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 Start dateReporting criterionEvent description
05000362/LER-2013-001

On October 23, 2012, during engineering walkdowns, the hydraulic fluid in the level sight glass of the San Onofre Nuclear Generating Station (SONGS) Unit 3 Train A Emergency Diesel Generator (EDG) governor actuator was found with an abnormal color (purple) and higher than normal indicated level.

On November 27, 2012, during subsequent investigation, additional reliable and substantive information including physical evidence was identified that supported a reason to believe (at that time) that tampering may have caused the abnormal condition. This event was reported as a one- hour notification to the NRC in accordance with 10 CFR 73, Appendix G, 1(a)(3). Subsequently, while tampering could not be confirmed, it also could not definitively be ruled out as a possible cause. As such, this followup 60-day written report is being submitted.

This event did not affect plant operation or safety, since the EDG was out of service and not required to be operable during the period of time the governor actuator hydraulic fluid was contaminated.

Unit 3 has been shutdown since January 31, 2012, due to an unrelated event.

05000362/LER-1998-012, Forwards LER 98-012-01 Re Occurrence Involving CCS RPV Being Set Above Required Relief Setpoint.Any Actions Listed Are Intended to Ensure Continued Compliance with Existing Commitments as Discussed in Applicable Licensing Docum29 September 1998
05000362/LER-1997-004, Forwards LER 97-004-00 for Occurrence Involving Typo in Ts. Health & Safety of Public or Plant Personnel Was Not Affected5 January 1998
05000362/LER-1997-003, Forwards LER 97-003-00 Re Out of Tolerance Condition Identified During Testing of Pressurizer Safety Valve Setpoints.Neither Health Nor Safety of Plant Personnel or Public Affected by Occurence19 January 1998
05000362/LER-1997-002, Forwards LER 97-002-00 Re Occurrence Involving RCS Pressure Boundary Leakage,Per 10CFR50.73(d)30 July 1997
05000362/LER-1996-001, Forwards Supplemental LER 96-001-01,providing Addl Info on Safety Significance of Occurrence Involving Inadvertent ESFs Actuation2 May 1996
05000362/LER-1995-001, Forwards LER 95-001 for Discovery of Minor RCS Pressure Boundary Weepage Which Occurred During Cycle 7 Operation. Neither Public Health Nor Safety of Plant Personnel or Public Affected by Occurrence23 August 1995
05000362/LER-1993-006, Forwards RCE-94-002, Reactor Coolant Pump 3P002 Mechanical Seal Failure, as Committed in LER 93-006,dtd 9401128 March 1994
05000362/LER-1986-015, Forwards Evaluation of Reported High Exposure to Extremity TLD 80365 in Oct 1986, Per LER 86-015-013 March 1987
05000362/LER-1984-045, Forwards LER 84-045-00 for 1984 & 85 Occurrences Re Dose Equivalent Iodine Concentrations That Exceeded TS Limits,But Were Not Reported as Required by TS in Effect at That Time. Healt Nor Safety of Plant Personnel or Public Was3 March 1998
05000362/LER-1984-009, Forwards LER 84-009-011 June 1984
05000362/LER-1983-097, Revised LER 83-097/03L-1:on 831029 & 30,control Element Assembly (CEA) 57 Dropped More than 19 Inches & CEA 61 Dropped More than 19 Inches on 831101.Caused by Sluggishness of CEA Grippers20 January 1984
05000362/LER-1983-073, /03L-0:on 830929,boronmeter 3AE0203 Rendered Inoperable When Manual Isolation Valves S31208MU084 & S31208MU091 Closed.Caused by Improper Sys Lineup.Corrective Actions Described in LER 83-073/03L-027 October 1983
05000362/LER-1983-065, Corrected LER 83-065/03L-0:on 830905 & 12,high-range in-containment Radiation Monitor 3RI-7820-1 Declared Inoperable After Discovery in Failed Low Condition.Caused by Faulty Electrical Cable Penetration Path5 October 1983
05000362/LER-1983-036, Forwards Updated LER 83-036/03X-1 & LER 83-042/03L-0. Detailed Event Summary Submitted8 August 1983
05000362/LER-1983-035, Forwards LER 83-035/03L-03 May 1983
05000362/LER-1983-033, Forwards LER 83-033/03L-03 May 1983
05000362/LER-1983-027, Forwards LER 83-027/03L-06 April 1983
05000362/LER-1983-026, Forwards LER 83-026/03L-06 April 1983
05000362/LER-1983-024, Forwards LER 83-024/03L-01 April 1983
05000362/LER-1983-022, Forwards LER 83-022/01T-018 March 1983
05000362/LER-1983-021, Forwards LER 83-021/03L-02 March 1983
05000362/LER-1983-020, Forwards LER 83-020/01T-017 March 1983
05000362/LER-1983-019, Forwards LER 83-019/03L-017 February 1983
05000362/LER-1983-018, Forwards LER 83-018/03L-023 February 1983
05000362/LER-1983-017, Forwards LER 83-017/03L-07 March 1983
05000362/LER-1983-016, Forwards LER 83-016/03L-09 March 1983
05000362/LER-1983-012, Forwards LER 83-012/03L-022 February 1983
05000362/LER-1983-009, Forwards LER 83-009/03L-01 March 1983
05000362/LER-1983-008, Forwards LER 83-008/03L-022 February 1983
05000362/LER-1983-007, Forwards LER 83-007/03L-018 February 1983
05000362/LER-1983-006, Forwards LER 83-006/01T-015 March 1983
05000362/LER-1983-005, Forwards LER 83-005/01T-011 March 1983
05000362/LER-1983-004, Forwards LER 83-004/03L-017 February 1983
05000362/LER-1983-003, Forwards LER 83-003/03L-017 February 1983
05000362/LER-1983-002, Forwards LER 83-002/03L-017 February 1983
05000362/LER-1983-001, Forwards Revised LER 83-001/03X-13 March 1983
05000362/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Submitted28 January 1983
05000362/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Submitted31 January 1983
05000362/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted14 January 1983
05000362/LER-1982-006, Ro:On 821217,incident Involving Emergency Safety Features Actuation Signal Occurred.Written Followup Rept W/Interim LER 82-006 Will Be Submitted by 82122827 December 1982
05000362/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Submitted27 December 1982
05000362/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted17 December 1982
05000362/LER-1950-362, Clarifies Corrective Actions Taken by Util to Prevent Recurrence of Reactor Trips During Startup as Ref in LER 50-362/86-06 on 860413.Procedure SO123-V-4.22 Revised to Require Changes Approved by Supervising Engineer30 September 1986
05000361/LER-1999-005, Forwards 30-day follow-up LER 99-005-00,describing Loss of Physical Train Separation in Control Room.Any Actions Listed Intended to Ensure Continued Compliance with Existing Commitments23 September 1999
05000361/LER-1999-004, Forwards LER 99-004-00 Re Automatic Tgis Actuation.Event Affected Units 2 & 3 Equally Because Tgis Is Shared Sys. Single Rept Is Being Provided for Unit 2 IAW NUREG-1022, Rev 1.No New Commitments Are Contained in Encl6 August 1999
05000361/LER-1999-003, Forwards LER 99-003-00 Re Inoperability of Ccws non-critical Loop Isolation Valves Due to Previously Unrecognized Instrument Air Configuration Anomaly.Single Rept for Unit 2 Is Being Submitted IAW NUREG-1022,rev 112 March 1999
05000361/LER-1998-025, Forwards LER 98-025-00,re Occurrence Involving MSSV Setpoints.Actions Listed Are Intended to Ensure Continued Compliance with Existing Commitments.No New Commitments Made29 January 1999
05000361/LER-1998-024, Forwards LER 98-024-00 Re Occurrence Involving Creacs Boundary Control During HVAC Component Maint.Single Rept for Unit 2 Is Being Submitted IAW NUREG-1022,rev 19 December 1998
05000361/LER-1998-023, Provides 30-day Written LER 98-023-00 for Occurrence Involving Surveillance of Portions of Fire Detection Circuits Located Inside Containment Bldg19 November 1998