6-8-2015 | On March 3, 2015, while in Mode 5 (cold shutdown) for a refueling outage, during performance of 3-PT-R200 (Essential Service Water Header Flow Balance) the As-Found service water ( SW) flow rates for the 31 Fan Cooler Unit (FCU), 32 FCU and 33 FCU were less than the Technical Specification (TS) 3.6.6 ( Containment Spray and Containment Fan Cooler System) Surveillance Requirement (SR) 3.6.6.3 flow of 1430 gpm.
The SW essential header was re-balanced by adjusting FCU throttle valves to obtain a minimum of 1430 gpm for all five FCUs. On April 9, 2015, an engineering review of test data recorded from test 3-PT-R200, determined that the quarterly test (3-PT-Q016) that verifies FCU flows is not performed in the correct alignment for validating SW flow for the FCUs per TS SR 3.6.6.3.
Test 3-PT-Q016 tests SW flow through FCU with SW isolated through the Emergency Diesel Generator (EDG) coolers.
This configuration is not consistent with post accident operation in which SW is aligned to the FCUs and EDGs.
The apparent cause was improper implementation of improved TS requirements.
Corrective action was a revision of procedure 3-PT-Q016 to require validation of FCU SW flow with the EDG SW flow control valves and FCU outlet temperature control valves open.
The event had no significant effect on public health and safety. |
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LER-2015-003, Buchanan, N.Y. 10511-0249
Tel (914) 254-6700
Lawrence Coyle
Site Vice President
NL-15-065
June 8, 2015
U.S. Nuclear Regulatory Commission
Document Control Desk
11545 Rockville Pike, TWFN-2 Fl
Rockville, MD 20852-2738
SUBJECT: Licensee Event Report # 2015-003-00, "Technical Specification
Prohibited Condition Caused by Failure to Meet Containment Fan Cooler
Unit Service Water (SW) Flow Rate Due to Improper SW Surveillance
Test Configuration"
Indian Point Unit No. 3
Docket No. 50-286
DPR-64
Dear Sir or Madam:
Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby
provides Licensee Event Report (LER) 2015-003-00. The attached LER identifies an
event where containment fan cooler unit service water flow rates did not meet test
criteria as a result of improper test configuration, which is reportable under 10 CFR
50.73(a)(2)(i)(B) as a Technical Specification Prohibited Condition during past operation.
This condition was recorded in the Entergy Corrective Action Program as Condition
Report CR-IP3-2015-01063 and CR-IP3-2015-02448.
There are no new commitments identified in this letter. Should you have any questions
regarding this submittal, please contact Mr. Robert Walpole, Manager, Regulatory
Assurance at (914) 254-6710.
Sincerely,
fild-#44‘xe
LC/cbr
cc: Mr. Daniel H. Dorman, Regional Administrator, NRC Region I
NRC Resident Inspector's Office, Indian Point 3
Ms. Bridget Frymire, New York State Public Service Commission
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION
(01-2014)
LICENSEE EVENT REPORT (LER)
APPROVED BY OMB NO. 3150-0104 EXPIRES: 01/31/2017
Estimated burden per response to comply with this mandatory collection
request: 80 hours. Reported lessons learned are incorporated into the
licensing process and fed back to industry. Send comments regarding burden
estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S.
Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet
e-mail to infocollectssesource@nrc.gov, and to the Desk Officer, Office of
Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of
Management and Budget, Washington, DC 20503. If a means used to impose
an information collection does not display a currently valid OMB control
number, the NRC may not conduct or sponsor, and a person is not required to
respond to, the information collection.
1. FACILITY NAME: INDIAN POINT 3 2. DOCKET NUMBER
05000-286
3. PAGE
1 OF 5
4.TITLE:Technical Specification Prohibited Condition Caused by Failure to Meet Containment
Fan Cooler Unit Service Water (SW) Flow Rate Due to Improper SW Surveillance Test
ConfigurationIndian Point 3 |
Event date: |
4-9-2015 |
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Report date: |
6-8-2015 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident |
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2862015003R00 - NRC Website |
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Note: The Energy Industry Identification System Codes are identified within the brackets {}.
DESCRIPTION OF EVENT
On March 3, 2015, while in Mode 5 during shutdown for a refueling outage, the Operations test group commenced performance of 3-PT-R200 (Essential Service Water Header Flow Balance) at approximately 19:00 hours (this test was last performed in 1997). The purpose of the flow balance test is to verify accident Service Water (SW) {BI} flow rates are met for safety related components with the SW system in its design basis alignment. Performance of the test includes the use of Ultrasonic Flow Meters (UTs) installed on the Fan Cooler Unit (FCU) {FCU} SW outlet lines. The test acceptance criteria for minimum SW flow on the FCU discharge flow indicator is equal to or greater than 1575 gpm. The As-Found FCU outlet SW flow of 1575 gpm for the five Fan Cooling Unit (FCU) cooling coils could not be obtained during performance of 3-PT-R200. The As-Found SW flow rates for the 31 FCU, 32 FCU and 33 FCU were also less than the quarterly test [3-PT-Q016 (EDG and VC Temperature Valves SWN-FCV- 1176 and 1176A, and SWN-TCV-1104 and 1105)] acceptance criteria flow of 1430 gpm used to demonstrate operability in accordance with Surveillance Requirement (SR) 3.6.6.3 of Technical Specification 3.6.6 (Containment Spray and Containment Fan Cooler System). The test procedure (3-PT-R200) FCU SW flow rate of 1575 gpm is a bounding value for assumed worst case SWS condition and to provide margin over the required flow rate of 1430 gpm specified in surveillance procedure 3-PT-Q016 used to verify operability to the TS SR 3.6.6.3 value of equal to or greater than 1400 gpm.
Test acceptance criteria for FCU flows have a 30 gpm correction factor for instrument error. The test was stopped per the procedure and Engineering and test supervisor notified for further guidance. After review, engineering directed the test to continue and re-balancing performed to obtain a minimum FCU outlet SW flow.
of 1430 gpm. The test was resumed and the essential SW header was re-balanced by adjusting FCU throttle valves (SWN-44-1, SWN-44-2, SWN-44-3, SWN-4474, SWN-44-5) to obtain a minimum of 1430 gpm for all five FCUs. As-Left FCU outlet SW flow indications in the Safety Injection Mode were 1480, 1435, 1460, 1500 and 1496 gpm for 31 through 35 FCUs respectively. In the recirculation Mode, all FCU outlet SW flow indications were greater than 1575 gpm. The condition in which the As-found FCU outlet SW flow of 1575 gpm was not obtained in accordance with 3-PT-R200 was recorded in the Indian Point Energy Center (IPEC) Corrective Action Program (CAP) as Condition Report CR-IP3-2015-01063. Included in CR-IP3-2015-01063 was a corrective action for engineering to justify the acceptability of the SW flow balance FCU outlet flow test acceptance criteria reduction from 1575 gpm to 1430 gpm.
An engineering review of test data recorded from test 3-PT-R200 was performed and on April 9, 2015, engineering determined that the quarterly test (3-PT-Q016) is not performed in the correct alignment for validating SW flow for the FCUs per TS SR 3.6.6.3. Test 3-PT-Q016 tests SW flow through FCUs with SW isolated through the Emergency Diesel Generator (EDG) coolers. This configuration is not consistent with post accident operation in which SW is aligned to the FCUs and EDGs. A review of prior procedure revisions identified that a procedure revision was made to incorporate improved TS (ITS) surveillance requirements (3-PT-Q016 Revision 13 preparer approval dated March 8, 2001). Performance of FCU SW flow measurements was incorporated in the procedure after stroke testing of the EDG SW outlet valves whose position switch was returned to its normal position of AUTO. This position of EDG SW outlet valves causes the valves to close. A review of previous essential SW header flow balancing determined that the last documented essential SW header flow balance was performed in 1997 under ENG-281B. The condition in which the evaluation of test data recorded under SW flow balance test 3-PT-R200 discovered that the quarterly surveillance was not performed in the correct alignment was recorded in the IPEC CAP as Condition Report CR-IP3-2015-02448.
This normal position of the EDG flow control switch closes the flow control valves.
While the normal position of the EDG flow control valves is closed, they are designed to automatically open on receipt of a SI signal. Quarterly TS SR Testing of the FCU outlet flow with the EDG SW outlet valves closed results in higher FCU SW outlet flows than if the FCU outlet flows were measured with the EDG SW outlet valves open. Unlike the quarterly surveillance test, the SWS flow balance procedure (3-PT-R200) directs that the EDG SW outlet valves be open by placing the control switch in the OPEN position.
Corrective Actions
The following corrective actions have been performed under the Corrective Action Program (CAP) to address the causes of this event.
- Procedure 3-PT-Q016 was revised to perform FCU outlet SW flow with EDG cooling water valve SWN-FCV-1176 and SWN-FCV-1176A, and FCU outlet temperature control valve SWN-TCV-1104, and SWN-TCV-1105 in the full open position.
Event Analysis
The event is reportable under 10 CFR 50.73(a)(2)(i)(B). The licensee shall report any operation or condition which was prohibited by the plant's TS. This condition meets the reporting criteria because during past operation the SW flow through 3 of 5 FCUs did not meet required minimum FCU SW flow specified in TS SR 3.6.6.3 due to improper SWS flow balancing. Engineering discovered this condition on April 9, 2015, during their review of test data recorded in test 3-PT-R200.
The event is not reportable under 10CFR50.73(a)(2)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to (D) mitigate the consequences of an accident (safety system functional failure). An engineering calculation that evaluated fan cooler thermal performance during a LOCA under reduced SW cooling flow determined that with an average cooling water flow of 1330 gpm per FCU, the FCUs would still meet their heat removal requirement during a design basis LOCA. An engineering review of the As-Found FCU SW flows obtained from 3-PT-R200 determined the average as- found FCU flowrate from 3-PT-R200 corrected for instrument uncertainties was 1372 gpm. This flow rate takes into account failure of the containment fan cooler train associated with the highest as-found FCU flow (FCU 35). Since the average as-found FCU SW flow from 3-PT-R200 was greater than the average flow required to meet the design basis heat removal, the safety function would have been met.
Past Similar Events
A review was performed of the past three years of Licensee Event Reports (LERs) for events that involved TS prohibited conditions due to inadequate FCU SW flow capability. No LERs were identified.
Safety Significance
This event had no significant effect on the health and safety of the public. There were no actual safety consequences for the condition because there were no accidents, transients or seismic events during the time of the condition.
The Containment Spray System and Containment Fan Cooler System limit the temperature and pressure that could be experienced following a DBA. The limiting DBAs are the loss of coolant accident (LOCA) and the steam line break (SLB). No DBAs are assumed to occur simultaneously or consecutively.
The postulated DBAs are analyzed with regard to containment engineered safety features (ESF) systems, assuming the loss of one safeguards power train, which is the worst case single active failure and results in one train of Containment Spray and Containment Fan Coolers being rendered inoperable. Accident analysis results show that containment air cooling and iodine removal are met by one containment spray train and two fan cooler trains (i.e., four FCUs).
An engineering calculation (Calculation No. 83990.003-8-SW-209) evaluated fan cooler thermal performance during a LOCA under reduced SW cooling flow conditions.
Under the case of maximum fouling in the FCUs, the calculation determined that with an average cooling water flow of 1330 gpm per FCU, the FCUs would still meet the design basis heat removal rate assuming maximum fouling (a tube fouling factor of 0.004, and 4 percent tube plugging). An engineering review of the As-Found FCU SW flows obtained from 3-PT-R200 determined the average as-found FCU flowrate from 3- PT-R200 corrected for instrument uncertainties was 1372 gpm. This flow rate takes into account failure of the containment fan cooler train associated with the highest as-found FCU flow (FCU 35). Since the average as-found FCU SW flow from 3- PT-R200 was greater than the average flow required to meet the design basis heat removal, the safety function would have been met.
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05000286/LER-2015-001, Safety System Functional Failure Due to Inoperable Refueling Water Storage Tank Level Alarms Due to Freezing of the Level Instrument Sensing Lines Caused by a Failed Strip Heater | Safety System Functional Failure Due to Inoperable Refueling Water Storage Tank Level Alarms Due to Freezing of the Level Instrument Sensing Lines Caused by a Failed Strip Heater | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000286/LER-2015-001 | Safety System Functional Failure Due to Inoperable Refueling Water Storage Tank Level Alarms Due to Freezing of the Level Instrument Sensing Lines Caused by a Failed Strip Heater | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000247/LER-2015-001 | Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for Containment LER 15-001-02 for Indian Point, Unit 2, Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for Containment | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2015-002 | Safety System Functional Failure Due to Fuses for Residual Heat Removal Heat Exchanger Outlet Valves That Would Not Remain Operable Under Degraded Voltage Conditions | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000286/LER-2015-002 | Technical Specification Prohibited Condition Caused by Four Main Steam Safety Valves .Outside Their As-Found Lift Set Point Test Acceptance Criteria | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2015-003 | Manual Reactor Trip Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to a Power Supply Failure LER 15-003-00 for Indian Point, Unit 2, Regarding Manual Reactor Trip Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to a Power Supply Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000286/LER-2015-003 | Buchanan, N.Y. 10511-0249 Tel (914) 254-6700 Lawrence Coyle Site Vice President NL-15-065 June 8, 2015 U.S. Nuclear Regulatory Commission Document Control Desk 11545 Rockville Pike, TWFN-2 Fl Rockville, MD 20852-2738 SUBJECT: Licensee Event Report # 2015-003-00, "Technical Specification Prohibited Condition Caused by Failure to Meet Containment Fan Cooler Unit Service Water (SW) Flow Rate Due to Improper SW Surveillance Test Configuration" Indian Point Unit No. 3 Docket No. 50-286 DPR-64 Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2015-003-00. The attached LER identifies an event where containment fan cooler unit service water flow rates did not meet test criteria as a result of improper test configuration, which is reportable under 10 CFR 50.73(a)(2)(i)(B) as a Technical Specification Prohibited Condition during past operation. This condition was recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2015-01063 and CR-IP3-2015-02448. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. Robert Walpole, Manager, Regulatory Assurance at (914) 254-6710. Sincerely, fild-#44‘xe LC/cbr cc: Mr. Daniel H. Dorman, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Ms. Bridget Frymire, New York State Public Service Commission NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (01-2014) LICENSEE EVENT REPORT (LER) APPROVED BY OMB NO. 3150-0104 EXPIRES: 01/31/2017 Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollectssesource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME: INDIAN POINT 3 2. DOCKET NUMBER 05000-286 3. PAGE 1 OF 5 4.TITLE:Technical Specification Prohibited Condition Caused by Failure to Meet Containment Fan Cooler Unit Service Water (SW) Flow Rate Due to Improper SW Surveillance Test Configuration | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2015-004 | Safety System Functional Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe LER 15-004-00 for Indian Point 2 Regarding Safety System Functional Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2015-004 | Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by a Failure of the 31 Main Transformer LER 15-004-01 for Indian Point Unit No. 3 Regarding Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by a Failure of the 31 Main Transformer | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2015-005 | Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by the Trip of 345kV Main Generator Output Breaker 3 due to a Failure of South Ring Bus 345kV Breaker 5 LER 15-005-01 for Indian Point 3 RE: Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by the Trip of 345kV Main Generator output Breaker 3 due to a Failure of South Ring Bus 345kV Breaker 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2015-006 | Technical SpecificatiOn Prohibited Condition Due to Two Pressurizer Code Safety Valves Discovered Outside their As-Found Lift Setpoint Test Acceptance Criteria LER 15-006-01 for Indian Point Unit No. 3 Regarding Technical Specification Prohibited Condition Due to Two Pressurizer Code Safety Valves Discovered Outside Their As-Found Lift Setpoint Test Acceptance Criteria | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000286/LER-2015-007 | Manual Reactor Trip Due to Decreasing Steam Generator Water Levels Caused by a Miss- Wired Circuit Board in the Main Feedwater Pump Speed Control System LER 2015-007-01 for Indian Point, Unit 3 Regarding Manual Reactor Trip Due to Decreasing Steam Generator Water Level Caused by a Miss-Wired Circuit Board in the Main Feedwater Pump Speed Control System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | 05000286/LER-2015-008 | Automatic Reactor Trip Due to a Turbine-Generator Trip as a Result of a Fault on 345 kV Feeder W96 Tower Lines Caused by Pre-Existing Degraded Insulator LER 15-008-00 for Indian Point, Unit 3, Regarding Automatic Reactor Trip Due to a Turbine-Generator Trip as a Result of a Fault on 345 kV Feeder W96 Tower Lines Caused by Bird Streaming | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
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