licensee event report (LER). This LER will be supplemented upon completion of the causal analysis.

CORRECTIVE ACTIONS

Replacement of the A RHR pump.

Successful retesting of the A RHR pump and restoration of the pump to operable status.

NRC FORM

(4-2017) 366A U.S. NUCLEAR REGULATORY COMMISSION

CONTINUATION SHEET

(See NUREG-1022, R.3 for instruction and guidance for competing thIs.form httplAvww.nrc.dovireadino-rm(doc-coRectionsinurectsistaff/sr1022/r3/) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/31/2020 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information colIection does not display a currently valid OMB con:rol number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

05000 416

SAFETY SIGNIFICANCE

The event posed no threat to the health and safety of the general public or to nuclear safety as safety-systems performed as designed. No Technical Specification safety limits were violated.

Industrial safety was not challenged, and there was no potential or actual radiological release during the event.

PREVIOUS SIMILAR OCCURRENCES

Removal Pump The causes and corrective actions associated with these previous similar events was reviewed and it is believed that the corrective actions could not have prevented the cause of this event.

05000528/LER-2017-001Palo Verde
Palo Verde Nuclear Generating Station Unit 1
11 April 2017
14 June 2017
Essential Chiller B Inoperable Due to Refrigerant Leak Resulting in Safety System Functional Failure
LER 17-001-00 for Palo Verde Nuclear Generating Station, Unit 1 Regarding Essential Chiller B Inoperable Due to Refrigerant Leak Resulting in Safety System Functional Failure

On April 17. 2017, the staff identified a low refrigerant level in the Unit 1 train B essential chilled water (EC) system chiller during inspection. Operations personnel immediately declared EC chiller train B inoperable. On April 17, 2017, the leak was corrected and EC chiller train B was refilled with refrigerant to within the manufacturer's specifications. Operations personnel declared the system operable on April 18, 2017. The chiller had been inoperable since April 11. 2017, when the automatic purge system was placed into service. The direct cause of the low refrigerant level was leakage due to prior installation of a fitting on the automatic purge system filter without a plug.

During the 7-day period that EC chiller train B was inoperable, the supported low pressure safety injection (LPSI) system train B was inoperable. LPSI train A was also inoperable for approximately 17 minutes on April 13, 2017, during the performance of a routine surveillance test. This 17-minute period represented a condition that could have prevented the fulfillment of a safety function.

The cause of the leak was determined to be ineffective work instructions that did not identify the appropriate part number to be used during filter replacement. Corrective actions include revision of the work instructions. This change will ensure that the existing plug remains in place during filter element replacement. A leak test was also added to the work instructions to verify that no refrigerant leaks are present following maintenance.

05000311/LER-2017-001Salem13 June 2017Emergency Diesel Generator Start Due to a Loss of Power to the 2C 4160 Volt Vital Bus
LER 17-001-00 for Salem, Unit 2, Regarding Emergency Diesel Generator Start Due to a Loss of Power to the 2C 4160 Volt Vital Bus

On April 14, 2017 at 13:57 while attempting to transfer the 2C 4 Kilovolt (kV) vital bus from 24 Station Power Transformer (SPT) to 23 SPT, the 24 SPT infeed breaker opened properly but 23 SPT infeed breaker failed to close.

The 23 SPT infeed breaker failing to close as expected resulted in de-energization of the 2C 4kV vital bus and subsequent start and loading of the 2C Emergency Diesel Generator (EDG) to power the bus.

This report is being made in accordance with 10CFR50.73 (a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B)," for this event actuation of the 2C EDG.

Notification of this event was provided via ENS report 52681 NS'C, FORM 366 I04-20

  • 17:1
05000316/LER-2017-001Cook23 March 2017
19 May 2017
1 OF 5
LER 17-001-00 for Cook, Unit 2 re Containment Hydrogen Skimmer Ventilation Fan #1 Inoperable Longer than Allowed by Technical Specifications

On March 23, 2017, at 0941, Eastern Daylight Time (EDT), with Unit 2 in Mode 1 at 100% power, the Unit 2 Containment CEQ Fan #1 Backdraft Damper opening force exceeded the Technical Specification (TS) Surveillance Requirement (SR) limit.

Maintenance was performed on the damper and operability of the Unit 2 CEQ Fan #1 was restored at 1724 EDT. A past operability evaluation was performed and determined that the condition likely existed since maintenance was performed to lubricate the damper on February 24, 2017. As a result, the Unit 2 CEQ Fan #1 was inoperable longer than allowed by TS. During this time, the Unit 2 CEQ Fan #2 was declared inoperable to perform surveillance testing on March 2, 2017, from 0938 Eastern Standard Time (EST) until 1326 EST. This resulted in both trains being inoperable simultaneously for a short period of time.

The cause of the elevated force required to open the Unit 2 CEQ Fan #1 Backdraft Damper was determined to be that the lubrication Preventive Maintenance (PM) work order instructions were not adequate and did not provide adequate Post-Maintenance Testing (PMT) instruction. Corrective action is to revise model work order tasks to provide additional details and appropriate PMT. The risk significance of this condition has been determined to not constitute a significant increase in risk.

This event is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v)(D).

05000247/LER-2016-010Indian Point
Docket Number ,
28 February 2017Safety System Functional Failure Due to an Inoperable Containment Caused by a Through Wall Defect in a Service Water Supply Pipe Elbow to the 24, Fan Cooler Unit
LER 16-010-01 for Indian Point 2 Regarding Safety System Functional Failure Due to an Inoperable Containment Caused by a Through Wall Defect in a Service Water Supply Pipe Elbow to the 24 Fan Cooler Unit

On November 21, 2016, as a result of investigating an increased level rise in the Waste Hold-Up. Tank (WHUT), Operators identified a corresponding rise in containment sump level. A containment entry was made to investigate the source of the sump level rise and determined the source was a through wall leak in a Service Water (SW) supply pipe elbow to the 24 Fan Cooler Unit (FCU). The leak constituted a breach of a closed system within containment. Technical Specification (TS) 3.6.1 (Containment) was entered and containment declared inoperable. TS 3.6.6 (Containment Spray and Fan Cooler System) was entered when the 24 FCU was secured and SW to the 24 FCU was isolated. Inspections identified a through wall leak on .a SW supply pipe elbow to one of the 24 FCU water boxes.

The leak is on a 3 inch carbon steel epoxy-lined elbow.

The pipe fitting is in an ASME ISI Code Class 3, nuclear safety related piping system.

The direct cause was failure of the interior coating allowing brackish river water to corrode the carbon steel fitting. The root cause was the maintenance coating procedure requirements for post-coating inspections were inadequate. Key corrective actions included removal of the defective elbow and weld repair, recoating and re-installation.

Maintenance procedure 0-SYS-409-GEN will be revised to mandate detailed inspections and/or testing of surface preparation and applied coatings to ensure proper coverage and adhesion. The event had no effect on public health and safety.

NO:

Indian Point 2 05000-247

05000346/LER-2016-008Davis Besse27 February 2017Application of Technical Specification for the Safety Features Actuation System Instrumentation
LER 16-008-01 for Davis-Besse Nuclear Power Station Unit 1 Regarding Application of Technical Specification for the Safety Features Actuation System Instrumentation

On June 30, 2016, at 0829, with the Davis-Besse Nuclear Power Station in Mode 1 and at approximately 100 percent power, a level transmitter for Safety Features Actuation System (SFAS) Channel 1 was declared inoperable for scheduled maintenance and Technical Specification (TS) Limiting Condition of Operation (LCO) 3.3.5 Condition A was entered. At 2342 hours a power supply in SFAS Channel 2 failed and a separate TS LCO 3.3.5 Condition A was entered. Upon recognition that two channels of SFAS were inoperable, TS LCO 3.3.5 Condition B was entered at 0245 and then exited at 0330 with the use of compensatory actions to restore SFAS Channel 1 operability. After further review, it was determined the compensatory actions could not be credited and TS LCO 3.3.5, Condition B was re- entered at 1325. SFAS Channel 1 was restored and declared operable at 1351 hours.

Causes of the event were the Shift Manager failed to initially recognize that TS LCO Conditions A and B had been met; followed by Station Personnel failing to effectively implement required processes. The root cause was that Station Management failed to recognize that a normalized deviation had occurred that resulted in TS noncompliance. Corrective Actions include specific refresher training to all applicable personnel, revising relevant documents, and developing an event Case Study for training purposes. This condition is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as an operation or condition prohibited by the plant's Technical Specifications.

05000445/LER-2016-002Comanche Peak22 February 2017Unanalyzed Condition Involving Potential Moderate Energy Line Break
LER 16-002-01 for Comanche Peak Nuclear Power Plant, Units 1 & 2 Regarding Unanalyzed Condition Involving Potential Moderate Energy Line Break

On September 13, 2016, and September 14, 2016, during plant walk downs by Engineering and the NRC Senior Resident inspector, pressurized fire protection piping in the Service Water Intake Structure was found to not be shielded against a Moderate Energy Line Break (MELB), resulting in inoperability of one train of Service Water for both units.

During extent of condition walk downs conducted on October 6, 2016, October 10, 2016, November 17, 2016, December 5, 2016, and December 22, 2016, additional piping in the Unit 1 and Unit 2 Safeguards and Auxiliary Buildings was found to not be shielded against a MELB, resulting in inoperability of one train of various.safety related equipment for both units. The most likely cause of this event was the methodology used to conduct the initial MELB walk downs was flawed and allowed some MELB threats to be missed.

Corrective actions include shielding the affected piping, performing a 100 percent walk down of rooms containing MELB piping identified for shielding, and revising the systems interaction program maintenance procedure. I All times in this report are approximate and Central Time unless noted otherwise.

05000400/LER-2016-007Harris26 October 2016
9 February 2017
Containment Spray System Valve Actuation
LER 16-007-01 for Shearon Harris Unit 1, Regarding Containment Spray System Valve Actuation

On October 26, 2016, the Shearon Harris Nuclear Power Plant was in a planned refueling outage. Operations was in the process of restoring the containment spray system following maintenance. During this restoration process, operations started the 'B' containment spray pump with Refueling Water Storage Tank (RWST) level below 23.4 percent. As a result, the logic to initiate containment spray switchover to the containment sump was satisfied, opening the containment sump suction valve, which established a flowpath that allowed water to be transferred from the RWST to the containment sump. Operations secured the 'B' containment spray pump and re-closed the containment sump suction valve to restore the plant to the desired configuration. During the event, the containment spray system was aligned for recirculation of the spray pump discharge back to the RWST, so no water flowed through the spray header.

The primary cause of the event was a procedural deficiency. The procedure did not establish a physical barrier to prevent the containment sump valves from opening in Modes 5, 6 and defueled. The corrective actions include revising the procedure to remove power to the containment sump valves to prevent them from opening in Modes 5, 6 and defueled.

05000286/LER-2016-001Indian Point3 November 2016Safety System Functional Failure Due to an Inoperable Containment Caused by a Flaw on the 31 .Fan Cooler Unit Service Water Return Coil Line Affecting Containment Integrity

On November 3, 2016, as a result of a containment sump pump alarm, operations obtained from Chemistry a sample which indicated a Service Water (SW) leak due to abnormal chlorides levels.

Technical Specification (TS) 3.6.1 (Containment) was entered and containment declared inoperable.

Inspections identified a through wall leak on the 31 SW Fan Cooler Unit (FCU) from FCU coil 3 which - feeds a SW return line header. TS 3.6.6 (Containment Spay and Fan Cooler System) was entered when the 31 FCU was secured and SW to the 31 FCU was isolated. TS 3.6.1, Condition A was exited after the 31 FCU was secured and SW was isolated to the 31 FCU.

The leak is at a 3 inch butt-welded joint that is ISI Class 3, nuclear safety related.

Leak rate estimate was 0.16 gpm. The direct cause was a leak in a SW pipe due to a through-wall flaw as a result of corrosion.

The root cause is indeterminate. The specific. cause for the pipe joint defect requires the component to be removed and a metallurgical failure analysis performed. Corrective actions included installation of a leak limiting clamp. The clamp is being monitored daily and UT monitoring will be performed every 90 days until the pipe is repaired. The pipe will be replaced in the next refueling outage in 2017.

The affected pipe will be analyzed after removal. The event had no effect on public health and safety.

Indian Point 3 05000-286 APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Note: The Energy Industry Identification System Codes are identified within the brackets ().

DESCRIPTION OF EVENT

On November 3, 2016, while at 100 percent reactor power, operations received a "Vapor Containment (VC) Sump Pump Running," alarm at approximately 00:27 hours, following a VC sump pump out. In accordance with actions of 3-ARP-009, a check of the Unit Log identified that the last sump pump out was on October 30, 2016. Receipt of this alarm was earlier than expected and a possible indicator of a leak. VC radiation monitors R-11 and R-12 (IL), VC Humidity (1,7), and Fan Cooler Unit (FCU) Weir Levels WI were normal. As a result of the early VC Sump Pump Running alarm (FQA), operations requested Chemistry to obtain a sample of the VC pump out line. Results of the sample showed approximately 149 ppm chlorides, indicating a possible Service Water (SW) (BI) leak due to abnormal chloride levels. Operations entered Technical Specification (TS) 3.6.1 (Containment), Condition A (Containment Inoperable) at 03:00 hours, due to the possibility of a loss of containment (NH) integrity. At 3:19 hours, the 31 FCU (FCU) was secured due to suspected SW FCU coil leakage and entered TS 3.6.6 (Containment Spray System and Containment Fan Cooler System), Condition C (One Containment FCU Train Inoperable). At 3:19 hours, a Safety Function Determination was performed which concluded there had been a loss of safety function and VC became inoperable when indications of a possible SW leak was identified for the 31 FCU. At 3:44 hours, TS 3.6.1, Condition A was exited after the 31 FCU was secured and SW was isolated to the 31 FCU. The leak was recorded in Indian Point Energy Center (IPEC) corrective action program (CAP) as CR-IP3-2016-03607. An 8 hour non-emergency event notification (#52344) was made under 10 CFR 50.72(b) (3)(v) for a loss of safety function.

The SW System (SWS) (BI) is designed to supply cooling water from the Hudson River to various heat loads in both the primary and secondary portions of the plant. The design ensures a continuous flow of cooling water to those systems and components necessary for plant safety during normal operation and under abnormal or accident conditions. The SWS consists of two separate, 100% capacity, safety related cooling water headers. Each header is supplied by 3 pumps to include pump strainers, with SWS heat loads designated as either essential or non-essential.

The essential SWS heat loads are those which must be supplied with cooling water immediately in the event of a Loss of Cooling Accident (LOCA) and/or Loss of Offsite Power (LOOP). The essential SWS heat loads can be cooled by any two of the three SW pumps on the essential header. Either of the two SWS headers can be aligned to supply the essential heat loads or the non-essential SWS heat loads.

A VC entry was performed and inspections identified leak indications at the 31 FCU on the 3rd coil feeding the SW return line fPSP1. To confirm the specific leak location, scaffolding was erected and insulation was removed. A through wall leak was identified on the 31 SW Fan Cooler Unit (FCU) at weld B-297, in branch line C from FCU coil 3. This is one of the 3 inch SW return branch lines from the 31 FCU cooling coils which feeds a 10 inch SW return line header 12b upstream of containment penetration Mb. Line 12b is the SW system return piping from the 31 FCU back to the river.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to 2016 - 001 - 00 The piping for the 3 inch cooling coil return line is 904L stainless steel (SS) with a nominal pipe wall thickness for Schedule 40 pipe (0.216 inches). Leak rate estimate was 0.16 gpm. The leak is at a 3 inch butt-welded joint between a 904L stainless steel elbow (PSF) and pipe IPSP1 located on approximately the 76 foot elevation in containment. The piping leak is in a moderate energy ASME ISI Code Class 3, nuclear safety related piping system. 904L SS material is susceptible to the development of corrosion pits. Pin hole leaks and weld defects in this piping have previously occurred and have been evaluated. The evaluation concluded the 904L piping does not have a general corrosion problem.. Current analysis for SW pipe failures are postulated to be limited to small through-wall leakage flaws as opposed to guillotine breaks. There is no evidence of leakage at any other location on this weld or elsewhere on the piping adjacent to it.

Code Class 3 piping systems are addressed in ASME Code Case N-513-3. This Code Case provides the requirements for demonstrating structural integrity and therefore operability of a flawed pipe section. Characterization of the weld condition was performed by conducting an ultrasonic examination (UT) on November 4, 2016. The weld was examined circumferentially in a 1/5 inch by '1 inch grid pattern and by using a bulls-eye grid pattern in '4 inch increments. These UT, (Non Destructive Examinations) NDE results were documented in an NDE report. However, due to physical obstructions presented by the FCU enclosure, two circumferential grid rows on the backside of the weld could not be reached. Due to the leak location on the bottom side of the pipe on the side opposite from the FCU enclosure, the bulls-eye grid was not obstructed, and all required readings were taken. As a result of limited access, the UT examination of weld B297 resulted in completion of only approximately 70 percent of the circumference of the weld. The remaining 30 percent (approximately 3 inches) was unable to be inspected due to space constraints between the weld and the adjacent FCU plenum wall. ASME Code Case N-513-3 requires the flaw geometry to be characterized by volumetric inspection methods or by physical measurement. It mandates that the full pipe circumference at the flaw location be inspected to characterize the length and depth of all flaws in the pipe section.

Since a full volumetric examination could not be completed, the Code Case requirements could not be met. An immediate on-line weld repair of the defect was not considered feasible due to restrictions preventing 360 degree access, time required for work prep, and the potential for excessive sump filtration loading. As such, an NRC Relief Request to deviate from the 10CFR50.55a ASME Code requirements, specifically full compliance with ASME CC-N-513-3 was required. Therefore, pursuant to 10CFR50.55a(z)(2) Entergy requested relief by letter NL-16-133 (Request IP3-ISI- RR-10, Alternative to the Full Circumferential Inspection Requirement of Code Case N- 513-3), dated November 7, 2016. The NRC approved the relief request which concluded the inability to obtain full circumference readings does not adversely impact the ability to fully characterize the weld condition vs the code case requirements.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to The approval of the relief request allowed Entergy to re-establish SW to the FCU to verify that leakage limits are met using a qualified clamp over the pinhole leak.

The leakage will be inspected daily in accordance with the Code Case requirements.

SW piping to the 31 FCU must be isolated when an allowable leakage is exceeded. The qualified clamp is an engineered clam-shell type clamp comprised on an outer metal jacket and rubber gasket. The clamp is classified as a temporary modification. The clamp will withstand post-accident containment pressure, temperature and environment, is located away from potential missiles and, pipe whip effects, is dedicated for safety-related use, and is rigidly attached to Seismic Category 1 piping. The clamp over the defect will return the system to its original containment integrity configuration and allow the 31 FCU to remain operable.

The defect in the SW return pipe from the 31 FCU was evaluated with respect to TS 5.5.15 (Containment Leak Rate Testing Program), and the Appendix J Leakage program.

TS 5.5.15 requires that the SW in-leakage into containment must be limited to less than 0.36 gpm per FCU when pressurized equal to or greater than 1.1Pa. This limit protects the internal recirculation pumps from flooding during the 12 month period of post-accident recirculation. TS 5.5.15 also implements the leakage rate testing of the containment as required by 10CFR50, Appendix J. The maximum leakage to assure that the post-accident containment leakage remains within allowable limits is 0.023 gpm. This limit is based upon an evaluation to calculate the amount of SW which can leak through this pinhole under normal system operating conditions to ensure that 10CFR50 appendix J containment leakage limits are not exceeded under any mode of operation including accident conditions. The leak does not impinge upon any safety related equipment. As a result, no damage from the leakage is expected to occur.

Based on UT measured readings from the NDE Report, a new calculation was generated (IP-CALC-16-00079 FCU 31 Leak) per the ASME CC-N-513-3 requirements. The minimum required thickness for the elbow containing the weld B297 is 0.073 inches. The minimum measured thickness was 0.117 inches. The maximum allowable axial flaw size is 4.11 inches and the maximum allowable circumferential flaw size is 3.65 inches.

The existing flaw is characterized as approximately 0.50 inches by 0.50 inches, and the uninspected arc length (approximately 3 inches) of the pipe circumference is less than the allowable circumferential flaw length. Therefore, if the entirety of the uninspected portion of the pipe were to be considered a flaw, the pipe would still retain its structural integrity as evaluated in the new calculation. The pinhole flaw is opposite the uninspected portion and the flaw sizes of the two areas are independent and not additive. Based on this information, the pipe is structurally adequate for service consistent with the requirements of ASME Code Case N-513-3. The remaining service life was calculated to be 3.3 years, which is beyond the next scheduled refueling outage in the spring 2017 when a permanent repair will be made.

An extent of condition review determined the Code Case requires five similar and susceptible locations in the SW system to be volumetrically examined. NDEs were performed on November 5, 2016, on five 31 FCU SW pipe welds and recorded in NDE reports. All five weld locations were found to be structurally acceptable and documented in CR-IP3-2016-03607, corrective action (CA-6). The additional inspections confirm the integrity of the SW piping inspected since all UT data measurements were above the 87.5 percent of pipe nominal wall thickness. Also, there was no evidence of additional leakage at any other place in the 31 FCU 3 inch return line or at any other location in the other four FCU return lines. Unit 2 does not apply as it does not have similar 904L SS FCU supply or return lines.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to

CAUSE OF EVENT

The direct cause was a SW leak associated with the 31 FCU at weld B297 in branch line C from coil 3 feeding the 10 inch SW return line 12b. The leak was from a through-wall pinhole flaw at a butt-welded joint between a 904L SS elbow and pipe in containment. The likely degradation mechanism leading to the leak was corrosion. The pipe with the flaw resulted in containment out leakage in excess of 10CFR50, Appendix J limits. The root cause is indeterminate. The specific cause for the pipe joint defect requires the component to be removed and a metallurgical failure analysis performed.

CORRECTIVE ACTIONS

The following corrective actions have been or will be performed under the Corrective Action Program (CAP) to address the causes of this event:

  • A leak-limiting engineered clam-shell type clamp was applied to the pipe flaw.
  • The clamp is being monitored daily by a special operator log for any signs of increased leakage. The maximum allowed leakage rate past the clamp is 0.023 gpm.
  • UT monitoring will be performed every 90 days until the pipe is repaired.
  • The pipe/elbow will be replaced in the next refueling outage (RO) in the spring 2017.
  • The removed pipe/elbow will be inspected and a metallurgical analysis performed by an independent vendor to determine the specific cause.
  • A volumetric inspection of a sample of 3 inch 904L SS butt-welds at the 32, 33, 34, and 35 FCUs will be performed in the spring 2017 RO.
  • The Generic Letter 89-13 Program will be revised to include a requirement to conduct a definitive number of 904L weld volumetric inspections each pre-outage interval.
  • This LER will be updated after engineering review of the metallurgical analysis and revision as necessary of the cause analysis.

EVENT ANALYSIS

The event is reportable under 10 CFR 50.73(a)(2)(v)(C). The licensee shall report any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to (C) Control the release of radioactive material. This condition meets the reporting criteria because TS 3.6.1 Containment Operability was not met.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to The pipe flaw leakage was approximately 0.16 gpm which was greater than the calculated 10 CFR 50, Appendix J allowable leak rate of 0.023 gpm. TS 3.6.1 (Containment) requires the containment to be operable in Modes 1-4. TS Surveillance Requirement (SR) 3.6.1.1 requires visual examinations and leakage rate testing in accordance with the containment Leakage Rate Testing Program specified in TS 5.5.15.

SR 3.6.1.1 leakage rate requirements comply with 10 CFR 50, Appendix J, Option B. As SW is required in an accident, the SW to the FCU would not be isolated in DBA and the piping credited as a closed system inside containment for containment integrity.

Consequently, defects discovered within the FCU SW piping may adversely affect containment integrity and the ability to control releases of radioactive material.

The condition also meets the reporting criteria of 10 CFR 50.73(a) (2)(i)(B). The licensee shall report any operation or condition which was prohibited by the plant's TS. During the previous period of operation for an unknown period of time the SW pipe contained a through wall leak that did not meet code requirements. This previously unrecognized condition required entry into TS 3.7.9 and corrective actions implemented to return the pipe to operable. Failure to comply with the TS LCO and perform required actions is a TS prohibited condition.

PAST SIMILAR EVENTS

A review of the past three years of Licensee Event Reports (LERs) for events that involved containment integrity due to flawed piping credited as a closed system inside containment. No applicable LERs were identified. There was one LER, LER-2014- 002 reporting a Technical Specification prohibited condition for a flaw discovered on a SW pipe connected to the Component Cooling Water Heat Exchanger. This LER is not similar as the impacted piping is outside containment and not credited as a closed system for containment integrity.

SAFETY SIGNIFICANCE

This condition had no effect on the health and safety of the public.

There were no actual safety consequences for the event because there were no accidents or events during the degraded condition.

There were no significant potential safety consequences of this event. The leakage from the affected SW pipe was within the capability of the SW system to provide adequate SW flow to SW loads. The degraded piping was on the discharge of the FCU therefore any failure would not prevent the SW cooling function. Current analysis for SW pipe failures are postulated to be limited to small through-wall leakage flaws as SW is defined as a moderate energy fluid system. The SW leak would eventually drain to the containment sump. The containment sumps have pumps with sufficient capacity to remove excessive leakage and instrumentation to alert operators to a degraded condition.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to The containment consists of the concrete reactor building, its steel liner, and the penetrations through the structure. The containment building is designed to contain radioactive material that might be released from the reactor following a design basis accident (DBA). The containment building steel liner and its penetrations establish the leakage limiting boundary of the containment. Maintaining the containment operable limits the leakage of fission product radioactivity from the containment to the environment. The DBA analysis assumes that the containment is operable such that, for the DBAs involving release of fission product radioactivity, release to the environment is controlled by the rate of containment leakage.

The containment was designed with an allowable leakage rate of 0.1 percent of containment air weight per day. Containment isolation valves form a part of the containment pressure boundary. Two barriers in series are provided for each penetration so that no single credible failure or malfunction of an active component can result in a loss of isolation or leakage that exceeds limits assumed in the safety analysis. One of these barriers may be a closed system such as the SW piping for the FCUs. The only time containment integrity can be affected is post accident when the FCUs safety function is being performed and SW pressure for the FCU cooling piping and coils fall below peak accident pressure. Mitigation of radiation release by the degraded SW pipe pathway can be by use of radiation monitors R-16A and R-16B which monitor containment fan cooling water for radiation indicative of a leak from the containment atmosphere into the cooling water. If radiation is detected, each FCU heat exchanger can be individually sampled to determine the leaking unit. The SW for the 31 FCU can be isolated to prevent radioactive effluent releases. During the time the FCU SW piping was degraded there was no leakage out of containment.

A risk assessment was performed to determine the overall probability of a core damage event which could cause a loss 'of containment integrity due to a SW to FCU leak assuming it would take 5 days to detect a SW leak to a FCU. The risk result was 7.8E-8 which is considered negligible in terms of both core damage and large early release.

Indian Point 3 05000-286

05000416/LER-2016-007Grand Gulf8 September 2016Technical Specification Shutdown due to Loss of Residual Heat Removal Pump

On September 4, 2016 at 02:58, Grand Gulf Nuclear Station entered three TS LCO Action Statements because RHR 'A' pump was declared inoperable.

LCO Actions entered:

1) 3.5.1 for one low pressure ECCS injection/spray subsystem, 2) 3.6.1.7 for one RHR containment spray subsystem, and 3) 3.6.2.3 for one RHR suppression pool cooling subsystem. All have 7 day Completion Times A decision was made to shutdown the plant to repair the RHR 'A' pump because, based on the troubleshooting and testing plan, the pump could not be repaired and returned to service within the LCO Completion Times. At 0300 CDT on 09/08/16, GGNS initiated the transition to Mode 4.

The pump was removed from service and sent to the vendor facility for decontamination, disassembly and failure analysis.

The 'A' pump was then replaced and tested satisfactorily. RHR 'A' was returned to operable.

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Intocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may 366A U.S. NUCLEAR REGULATORY COMMISSION

CONTINUATION SHEET

2. DOCKET 3. LER NUMBER 05000 416

PLANT CONDITIONS PRIOR TO THE EVENT

At the time of the event, Grand Gulf Nuclear Station (GGNS) Unit 1 was in Mode 1, at 100% rated thermal power.

All systems, structures and components, with the exception of the RHR 'A' pump, that were necessary to mitigate, reduce the consequences of, or limit the safety implications of the event were available. No other safety significant components were out of service.

DESCRIPTION

On September 4, 2016, GGNS was performing a Residual Heat Removal (RHR) 'A' quarterly Technical Specification (TS) Surveillance Requirement (SR). At 02:58, The RHR pump failed to meet its TS SR Acceptance Criteria for flow and differential pressure (d/p) and was therefore declared Inoperable. Action Statements for TS Limiting Conditions for Operation (LCOs) 3.5.1, 3.6.1.7 and 3.6.2.3 were entered, each having Completion Times of 7 days.

LCO Action Statements entered:

1) 3.5.1 for one low pressure ECCS injection/spray subsystem, 2) 3.6.1.7 for one RHR containment spray subsystem, and 3) 3.6.2.3 for one RHR suppression pool cooling subsystem.

Initial troubleshooting verified that the pump was incapable of meeting the flow requirement of 7756 gpm and d/p of 131 psid simultaneously. The observed pump flow and discharge pressures were verified to be correct via a temporarily installed ultrasonic flow meter and pressure gauge. RHR system valves and lines were verified not to be clogged or leaking. The pump motor was confirmed to be operating at the proper speed.

Further troubleshooting and testing lead station management to the conclusion that RHR 'A' would not be returned to operable status within the 7 day Completion Time. A decision was made to commence an orderly shutdown. On September 8, 2016 at 0300, GGNS began the transition to Mode 4. No other systems were out of service that would have complicated an orderly shutdown to Mode 4.

REPORTABILITY

Event Notification No. 52225 was made to the U.S. Nuclear Regulatory Commission (NRC) Operations Center.

This LER is being submitted pursuant to Title 10 Code of Federal Regulations 10 CFR 50.73(a)(2)(i)(A) for the completion of any nuclear plant shutdown required by the plant's Technical Specifications. Telephonic notification was made to the NRC Emergency Notification System on September 8, 2016, at 03:27, pursuant to 10 CFR 50.72(b)(2)(i) for the initiation of any nuclear plant shutdown required by the plant's Technical Specifications.

CAUSE

Direct Cause: The RHR 'A' pump was unable to provide its required flow at the required differential pressure in order to perform its safety function.

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs. NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may

NRC FORM

366A U.S. NUCLEAR REGULATORY COMMISSION

CONTINUATION SHEET

Grand Gulf Nuclear Station, Unit 1 05000 416 Apparent Cause: Subsequent investigation suggests internal pump degradation but the Apparent Cause is ongoing. A supplemental report to this LER will be provided when the Apparent Cause investigation is complete.

EXTENT OF CONDITION

Quarterly surveillance data of similar Emergency Core Cooling System (ECCS) pumps showed no evidence of degradation. Data was re-examined from the following pumps: Low Pressure Core Spray (LPCS), High Pressure Core Spray (HPCS) and RHR 'B' and 'C.' GGNS also performed a partial quarterly surveillance on the RHR 'B' which was completed satisfactorily.

CORRECTIVE ACTIONS

The RHR 'A' pump was replaced and retested satisfactorily. The pump removed from service has been sent to the vendor facility for failure analysis.

SAFETY SIGNIFICANCE

The event posed no threat to the health and safety of the general public or to nuclear safety as safety- systems performed as designed. No Technical Specification safety limits were violated. Industrial safety was not challenged, and there was no potential or actual radiological release during the event.

PREVIOUS SIMILAR EVENTS

Previous similar events. will be discussed in the supplemental report upon completion of the Apparent Cause investigation.

05000456/LER-2016-002Braidwood25 May 2016
19 July 2016
Inadequate Protection from Tornado Missiles Identified Due to Non-Conforming Design Conditions
LER 16-002-00 for Braidwood, Unit 1, Regarding Inadequate Protection from Tornado Missiles Identified Due to Non-Conforming Design Conditions

On May 25, 2016, during evaluation of protection for Technical Specification (TS) equipment from the damaging effects of tornadoes, Braidwood identified non-conforming conditions in the plant design such that specific TS equipment on both units was considered to not be adequately protected from tornado missiles.

On May 25, 2016 at 1415 Operations declared the affected equipment inoperable, implemented Enforcement Guidance Memorandum (EGM) 15-002, "Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance" and the required compensatory measures, and then declared the affected equipment operable but non-conforming.

The cause of this issue was a lack of clarity and changing requirements during the original licensing of the plants which led to inadequate understanding of the original NRC regulatory guidance.

The corrective actions planned are to complete the EGM 60-day comprehensive compensatory measures to demonstrate a discernable change from its pre-discovery actions, to modify the refueling water storage tank hatches to eliminate the tornado missile vulnerability, and to obtain and implement a license amendment for an analytical solution dispositioning tornado generated missile nonconforming conditions.

05000285/LER-2016-002Fort Calhoun10 May 2016
7 July 2016
Unanalyzed Condition Shutdown Heat Exchanger Isolations ti
LER 16-002-00 for Fort Calhoun, Unit 1, Regarding Unanalyzed Condition Shutdown Heat Exchanger Isolations

On May 10, 2016, at 1138 Central Daylight Time (CDT), during scheduled maintenance, an unanalyzed condition was discovered as a result of maintenance on Shutdown Cooling Heat Exchanger valves. This condition could have led to the inability of the Component Cooling Water (CCW) system to perform its design function of providing a cooling medium for the Containment atmosphere under Loss Of Coolant Accident (LOCA) conditions.

As part of the maintenance, HCV-484, Shutdown Heat Exchanger AC-4A CCW Outlet Valve, and HCV-481, Shutdown Cooling Heat Exchanger AC-4B CCW Inlet Valve, were open. Under these conditions, with the assumed single failure loss of DC control power and accident condition of a LOCA, CCW would be allowed to flow through both shutdown cooling heat exchangers, bypassing a portion of the flow to the Containment Cooling Units. These conditions are not assumed under plant design basis calculations, and therefore placed the plant in an unanalyzed condition. Both HCV-484 and HCV-481 were returned to service and the condition no longer exists.

05000413/LER-2016-001Catawba13 December 2015
23 June 2016
Mispositioned Breaker for Residual Heat Removal Loop Suction Results in Inoperable Train of Emergency Core Cooling System
LER 16-001-00 for Catawba Nuclear Station Unit 1 Regarding Mispositioned Breaker for Residual Heat Removal Loop Suction Results in Inoperable Train of Emergency Core Cooling System

On March 28, 2016, Operators did not receive the expected results from a relay while performing the 1B train Emergency Core Cooling System (ECCS) Cold Leg Recirculation interlock test. Investigation found the breaker for the residual heat removal pump's loop suction valve incorrectly positioned open. ECCS 1B was declared inoperable. Subsequently, the breaker was closed after it was verified not to have been tripped open.

The last manipulation of this breaker was determined to have been during the coordination for pressure boundary valve testing and standby readiness alignment during the previous refueling cycle (December 2015). A past Operability Evaluation concluded the breaker being open led to a condition prohibited by Technical Specifications, and also a condition that could have prevented the fulfillment of a safety function for Unit 1 ECCS while the 1A emergency diesel generator was inoperable for greater than four hours during this time period. This event was determined to be reportable on April 26, 2016.

The cause of this event is that the test procedure for pressure boundary valve testing did not contain specific procedural guidance for establishing a suction source for the 1B train residual heat removal (RHR) pump. The test procedure required coordination with another procedure to ensure the breaker for the 1B train RHR pump loop suction valve was returned to the closed position. Corrective actions include procedural revisions to these procedures.

05000483/LER-2016-001Callaway20 April 2016
20 June 2016
Control Room Air Conditioning Inoperability Due To Essential Service Water Pressure Transient
LER 16-001-00 for Callaway, Unit 1, Regarding Control Room Air Conditioning Inoperability Due to Essential Service Water Pressure Transient

On 4/20/2016, Callaway received preliminary analysis results showing that during a Design Basis Accident (DBA) the 'B' Train Control Room Air Conditioning System (CRAGS) would experience a pressure transient in the associated cooling water system greater than what is experienced during Engineered Safety Feature Actuation Signal (ESFAS) testing. This condition could damage the NC unit's gaskets, as evidenced during ESFAS testing completed on 4/14/2016, resulting in the affected CRAGS and Control Room Emergency Ventilation System (CREVS) trains not being capable of performing their required safety function. This event is being reported as a condition prohibited by Technical Specifications, an unanalyzed condition, and a condition that could have prevented fulfillment of a safety function.

The root cause of the event is that the original Essential Service Water (ESW) system design did not appropriately account for water column separation and collapse pressure transients inherent during operation. Following the 'B' train ESFAS testing on 4/14/2016, more robust gaskets were installed in affected components. A complete evaluation of the pressures and dynamic forces experienced by all ESW system subcomponents will be performed. The results will be compared to current design limits, and appropriate modifications will be performed to ensure sufficient margin exists in the plant design.

05000266/LER-2016-003Point Beach2 April 2016
1 June 2016
Operation or Condition Prohibited by Technical Specifications
LER 16-003-00 for Point Beach, Unit 1, Regarding Operation or Condition Prohibited by Technical Specifications

On April 2, 2016, Unit 1 entered MODE 4 from MODE 5 without satisfying all of Technical Specification 3.6.6, Containment Spray and Cooling System Limiting Conditions for Operation (LCO) as required by LCO Applicability 3.0.4.

LCO Applicability 3.0.4 does not permit entry into a MODE of applicability when an LCO is not met, unless the associated actions to be entered permit continued operation in the MODE for an unlimited time or after performance of an acceptable risk assessment and the appropriate risk management actions have been established. After entering MODE 4, it was discovered that components were not operable, contrary to LCO 3.0.4.

This event is being reported pursuant to 10 CFR 50.73(a)(2)(i)(B) for operation or condition prohibited by technical specifications.

05000390/LER-2016-003Watts Bar11 March 2016
10 May 2016
Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting
LER 16-003-00 for Watts Bar, Unit 1, Regarding Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting

On March 11, 2016, Watts Bar Nuclear Plant (WBN) Unit 1 concluded that a condition prohibited by Technical Specification (TS) Limiting Condition for Operation (LCO) 3.5.2, ECCS - Operating, had occurred during recent performances of TS Surveillance Requirement (SR) 3.5.2.3. Due to inadequacies with gas quantification methodologies for Safety Injection (SI) and Residual Heat Removal (RHR) system discharge piping, the ability to meet TS SR 3.5.2.3 could not be demonstrated, which is required in accordance with TVA's response to NRC Generic Letter 2008-01, "Managing Gas Accumulation In Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems." This condition existed from March 2012 to December 2015. In a subsequent analysis, WBN determined that the worst case gas accumulation in SI and RHR discharge piping would not have affected the ability of the SI and RHR systems from performing their safety functions. However, because the required actions of TS LCO 3.5.2 were not taken within the required times, WBN was in a condition prohibited by Technical Specifications.

TVA is reporting this issue pursuant to 10 CFR 50.73(a)(2)(i)(B).

05000250/LER-2016-001Turkey Point7 April 2016Loose Breaker Control Power Fuse Caused 3B Emergency Containment Cooler to be Inoperable Longer Than Allowed
LER 16-001-00 for Turkey Point, Unit 3 Regarding Loose Breaker Control Power Fuse Caused the 3B Emergency Containment Cooler to be Inoperable Longer Than Allowed

On February 8, 2016 at approximately 0147 hours, during a surveillance test, control room indications identified that 3B Emergency Containment Cooler (ECC) fan tripped. Troubleshooting found the control power fuse for the fan's power supply breaker was loose in its fuse holder. Investigation revealed that the fuse holder clips had been widened during work activities associated with the installation of the new breaker during the prior Unit 3 refueling and maintenance outage. The most probable cause of the loose fuse was improper insertion.

The installation procedure did not validate fuse holder gap, fuse alignment, and fuse tightness after its last removal and insertion prior to placing the new breaker in service. Inadequate contact during the surveillance test caused the fan trip. The 3B ECC would not have reliably met its safety function mission time and so was determined to be inoperable for approximately 72 days exceeding the 72 hour Technical Specification allowed outage time. In addition, on several occasions during the 72-day period one of the other two ECCs was inoperable concurrently for testing. Corrective actions include: 1) The fuse holder clips were adjusted to provide a tight fit. 2) A review determined additional similar breakers will be inspected for fuse tightness. 3) Future installation and preventive maintenance of similar breakers will check for fuse tightness and correct if necessary. Safety significance is considered low based on a risk assessment showing - Incremental Conditional Core Damage Probability and Incremental Conditional Large Early Release Probability are below the NRC acceptance criteria for minimal risk impact.

05000247/LER-2015-004Indian Point20 December 2015
18 February 2016
Safety System Functional Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe
LER 15-004-00 for Indian Point 2 Regarding Safety System Functional Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe

On December 20, 2015, operator investigations identified service water (SW) leakage in containment and on December 22, 2015 discovered a through wall leak on a socket welded elbow for the 21 Fan Cooler Unit (FCU) motor cooler SW 2 inch copper-nickel return line.

The leak was located in a pipe fitting that is within the ASME Section XI Code ISI Class 3 boundary and estimated to be

  • approximately-1 gpm.

Since the pipe flaw was through wall and was located within the ASME Section XI boundary, it exceeded the flaw allowable limits provided per IWD-3000. Engineering determined that since the through wall flaw was located on a socket welded fitting, the ASME Code Case N-513-3 did not apply.

The 21 FCU was declared inoperable and Technical Specification (TS) 3.6.6 (Containment Spray and Containment FCU System), entered for one FCU train inoperable and TS 3.6.1 Condition A entered for containment inoperable.

The 21 FCU SW return line was isolated.

The pipe is part of a closed loop system inside containment and is required to meet containment integrity. Since a containment leakage evaluation was not performed, the pipe flaw -was conservatively assumed to result in post-accident containment out leakage in excess of the 10CFR50, Appendix J limits resulting in violation of the containment integrity requirements and therefore is a safety system functional failure.

The direct cause was flow assisted erosion-corrosion. The apparent cause was high SW flow conditions that caused high localized velocities and flow separation at the sharp interior edge of the socket welded fitting.

Corrective actions included replacement of the affected fitting.

The faulted fitting was sent out to a vendor for metallurgical failure analysis.

The procedure for FCU SW flow balanced will be revised to reduce the SW flow in FCU motor coolers. The event had no significant effect on public health and safety.

FACILITY NAME (1) PAGE (3) DOCKET (2) LER NUMBER (6)

05000461/LER-2016-001Clinton20 January 20161 OF 4On January 20, 2016 at 1311, during planned clean and inspect maintenance activities on the 4160/480 Volt Unit Substation K (0AP52E), the Unit Substation K switchgear breaker OAP52E-5D for Continuous Containment Purge (CCP) exhaust fan "A" was racked out which resulted in tripping off the CCP "B" exhaust fan. This event caused Clinton Power Station (CPS) to enter one hour Required Action A.1 under Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.6.1.4, Primary Containment Pressure, due to primary to secondary containment differential pressure being greater than +0.25 psid. Operations staff took appropriate actions to rack in breaker OAP52E-5D to restart CCP "B" exhaust fan, restore primary to secondary containment differential pressure within limits at 1339. Event Notification #51669 was transmitted to the NRC on January 20, 2016 at 1731. The root cause of this event is the station did not validate assumptions resulting in an inadequate work package. Corrective actions include updating the maintenance planning checklist, performing a read and sign and presenting a case study to maintenance planning personnel on this event. This event is reportable under 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition and 10 CFR 50.73(a)(2)(v)(D) as a condition that could have prevented fulfillment of a safety function.
05000328/LER-2015-002Sequoyah
F
10 November 2015
6 January 2016
Unanalyzed Condition Due To Inoperable Containment Recirculation Drains
LER 15-002-00 for Sequoyah, Unit 2, Regarding Unanalyzed Condition Due to Inoperable Containment Recirculation Drains

On November 10, 2015, at 1502 Eastern Standard Time (EST), two cold weather suits were inadvertently dropped into the equipment pit portion of the Sequoyah Nuclear Plant Unit 2 reactor cavity, resulting in two containment recirculation drains being declared inoperable. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.15, "Containment Recirculation Drains," and TS LCO 3.0.3 were entered. The first suit was removed from the equipment pit at 1553 EST.

At that time, only one of the drains remained inoperable and LCO 3.0.3 was exited. The remaining suit was removed from the equipment pit at 1556 EST, and LCO 3.6.15 was exited. Plant conditions were restored to normal within the allowed LCO times and no plant shutdown was required. The two cold weather suits in the Unit 2 reactor cavity area created the potential for obstructing the flow path for containment recirculation adversely affecting the safety function of the Containment Spray and Emergency Core Cooling Systems that are needed to mitigate the consequences of a design basis accident. The effect of this condition resulted in an unanalyzed condition that significantly degraded plant safety.

The apparent cause was failure of the Maintenance personnel to identify and mitigate potential hazards and risks during the pre-job briefs, 2-minute rule, and walk downs. Corrective action includes addition of risk mitigation strategies to the containment access control procedure. Unit 1 was unaffected by this event.

05000272/LER-2015-005Salem22 June 2015Low Containment Spray Additive Tank Sodium Hydroxide Concentration

On June 22, 2015, at 1406, control room operators were notified by chemistry personnel that the Salem Unit 1 Containment Spray Additive Tank Sodium Hydroxide (NaOH) concentration was less than the minimum concentration by weight as required by Technical Specification (TS). Salem entered TS Action Statement 3.6.2.2.a for low NaOH concentration in the Containment Spray Additive Tank. On June 23, 2015 at 1908, NaOH concentration was returned to its minimum required TS value and the plant exited TS 3.6.2.2.a.

This report is made in accordance with 10 CFR 50. 73(a)(2)(i)(B) for "Any operation or condition which was prohibited by the plant's Technical Specifications ... " and 10 CFR 50.73(a)(2)(v) for "Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: ... (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident.

05000336/LER-2015-002Millstone11 June 2015Degraded Emergency Core Cooling System Check Valve

On June 11, 2015, while Millstone Power Station Unit 2 (MPS2) was in MODE 1 operating at 100 percent power, Engineering identified that due to a degraded check valve, the post-accident radioactivity release rates assumed in the FSAR could be affected. While performing 'B' High Pressure Safety Injection (HPSI) pump in-service testing, the measured flow was lower than expected. Because both trains of HPSI, Low Pressure Safety Injection (LPSI) pumps, and Containment Spray (CS) pumps share a common minimum flow recirculation line back to the Refueling Water Storage Tank, back-leakage through one of the idle pump's recirculation check valves was postulated as the cause of the observed drop in recirculation flow. Troubleshooting was performed, and it was determined that the minimum flow check valve associated with the 'A' CS pump, 2-CS-6A, was back-leaking. The associated minimum flow isolation valve was closed to eliminate the flow path. Back-leakage of the minimum flow recirculation check valves on the HPSI, LPSI, and CS pumps was not previously considered in radiological release analysis. This leakage had the potential to adversely affect calculated post-Loss of Coolant Accident recirculation phase radioactivity release rates under some postulated scenarios.

This event is being reported as an event or condition that could have prevented fulfillment of a safety function to control the release of radioactive material under 10 CFR 50.73(a)(2)(v)(C). The cause of the event was a failed open check valve. As a corrective action, the failed check valve 2-CS-6A has been repaired.

NRC FORM 356 (02-2014) RC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (02-2o14) APPROVED BY OMB: NO. 3160-0104 EXPIRES: 0113112017 Reported lessons learned are Incorporated into the licensing process and fed back lo industry.

Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Intocollects.Resourcei10 CFR nrc.gov, and to the Desk Officer, Office of Information end Regulatory Affairs, NEOB-t0202, (3/5041104), Office of Managemen1 and Budget, Washington, DC 20503.11 a means used to impose an information collection does not of-splay a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not requi red to respond lo, the Information collection.

1. EVENT DE3CRIIPT

  • On June 11, 2015, while Millstone Power Station Unit 2 (MPS2) was in MODE 1 operating at 100 percent power, Engineering identified that due to a degraded check valve, the post-accident radioactivity release rates assumed in the FSAR could be affected. While performing 'B' High Pressure Safety Injection (HPSI) pump in-service testing, the measured flow was lower than expected. Because both trains of HPSI, Low Pressure Safety injection (ILPSO pumps, and Containment Spray (CS) pumps share a common minimum flow recirculation line back to the Refueling Water Storage Tank (RWST), back-leakage through one of the idle pumps recirculation check valves was postulated as the cause of the observed drop in flow. Troubleshooting was performed, and it was determined that a degraded minimum flow check valve associated with the 'A' CS pump (2-CS-6A) was back-leaking into the “A" train suction line and flowing to the RWST through 2-CS-14A (RWST suction check valve) and normally open 2-CS-13.1A (RWST suction line isolation).

The associated minimum flow isolation valve for 2-CS-6A was closed to eliminate the path and the valve was repaired.

Subsequently, engineering evaluation determined that during a loss of power to one facility or train of the Emergency Core Cooling System (ECCS), this back-leakage flow path could result in more leakage to the RWST than had been previously considered in the accident analysis. This leakage was evaluated for the potential to adversely affect calculated post—Loss of Coolant Accident recirculation phase radioactivity release rates under some postulated scenarios. Specifically, without power on the affected (i.e.: back-leaking) train, the CS discharge flowpath would not automatically open resulting in leakage to the RWST.

Prior to this discovery, the East time that the 'A' containment spray pump was run was on April 15, 2015, which would have opened 2-CS-6A. On this basis, it was concluded that this condition existed from April 15, 2015 to June 11, 2015. During this period, the 'A' Emergency Diesel Generator (EDG) was inoperable 4 times for a total of approximately 25 hours. However, all 4 times were for surveillances. At no time during this period was any maintenance done on the 'A' EDG. It is judged that, between accident initiation and commencement of sump recirculation (approximately 2 hours with only one train available), the EDG could have been made available.

This event is being reported as an event or condition that could have prevented fulfillment of a safety function to control the release of radioactive material under 10 CFR 50.73(a)(2)(v)(C). Note: The initial non-emergency report (#51149) of this issue on June 11, 2015 was subsequently updated on July 10, 2015. An additional unidentified release path from the original design of the plant was reported to the NRC as a follow-up notification on July 10, 2015.

BACKGROUND

The MPS2 Containment Spray (CS) system functions as an engineered safety feature to limit containment pressure and temperature after a loss-of-coolant accident (LOCA) and Main Steam Line Break (MSLE) accident, and thereby reduce the potential for leakage of airborne radioactivity to the outside environment. A minimum flow recirculation line is included in the design for recirculating water from the outlet of the pump to the RWST.

With the CS system operating during a design basis accident, a small portion of the CS pump discharge flow recirculates to the RWST during the injection phase; however, the recirculation line is isolated from the RWST when transferring to sump recirculation. All seven ECCS/CS pumps (2 LPSI, 2 CS, and 3 HPSI) have minimum flow recirculation lines that tie into one common header to the RWST. Exhibit A attached to this LER is a sketch depicting the configuration.

Evaluation of this failure identified that during a SBLOCA (Small Break Loss of Coolant Accident) concurrent with a loss of power to the "A" train associated with the leaking 2-CS-6A, the operating (opposite) train HPSI pump would pressurize the common recirculation header during the injection phase of the accident as was described above. In the operator response to this postulated event when the 2-CS-6A leaks to the RWST, suction 2-CS-13.1B is manually isolated terminating the release to the RWST. However, it was additionally identified that the "A" train suction header would pressurize because of the continued back leakage with none of the "A" train pumps flowing due to loss of power and no open flowpath (to containment spray or RWST). This pressurization would continue, exceeding the design pressure of the suction header (60 psig) ultimately reaching 500 psig, the lift setpoint for the two "A" train shutdown cooling heat exchanger relief valves downstream of the "A" LPSI and CS pumps. These relief valves discharge to the EDST (Equipment Drains Sump Tank) which is located outside the filtered ventilation boundary. Upon emptying of the RWST and initiation of sump recirculation, the described back-leakage flowpath would contain sump fluid. This additional unidentified release path from the original design of the plant was reported to the NRC as a follow-up notification on July 10, 2015.

For this accident and radiological release sequence to occur the following are required:

  • 2-CS-6A back-leakage
  • SBLOCA
  • Loss of Offsite Power (LOOP)
  • Loss of the "A" train of onsite electric power
  • SBLOCA break size that results in RCS re-pressurization and sustained RCS pressures above 500 psig, such that HPSI would continue to pressurize the recirculation header
  • Fuel damage While the discussion above relates to 2-CS-6A and the "A" train, back leakage from any of the minimum flow check valves and a concurrent loss of power to that train will have a similar outcome.

2. CAUSE:

The cause of the event was a failed-open check valve. Leakage of these check valves was not considered as a failure mode in the Millstone Unit 2 FSAR or original design basis.

3. ASSESSMENT OF SAFETY CONSEQUENCES:

An Operability Determination has been prepared and approved to document the radiological consequences of the condition. The radiological consequences of ECCS/CS min-flow check valve(s) leakage were evaluated for 5 gallons per minute of post LOCA containment sump liquid relieving to the Equipment Drains Sump Tank. This evaluation considered a 30 day unfiltered ground release and used a best estimate source term (gap release, 1% partitioning, etc.). This leakage was added to the consequences of previously identified leak paths, which had been analyzed using design basis LOCA analysis assumptions. The maximum train as found leakage was .089 gpm, well below the 5 gpm limit using best estimate source term.

Even with the addition of the minimum-flow leakage, the control room and offsite dose consequences are within the regulatory limits of 10CFR50.67,

4. CORRECTIVE ACTION:

During the recently completed 2R23 refueling outage, leak testing of ail MPS2 ECCS/CS min-flow check valves was completed. The testing was performed at 500 psig. The results were scaled to 1200 psid to reflect the highest HPSI discharge pressure. The resultant maximum as-found leak rate was 0.089 gpm through the 'A' ECCS/CS train. The failed check valve 2-CS-6A has been repaired. The 'B' HPSI check valve 2-SI-422, the check valve with the highest as-found leakage rate of 0.085 gpm, was repaired and retested. The maximum ECCS/CS pump min-flow as-left check valve leak rate in a train is 0.004 gpm.

Additional corrective actions are being taken in accordance with the station's corrective action program.

5. PREVIOUS OCCURRENCES:

  • None 6. Energy Industry Identification System (EIIS) codes:
  • Pump — P
  • Valve — V
  • Tank —T
  • Containment Spray — CS
  • Safety Injection — Si
05000285/LER-2015-003Fort Calhoun16 April 2015ouis P. Cortopassi
Site Vice President and CNO
Omaha Public Power District
444 South 161h Street Mall
Omaha, NE 68102-2247
10 CFR 50.73
LIC-15-0062
June 15, 2015
U.S. Nuclear Regulatory Commission
Attn: Document Control Desk
Washington, DC 20555-0001
Fort Calhoun Station, Unit No. 1
Renewed Facility Operating License No. DPR-40
NRC Docket No. 50-285
Subject: Licensee Event Report 2015-003, Revision 0, for the Fort Calhoun Station
Please find attached Licensee Event Report 2015-003, Revision 0. This report is being submitted
pursuant to 10 CFR 50.73(a)(2)(i)(B) and 50.73(a)(2)(v)(B). There are no new commitments being
made in this letter.
If you should have any questions, please contact Terrence W. Simpkin, Manager, Site
Regulatory Assurance, at (402) 533-6263.
LPC/epm
Attachment
c: M. L. Dapas, NRC Regional Administrator, Region IV
C. F. Lyon, NRC Senior Project Manager
S.M. Schneider, NRC Senior Resident Inspector
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION
(02-2014)
LICENSEE EVENT REPORT (LER)
(See Page 2 for required number of
digits/characters for each block)
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 01/31/2017
Estimated burden per response to comply with this mandatory collection request 80 hours.
Reported lessons learned are incorporated into the licensing process and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections
Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by
intemet e-mail to Infocollects.Resource@nrogov, and to the Desk Officer, Office of Information and
Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC
20503. If a means used to impose an information collection does not display a currently valid OMB
control number, the NRC may not conduct or sponsor, and a person is not required to respond to,
the information collection.
1. FACILITY NAME
Fort Calhoun Station
2. DOCKET NUMBER
05000285
3. PAGE
1 OF 4
Containment Spray Inoperable due to Original Design Error

During design basis reconstitution of the Containment Spray (CS) system, it was discovered that the CS piping inside containment and the containment liner have higher stresses during a postulated Main Steam Line Break (MSLB) or Loss of Coolant Accident (LOCA) than previously analyzed. The preliminary analysis concluded that both CS piping trains inside containment and the containment liner failed to meet the operability requirements of American Society of Mechanical Engineers (ASME) Section III Appendix F without implementing compensatory measures.

A cause analysis was performed and determined that thermal expansion was never considered for the containment riser supports. This is a flaw in the original design of the CS header and rings inside containment.

An operability evaluation was completed in support of plant operation. The operability evaluation conclude that the piping and pipe supports of the CS System as well as the Containment liner are capable of performing their intended safety functions per the operability criteria of ASME BPVC Section III Appendix F following modifications completed under Engineering Change (EC) 65926. Additional evaluation determined that only one pipe support exceeded the code allowable stresses. Final corrective action to fully qualify the CS system will be completed under the stations corrective action program.

05000286/LER-2015-003Indian Point9 April 2015Buchanan, N.Y. 10511-0249
Tel (914) 254-6700
Lawrence Coyle
Site Vice President
NL-15-065
June 8, 2015
U.S. Nuclear Regulatory Commission
Document Control Desk
11545 Rockville Pike, TWFN-2 Fl
Rockville, MD 20852-2738
SUBJECT: Licensee Event Report # 2015-003-00, "Technical Specification
Prohibited Condition Caused by Failure to Meet Containment Fan Cooler
Unit Service Water (SW) Flow Rate Due to Improper SW Surveillance
Test Configuration"
Indian Point Unit No. 3
Docket No. 50-286
DPR-64
Dear Sir or Madam:
Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby
provides Licensee Event Report (LER) 2015-003-00. The attached LER identifies an
event where containment fan cooler unit service water flow rates did not meet test
criteria as a result of improper test configuration, which is reportable under 10 CFR
50.73(a)(2)(i)(B) as a Technical Specification Prohibited Condition during past operation.
This condition was recorded in the Entergy Corrective Action Program as Condition
Report CR-IP3-2015-01063 and CR-IP3-2015-02448.
There are no new commitments identified in this letter. Should you have any questions
regarding this submittal, please contact Mr. Robert Walpole, Manager, Regulatory
Assurance at (914) 254-6710.
Sincerely,
fild-#44‘xe
LC/cbr
cc: Mr. Daniel H. Dorman, Regional Administrator, NRC Region I
NRC Resident Inspector's Office, Indian Point 3
Ms. Bridget Frymire, New York State Public Service Commission
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION
(01-2014)
LICENSEE EVENT REPORT (LER)
APPROVED BY OMB NO. 3150-0104 EXPIRES: 01/31/2017
Estimated burden per response to comply with this mandatory collection
request: 80 hours. Reported lessons learned are incorporated into the
licensing process and fed back to industry. Send comments regarding burden
estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S.
Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet
e-mail to infocollectssesource@nrc.gov, and to the Desk Officer, Office of
Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of
Management and Budget, Washington, DC 20503. If a means used to impose
an information collection does not display a currently valid OMB control
number, the NRC may not conduct or sponsor, and a person is not required to
respond to, the information collection.
1. FACILITY NAME: INDIAN POINT 3 2. DOCKET NUMBER
05000-286
3. PAGE
1 OF 5
4.TITLE:Technical Specification Prohibited Condition Caused by Failure to Meet Containment
Fan Cooler Unit Service Water (SW) Flow Rate Due to Improper SW Surveillance Test
Configuration

On March 3, 2015, while in Mode 5 (cold shutdown) for a refueling outage, during performance of 3-PT-R200 (Essential Service Water Header Flow Balance) the As-Found service water (SW) flow rates for the 31 Fan Cooler Unit (FCU), 32 FCU and 33 FCU were less than the Technical Specification (TS) 3.6.6 (Containment Spray and Containment Fan Cooler System) Surveillance Requirement (SR) 3.6.6.3 flow of 1430 gpm.

The SW essential header was re-balanced by adjusting FCU throttle valves to obtain a minimum of 1430 gpm for all five FCUs. On April 9, 2015, an engineering review of test data recorded from test 3-PT-R200, determined that the quarterly test (3-PT-Q016) that verifies FCU flows is not performed in the correct alignment for validating SW flow for the FCUs per TS SR 3.6.6.3.

Test 3-PT-Q016 tests SW flow through FCU with SW isolated through the Emergency Diesel Generator (EDG) coolers.

This configuration is not consistent with post accident operation in which SW is aligned to the FCUs and EDGs.

The apparent cause was improper implementation of improved TS requirements.

Corrective action was a revision of procedure 3-PT-Q016 to require validation of FCU SW flow with the EDG SW flow control valves and FCU outlet temperature control valves open.

The event had no significant effect on public health and safety.

05000346/LER-2015-001Davis Besse11 February 2015Borated Water Storage Tank (BWST) Rendered Inoperable due to Use of Non-Seismic Purification System

On February 11, 2015, with the Davis-Besse Nuclear Power Station operating in Mode 1 at approximately 100 percent full power, during a Nuclear Regulatory Commission (NRC) Component Design Basis Inspection, it was identified the seismic Borated Water Storage Tank (BWST) had been aligned in the past to the non- seismic Spent Fuel Pool (SFP) system for purification. This rendered the BWST inoperable for periods of time longer than allowed per Technical Specification 3.5.4 while the plant was operating in Modes 1 through 4.

Since initial plant design, the BWST had been aligned to the non-seismic SFP system at various times for purification of the BWST contents.

The cause of this event was that regulatory requirements for the separation of seismically qualified and non- qualified systems, structures, and components were not adequately incorporated into design basis documents and the Updated Safety Analysis Report. Administrative controls were established to restrict the alignments that could affect the operability of the BWST. All corrective actions have been completed. The condition is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition which was prohibited by the plant's Technical Specifications and 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function systems needed to mitigate the consequences of an accident.

05000529/LER-2015-001Palo Verde11 January 2015Condition Prohibited by Technical Specification (TS) Limiting Condition for Operation (LCO) 3.3.5, Engineered Safety Features Actuation System (ESFAS)

On January 11, 2015, at 0024, Unit 2 received a plant computer monitoring system (RJ) alarm on point SASB22, indicating the setpoint for the bistable relay that compares pressures between Steam Generators (SGs) was approaching the technical specification (TS) allowable limit for SG Pressure Difference-High. SASB22 does not alarm to control room annunciators (RK) and went unnoticed until late in the shift. Operators then verified the annunciator for SG differential pressure (DP) was not alarming and SG pressures were normal. The significance of the RJ alarm was not apparent because the value was displayed in units of voltage versus DP.

On January 24, 2015, further questioning determined the setpoint for the bistable that monitors differential pressure between SGs had exceeded its allowable value. Channel B SG Pressure Difference-High was declared inoperable and SG Level 2-Low was placed in bypass per LCO 3.3.5, Condition A.

The direct cause of the event was setpoint drift of the SASB22 bistable relay caused by potentiometers that had not recently been wiped clean. The root cause was the lack of an annunciated alarm for SASB22 and associated alarm response procedure to ensure the alarm condition was promptly acknowledged, understood, and correctly addressed within TS time limitations.

No previous similar events have been reported to the NRC by PVNGS in the prior three years.

05000286/LER-2015-001Indian Point8 January 2015Safety System Functional Failure Due to Inoperable Refueling Water Storage Tank Level Alarms Due to Freezing of the Level Instrument Sensing Lines Caused by a Failed Strip Heater

On January 8, 2015, the Refueling Water Storage Tank (RWST) level sensing instrumentation lines (LT-920 and LIC-921) were discovered frozen resulting in inoperable low-low level alarms in the Control Room. Entered Technical Specification (TS) 3.5.4 (RWST) Condition C due to both RWST low-low level alarms disabled in the CR.

TS Condition C requires at least one channel of RWST low-low level to be restored to operable in one hour. Actions initiated to return one RWST level channel to operable..

Entered TS 3.5.4 Condition D (Required Action and associated Completion Time not met) D.1 be in. Mode 3 in 6 hours and D.2 be in Mode 4 in 12 hours. Commenced unit shutdown per TS for inoperable RWST level alarms. Repairs and calibrations completed returning the RWST level alarms to operable. TS 3.5.4 exited and power ascension commenced. Loss . of-both LT alarms is a safety system functional failure as the alarms are credited for operator manual switchover for recirculation. Direct cause was failure of the RWST instrument level alarm strip heater to maintain the temperature in the instrument enclosure. - Due to the failure of the heat trace circuit EHT34-1 strip heater to . function combined with a period of severe cold weather resulted in the sensing lines for the RWST.to freeze. The apparent cause was a high resistance electrical connection at the strip heater wire lug due to thermal cycling and age. Corrective actions included _repair of ring lug to strip heater and calibration of level instrumentation.

Maintenance procedure 0-ELC-419-EHT will be revised to include inspection/repair of -. strip heater and ring lug connections within instrument enclosures. An action request (AR) will be initiated for a new model Work Order/PM to inspect strip heater connections and-operation. The event had no significant effect on public health and safety.

05000338/LER-2014-002North Anna10 December 2014Inadvertent Loss of Vital Instrumentation During Maintenance Due to Personnel Error .On December 10, 2014, at 1344 hours, two channels of the Unit 1 Refueling Water Storage Tank (RWST) level instrumentation were inadvertently removed from service at the same time during maintenance. Operations personnel responded by entering abnormal procedure 1-AP-3, Loss of Vital Instrumentation. Additionally, Technical Specification (TS) 3.0.3 was entered due to two channels being inoperable that affect Recirculation Spray (RS) pump auto-start logic. Had a Containment Depressurization Actuation (CDA) occurred during this time, accident mitigation may have been impacted. At 1356 hours, both level indications returned to normal. At 1417 hours, Channel II was declared operable and TS 3.0.3 was cleared. At 1439 hours, Channel I was declared operable and TS Actions were cleared. An 8-hour report was made at 1713 hours per 10 CFR 50.72(b)(2)(v)(D) for a condition that could have prevented the fulfillment of a safety function to mitigate the consequences of an accident. The health and safety of the public were not affected by this event.
05000336/LER-2014-005Millstone17 May 20141 OF 3

At 1933 on May 16, 2014 while in MODE 3, Millstone Power Station Unit 2 (MPS2) exceeded the Limiting Condition for Operation (LCO) of plant Technical Specification (TS) 3.6.2.1 'Containment Spray System' Action a.1 for an inoperable containment spray pump. The 'A' containment spray (CS) pump was declared inoperable at 0018 on May 17, 2014, the date of discovery, following completion of surveillance testing to determine the presence of gas voids.

However, the gas was introduced earlier during the refueling outage and the TS LCO went into effect upon first entry into MODE 3 greater than 1750 psia on May 13, 2014, at 1933. TS 3.6.2.1 Action a.1 requires that the pump be restored to OPERABLE status within 72 hours or be in at least HOT STANDBY within the next 6 hours and reduce pressurizer pressure to less than 1750 psia within the following 6 hours. MPS2 had been in a MODE where the CS system was required to be OPERABLE for 70.5 hours prior to completion of the testing. The gases were successfully removed by venting and the system was restored to OPERABLE status at 1221 on May 17, 2014.

This condition is being reported as any operation or condition which was prohibited by the plant's technical specifications in accordance with 10 CFR 50.73 (a)(2)(i)(B). The condition was caused by not adequately venting the CS system and delays in communicating the surveillance results, combined with a need to schedule performance of the surveillance testing earlier in a refueling outage. Corrective actions planned will improve scheduling of the testing and will result in more timely communications of the results from completed testing.

05000285/LER-2014-004Fort Calhoun24 April 2014Unqualified Limit Switches Render Safety Equipment Inoperable

On April 24, 2014, during a review of previous conditions affecting equipment qualification it was identified that the environmental qualification of Namco EA180 series limit switches were not being properly maintained per vendor requirements. This condition was not verbally reported at the time of discovery as the condition was identified and resolved while the plant was in an extended shutdown.

A cause evaluation was completed and determined that technical requirements from the vendor manual for maintaining environmental qualification of the Namco EA180 series limit switches were not captured in the applicable plant procedure.

The applicable plant procedure has been revised to include vendor information for maintaining environmental qualification of the limit switches. The limit switch top cover gasket and screw assemblies for all environmentally qualified Namco EA180 series limit switches were replaced and torqued in accordance with vendor requirements.

05000413/LER-2014-001Catawba7 March 2014Condition Prohibited by Technical Specifications (TS) and Notice of Enforcement Discretion (NOED) Due to Misaligned Connecting Rod Bearing on Diesel Generator (DG) 1A

On March 7, 2014 at 0929 hours, TS 3.8.1, "AC Sources - Operating" was violated as a result of maintenance activities on DG 1A to replace a connecting rod bearing that was found to have rotated from its normal horizontal position. Catawba had previously requested a NOED on March 6, 2014 in anticipation of exceeding the applicable TS 3.8.1 Required Action Completion Time. The NOED was subsequently granted by the NRC on that same day. This event is therefore reportable under 10 CFR 50.73(a)(2)(i)(B) as an operation or condition which was prohibited by the plant's TS. The affected bearing was proactively replaced, leading to the need for the NOED. The most probable cause of the rotation of the affected bearing is inadequate procedural control of lubricating oil temperature prior to starting an engine following extended periods of maintenance. Corrective actions taken in response to this event include revisions to plant procedures governing DG maintenance and operation. It was subsequently determined that the affected DG 1A bearing would have been able to perform its specified safety function in the as-found condition. During the period that DG 1A was inoperable while the affected bearing was being replaced, DG 1B was operable.

Therefore, this event had no adverse effect upon the health and safety of the public.

05000285/LER-2014-001Fort Calhoun8 January 2014Reactor Shutdown due to Sluice Gate Failure

At approximately 2230 Central Standard Time (CST), on January 8, 2014, CW-14C, Traveling Screen Sluice Gate, motor operator shaft was found damaged (bent) by Operations personnel. At 2330 CST a large block of ice buildup was observed on top of the sluice gate caused by a pinhole leak in the backwash piping located directly above the CW-14C gate. At 0250 CST, January 9, 2014, Operations unsuccessfully attempted manual closing of CW-14C. At 0315 CST the station entered TS 2.0.1(1) due to all raw water (RW) pumps being declared inoperable. At 0518 CST the station commenced a reactor shutdown. At 0900 CST the station completed the reactor shutdown.

The root cause was determined to be that CW-14C MOV torque setting was at a value that allowed the stem to be bent.

CW-14C was lowered and then verified closed by divers. The flooding strategy for the Intake Structure was met at 0350 CST on January 10, 2014. RW Pumps AC-10A, AC-10B, AC-10C and AC-10D were declared operable and TS 2.0.1(1) was exited.

05000327/LER-2013-003Sequoyah23 August 2013Limiting Conditions for Operation Exceeded for Emergency Core Cooling SystemOn August 8,2013, position indication for emergency core cooling system (ECCS) A-Train residual heat removal (RHR) Containment Sump Isolation Valve was found showing the valve to be in mid-position. The valve was verified to be in a closed position. On August 14, ECCS valve testing was conducted. Testing identified the 1A RHR Pump Suction Valve failed to close when requested. Operations personnel declared the valve inoperable and remained in the applicable LCO's. Maintenance troubleshooting determined that multiple grounds existed in the control circuits of each of the valves. Water was found in the motor limit-switch housing control circuit of the RHR Containment Sump Isolation Valve. The cause of the condition was that the conduit penetrations for RHR Containment Sump Isolation Valve were not designed to account for groundwater infiltration through the plant concrete structures resulting in leakage into the conduit. Actions are being taken to redesign the conduit penetrations for each Unit's RHR Containment Sump Isolation Valves, to ensure the penetrations are sealed and/or water tight to prevent water from entering the motor operator valve operator associated with each valve.
05000382/LER-2014-001Waterford8 May 2013Room Cooler Breaker Inoperability Causes Past Inoperability of Containment Spray System Train

On May 8, 2013 at 19:53, a safety-related circuit breaker failed when Operations personnel attempted to start Shutdown Cooling Heat Exchanger Room B air handling unit. In accordance with Operations administrative procedure for Technical Specification and Technical Requirements Compliance, Operations personnel entered the applicable Technical Specification Limiting Condition for Operation for Containment Spray (CS) train B. A replacement breaker was installed and a successful start of the air handling unit was performed. CS Train B was declared operable at 17:30 on May 9, 2013.

An evaluation of the failure determined that the air handling unit had been effectively rendered inoperable since installation of the circuit breaker on April 18, 2013. Containment Spray train B was inoperable from 03:09 on April 17, 2013, when the train was declared inoperable to perform preventative maintenance until 17:30 on May 9, 2013, a total of 22.6 days. This time period exceeds the Technical Specification allowed outage time of 7 days. Technical Specification 3.6.2.1 was not complied with, which requires that with one CS system (train) inoperable, restore the system (train) to operable status within 7 days or be in at least Hot Standby within the next six hours. During this time frame CS 'A' was inoperable for 6.65 hours. Since both trains of Containment Spray were inoperable this is considered a Safety System functional failure due to the system being unable to mitigate the consequences of an accident.

05000255/LER-2013-002Palisades5 May 20131 OF 3

At 0027 on May 5, 2013, the safety injection/refueling water (SIRW) tank was declared inoperable in accordance with the operational decision-making issue (ODMI) process. Water leakage from the tank had exceeded the pre-established limit of the ODMI process that directed the tank be declared inoperable.

Leakage from the tank was quantified at approximately ninety gallons per day. Technical Specification (TS) 3.5.4.B requires restoration of an inoperable SIRW tank within one hour. If the tank is not returned to an operable status within one hour, TS 3.5.4.0 requires the plant be placed in Mode 3 within six hours and in Mode 5 within the subsequent thirty-six hours.

Due to the inability to repair the leak within the required one-hour time frame, a plant shutdown was initiated at approximately 0100 hours on May 5, 2013. The plant entered Mode 3 at 0457 hours on May 5, 2013. At 2358 hours on May 5, 2013, the plant entered Mode 5 to execute repairs.

Testing identified an approximate 3/16-inch through-wall crack in a nozzle reinforcing collar to floor plate weld of the tank. Follow-up analysis determined there was significant lack of fusion in the weld that resulted in the failure of the weld and subsequent water leakage. The welder that fabricated the weld did not ensure adequate fusion at the weld root.

The entire SIRW tank floor was replaced with the exception of an annulus ring around the perimeter.

Several initiatives were implemented to preclude potential weld issues during the fabrication of the new tank floor, including welder proficiency training on revised welding techniques and utilization of several types of weld testing methods.

05000266/LER-2013-002Point Beach14 April 2013Condition Prohibited by Technical Specifications

On April 13, 2013 at 23:39 PBNP Unit 1 entered Mode 4 during start up from a refueling outage. On April 14, 2013 at 0620, approximately 6 hours after entering into MODE 4, the Unit 1 sodium hydroxide tank outlet valve (1S1-831A) was found to be closed. This valve isolated the flow path for both trains of spray additive equipment and resulted in not meeting LCO 3.6.7, Spray Additive System. That mode change resulted in a violation of LCO 3.0.4.

The incorrect valve position was discovered when a senior reactor operator identified a caution tag on the 1S1-831A valve. Operations investigated the unexpected condition then immediately placed the valve in its proper position to meet the Technical Specification requirements.

This event is being reported pursuant to 10 CFR 50.73(a)(2)(v)(D) and 10 CFR 50.73(a)(2)(i)(B).

05000528/LER-2013-002Palo Verde8 April 2013Inoperable Systems Due to Defective Relays Reported under Part 21

This LER reports the failure of components caused by a defect in ARD66OUR control relays reported by Westinghouse, pursuant to 10 CFR 21, on April 8, 2013. The defect resulted in the failure of five normally energized control relays at PVNGS in two different systems in Unit 1 and two different systems in Unit 2.

The relays were used in normally energized applications which are de-energized to position associated components to support the related safety function. The relays failed to change state when de-energized during testing.

The five failed relays were replaced. The cause was a change in the manufacturing process that occurred in May 2008. The defect was exhibited only on relays that failed in the manner described in the Westinghouse Part 21 report. An extensive testing program was completed to identify and replace ARD66OUR relays installed at PVNGS that exhibited the described failure mode. Westinghouse has modified the ARD66OUR relay plastic molding process to preclude this described failure mode. LER 05000529 / 2009-002-00 reported ARD66OUR relay failures that exhibited a similar failure mode.