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 Start dateReporting criterionEvent description
05000423/LER-2019-00113 February 2020
05000423/LER-2017-00120 January 2017
20 March 2017
10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
At 0835 on January 20, 2017 while operating in MODE 1 at 100% power, a door in the auxiliary building at Millstone Power Station Unit 3 failed to fully close following personnel passage due to the failure of the mechanical door closer mechanism. This door is part of the secondary containment boundary which must be intact for the supplemental leak collection release system to perform its safety function. Operators determined that the condition of the door rendered secondary containment inoperable and resulted in a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material and mitigate the consequences of an accident. The door was repaired and the door completely closed at 1256 on January 20, 2017. This condition is being reported under 10 CFR 50.73(a)(2)(v)(C) and 10 CFR 50.73(a)(2)(v)(D).
05000423/LER-2016-00512 June 2016
9 August 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

On June 12, 2016, with Millstone Power Station Unit 3 operating in MODE 1 at 100% power, operators identified the third stage of the "A" Reactor Coolant Pump (RCP) seal had failed, which resulted in an unidentified Reactor Coolant System leak greater than the Technical Specification (TS) limit of 1 gallon per minute. Operators initiated a plant shutdown as required by TS 3.4.6.2 ACTION Statement b. During the downpower, steam generator levels were not adequately maintained and the Engineered Safety Features Actuation System generated a Turbine Trip and Feed Water Isolation on Steam Generator Water Level - High-High being exceeded on the 'B' steam generator.

In response, operators manually tripped the reactor at 23:37 (MODE 1, at approximately 20 % power). The auxiliary feedwater system started as designed.

Safety systems functioned as expected. There were no radiological challenges as a result of the event. The plant entered COLD SHUTDOWN on June 14, 2016 at 01:29.

The cause of the unidentified leak was a failed third stage on the "A" RCP seal. The seal was replaced.

The cause of the feedwater transient and resultant manual reactor trip was due to operator performance in controlling steam generator level. This is being addressed in the Corrective Action Program.

This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in manual or automatic actuation of systems listed in 10 CFR 50.73(a)(2)(iv)(B). Additionally, the plant shutdown is being reported in accordance with 10 CFR 50.73 (a)(2)(i)(A) as the completion of any nuclear plant shutdown required by the plant's Technical Specifications.

05000423/LER-2016-00415 May 2016
13 July 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 15, 2016, with Millstone Power Station Unit 3 (MPS3) operating in MODE 1 at 74% power, the operators observed decreasing hydrogen pressure in the main turbine generator. Upon field investigation it was determined there was an active hydrogen leak from the main generator. The operators manually tripped the reactor and vented the hydrogen from the main generator. The reactor trip was uncomplicated. The auxiliary feedwater (AFW) pumps started as designed on low steam generator level and operators maintained steam generator level.

The active hydrogen leak was the direct cause of the manual reactor trip. The hydrogen leak was caused by a dislodged plug on a port on the main generator. MPS maintenance procedures did not contain adequate procedural guidance in that there was no specific direction for installation, i.e., torque value and verifications. The procedures will be revised to include specific direction to tighten the plugs and applicable verifications (i.e., torque value, peer checking). Additional corrective actions are being taken in accordance with the station's corrective action program.

The actuation of the RPS and the automatic start of the AFW pumps is being reported in accordance with 10 CFR 50.73 (a)(2)(iv)(A) as an event that resulted in manual or automatic actuation of systems listed in 10 CFR 50.73(a)(2)(iv)(B).

05000423/LER-2016-0039 April 2016
8 June 2016
10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

(MPS3) performed the 'B' train Supplementary Leak Collection and Release System (SLCRS) Negative Pressure Verification Surveillance. This test was completed with unsatisfactory results. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.6.1 was entered. Later, on April 9, 2016, with the reactor in MODE 1 and approximately 24 percent power, MPS3 operators conducted the 'A' train SLCRS Negative Pressure Verification Surveillance with unsatisfactory results. Because both trains of SLCRS failed the required surveillances, TS LCO 3.6.6.2 was entered. Operations continued with the planned plant shutdown associated with the RFO and entered COLD SHUTDOWN, MODE 5 at 1241 on April 10, 2016.

SLCRS did not meet the acceptance criteria due to the aggregate impact of a number of dampers not providing effective isolation.

SLCRS was restored to operable condition prior to entering MODE 4 when starting back up from RF017. Detailed procedural steps are being developed for verifying the closed position of SLCRS isolation dampers and being incorporated into the damper post maintenance testing matrix. Associated surveillance procedures are being revised to improve monitoring program for SLCRS isolation dampers.

Since both trains of SLCRS failed to meet TS acceptance criteria, this condition is reportable pursuant to 10CFR50.73(a)(2)(v)(C) as a condition that could have prevented the fulfillment of a safety function for systems or structures to control the release of radioactive material, and 10CFR50.73(a)(2)(v)(D) to mitioate the consequences of an accident.

05000423/LER-2016-00225 January 2016
23 March 2016
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On January 25, 2016 an automatic reactor trip occurred on Millstone Power Station Unit 3 (LER 2016-001-00). Following the Millstone Power Station Unit 3 reactor trip, (Mode 3, 0% power), while operators were performing feedwater isolation actuation verification steps, it was identified that the 'C' Feedwater Isolation Valve, 3FWS*CTV41C, did not auto-close as expected. Operators subsequently closed 3FWS*CTV41C from the control room.

Troubleshooting identified that a temporary jumper, associated with a maintenance activity completed in November 2014, was inadvertently left installed due to a human performance error. This jumper bypassed the input from the Solid State Protection System to isolate 3FWS*CTV41C upon receipt of an actuation signal. This input is required by Technical Specification 3.3.2 and Table 3.3-3, Engineered Safety Features Actuation System Instrumentation. The function to automatically isolate 3FWS*CTV41C was thus defeated. However, the safety function to isolate feedwater was met due to redundant valves in series that operated correctly via the 'C' feed regulating valve and the 'C' feed regulating bypass valves. Also, the containment isolation function was not lost as the valve, 3FWS*CTV41C, was capable of remote operation from the control room.

This condition is reportable in accordance with 10 CFR 50.73 (a)(2)(i)(B) as any operation or condition that is prohibited by the plant's Technical Specifications. The jumper was removed and the valve was verified to be OPERABLE.

05000423/LER-2016-00125 January 2016
16 March 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation
05000423/LER-2015-00119 February 201510 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

On February 19, 2015, with Millstone Power Station Unit 3 (MPS3) at 100% power and in operating mode 1, an individual on a fire watch rove processed through a dual train high energy line break (HELB) door normally and upon checking the door after passage the individual noted the door did not latch. The Control Room was promptly notified./ An operator was dispatched to investigate. The operator exercised the door lock-set mechanism freeing the latch allowing the door to properly latch. The door was inoperable for approximately 7 minutes. Technical Specification 3.0.3 was entered and exited appropriately.

Although no definite failure mechanism was identified, the door was experiencing high usage due to compensatory fire watch roves entering/exiting the door. The door lockset mechanism was manually manipulated and then tested several times satisfactorily by maintenance personnel. Further, the door design has the door swing such that the HELB event would act to open the door when the lockset mechanism fails. Engineering is evaluating the adequacy of the preventive maintenance frequency. Additionally, a design change to reverse the door swing such that the HELB event would cause the door to close and thus not rely on the lock-set mechanism is being considered. Additional corrective actions are being taken in accordance with the station's corrective action program.

This event is being reported pursuant to 10 CFR 50.73(a)(2)(v)(D), as a condition that could have prevented the fulfillment of a safety function for systems needed to mitigate the consequences of an accident.

05000423/LER-2014-00310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On May 1, 2014 with Millstone Power Station Unit 3 in operating mode 1 and 100% reactor power, an evaluation determined the installation of an incorrect vendor supplied bearing introduced a non-conforming condition, which over time and under certain variable conditions, resulted in excessive friction affecting the ability of the turbine driven auxiliary feedwater (TDAFW) pump to operate properly and could render it inoperable. Plant Technical Specification 3.7.1.2 Action c, requires, if one auxiliary feedwater pump is inoperable in operating modes 1, 2, and 3, the pump must be returned to operable status within 72 hours, or the plant be placed in at least hot standby within six hours and in hot shutdown within the following 12 hours.

An investigation determined the installation of an incorrect bearing in the TDAFW pump steam supply valve control linkage during refueling outage 3R15 (spring of 2013) caused a discrepant condition rendering the TDAFW pump inoperable for periods of time exceeding the limiting conditions for operations action statement for TS 3.7.1.2. The bearing manufacturer issued a 10 CFR 21 report on this issue. (ADAMS accession # ML14079A353).

The incorrect bearing was replaced, the governor and associated linkage were groomed/adjusted, and the TDAFW pump was tested satisfactorily. Additional corrective actions are being taken in accordance with the station's corrective action program.

This condition is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B), any operation or condition which was prohibited by the plant's TS.

05000423/LER-2014-00212 March 201410 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

While Millstone Power Station Unit 3 (MPS3) was operating at 100 percent power in Mode 1 on March 12, 2014, operations determined that a concern identified by Engineering as a result of recent industry operating experience (NRC Event Number 49889) could result in an unanalyzed condition. Engineering's review of the direct current (DC) circuits associated with the main turbine emergency lube oil and main generator emergency seal oil pumps determined the described condition to be applicable to MPS3.

This condition is reportable pursuant to 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly degraded plant safety. A prompt notification per EN49903 was submitted to the NRC on March 12, 2014.

The cause of the condition was a manufacturer's design error that was installed during plant construction.

Compensatory fire watches have been implemented for affected areas of the plant. Plant modifications are planned that will protect or isolate the affected circuits leaving the initial fire area.

05000423/LER-2013-00210 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On January 28, 2013 with Millstone Power Station Unit 3 (MPS3) in MODE 1 at 100% power, engineering completed a maintenance rule evaluation of a previously identified condition where a roll-up door in the auxiliary building at MPS3 was found not fully closed after a security test. The door was open approximately 3/8 of an inch.

This door is a secondary containment boundary, specifically a supplemental leak collection release system boundary. Engineering concluded the partially open roll-up door exceeded any available margin from the previous surveillance drawdown test. Additionally, during the investigation it was determined the door had been in the partially open condition in excess of the plant's Technical Specification Action Statement (TSAS) allowed outage time.

The direct cause of the event was the door had not been fully closed after completion of security testing. Upon discovery the door was unlocked, fully closed and relocked. The testing procedure has been changed to test the door without requiring the door to be opened. Additional corrective actions are being taken in accordance with the station's corrective action program.

This condition is being reported under 10 CFR 50.73(a)(2)(v)(C) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material. Additionally, since the secondary containment boundary was not re-established within the requirements of the TSAS (24 hours) this it is also being reported under 10 CFR 50.73(a)(2)(i)(B) as any operation or condition which was prohibited by the plant's Technical Specifications.

05000423/LER-2013-00119 February 201310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On February 15, 2013, with Millstone Power Station Unit 3 operating in MODE 1 at 100 percent power, operators discovered that the insulating cover installed over 3MSS*PT526, "B" Steam Generator Pressure Transmitter (SGPT) Channel 3, was not properly secured. When found, it was incorrectly assessed as not impacting equipment operability. However, on February 19, 2013, upon further review by the Electrical Equipment Qualification program engineer, it was determined that the SGPT would not be adequately protected from a postulated high energy line break (HELB). Therefore, 3MSS*PT526 was declared inoperable per Technical Specification (TS) 3.3.2, Engineered Safety Features Instrumentation, on February 19, 2013. Information exists that 3MSS*PT526 was inoperable on February 15, 2013, when the problem was initially discovered. Since the condition existed for longer than allowed by TS 3.3.2, Action 20 (i.e., for more than six hours without the bistable being placed in trip), this is a reportable condition per 10 CFR 50.73 (a)(2)(i)(B) as an event or condition which was prohibited by the plant's Technical Specifications.

Lack of awareness of the purpose of the enclosure boundary combined with the lack of clear labeling identifying the HELB enclosure resulted in a delay in declaring the equipment inoperable. Operations created and installed a new label for the insulating box around each SGPT clearly indicating the box is a HELB barrier and is part of the environmental qualification boundary.

05000423/LER-1999-006, Forwards LER 99-006-00,re Failure of Both Reactor Plant Aerated Drains SR Air Driven Sump Pumps During Technical Requirements Manual Surveillance on 990516.Commitments Also Encl15 June 1999
05000423/LER-1999-005, Forwards LER 99-005-00,re Failure to Perform Surveillance on RCS Pressurizer Heater Penetration Breakers,Determined Reportable on 990510.Commitments Made,Encl8 June 1999
05000423/LER-1998-045, Forwards LER 98-045-00,re Rt Due to MSIV Closure During Partial Stroke Testing Due to Solenoid Valve Failure on 981211.Commitments,encl11 January 1999
05000423/LER-1998-044, Forwards LER 98-044-00,re Rt Due to High Differential Pressure Between a & B Condensers on 981111.Util Commitments in Response to Event Contained within Attachment 1 of Ltr10 December 1998
05000423/LER-1998-043, Forwards LER 98-043-00,re Manual Rt Due to High Conductivity in Condensate Sys.Commitments Made by Util,Encl25 November 1998
05000423/LER-1998-042, Forwards LER 98-042-00,re Licensing & Design Basis Review of Lpms Which Identified That TS Definition of Acot Was Not Met.Determined Event Reportable on 981020.Special Rept Dtd 980909,is Supplemented.Commitments Included in Att19 November 1998
05000423/LER-1998-041, Forwards LER 98-041-00,re Failure to Enter Action Statement for Inoperable SG Water Level Channel IAW TSs on 981016. Commitments Made by Util Also Encl16 November 1998
05000423/LER-1998-040, Forwards LER 98-040-00,documenting Condition That Was Determined Reportable on 981017.Attachment 1 Contains Commitments Made in Response to Event13 November 1998
05000423/LER-1998-039, Forwards LER 98-039-00,documenting Event That Occurred on 981001 at Millstone Unit 3.Commitments Made by Util,Encl2 November 1998
05000423/LER-1998-038, Forwards LER 98-038-00 Re Manual Rt Due to High Conductivity in Condensate Sys on 980915.Commitments Made by Util,Encl15 October 1998
05000423/LER-1998-037, Forwards LER 98-037-00,re TS 3.0.3 Entry Due to Both SW Trains Declared Inoperable Following Failure of Check Valves Associated with Injection of Sodium Hypochlorite on 980910 & 18.Util Commitments Contained in Attachment 1 to13 October 1998
05000423/LER-1998-036, Forwards LER 98-036-00,which Discusses ESF Bldg Sump Pump Design Deficiencies.Commitments Made in Rept,Encl6 August 1998
05000423/LER-1998-035, Forwards LER-98-035-00,documenting Condition That Was Determined Reportable on 980612.Attachment 1 Contains Commitments to Ltr13 July 1998
05000423/LER-1998-034, Forwards LER 98-034-00,documenting Condition,Determined Reportable at Millstone Unit 3 on 980614.Util Commitments in Response to Event Contained within Attachments 1 to Ltr13 July 1998
05000423/LER-1998-033, Forwards LER 98-033-00,re Event Determined Reportable at Millstone Unit 3 on 980610.Commitments Made within Ltr,Encl10 July 1998
05000423/LER-1998-032, Forwards LER 98-032-00,re Event Determined Reportable at Millstone Unit 3 on 980618.Commitments Made within Ltr,Encl17 July 1998
05000423/LER-1998-031, Forwards LER 98-031-00,re Event Which Was Determined Reportable on 980526.Commitments Made within Ltr,Encl23 June 1998
05000423/LER-1998-030, Forwards LER 98-030-00,documenting Condition Determined Reportable at Mnps,Unit 3,on 980515.Commitments Made by Util Are Contained in Attachment 1 to Ltr15 June 1998
05000423/LER-1998-029, Forwards LER 98-029-00,supplementary Leak Collection & Release Sys Bypass Leakage May Result in Unaccounted Control Room & TSC Doses.Attachment 1 Contains Commitments Made in Ltr11 June 1998
05000423/LER-1998-028, Forwards LER 98-028-00,documenting Condition Determined Reportable at Unit 3 on 980513.Util Commitments in Response to Event Contained within Attachment 1 to Ltr12 June 1998
05000423/LER-1998-027, Forwards LER 98-027-00 Which Notes That Unmonitored Flowpath for Safety Injection Pump Cooling Pumps May Prevent Detection of Pump Degradation.Commitments,Encl26 June 1998
05000423/LER-1998-026, Forwards LER 98-026-00,documenting Condition Determined Reportable at Mnps,Unit 3 on 980416.Commitments Made by Util,Encl26 May 1998
05000423/LER-1998-025, Forwards LER 98-025-00,documenting Event at Millstone Unit 3 on 980427,per 10CFR50.73(a)(2)(i)(B).Commitments Made within Ltr,Encl26 May 1998
05000423/LER-1998-024, Forwards LER 98-024-00, Failure to Complete Action Associated W/Ts 4/3.3.1 within Required Time Period. Commitments Made by Util,Encl1 May 1998
05000423/LER-1998-023, Forwards LER 98-023-00,documenting Condition That Determined Reportable at Millstone Unit 3 on 980411.Util Commitments in Response to Event Contained within Attachment 1 to Ltr9 May 1998
05000423/LER-1998-022, Forwards LER 98-022-00,documenting Condition That Determined Reportable at Millstone Unit 3 on 980408.Util Commitments in Response to Event Contained within Attachment 1 to Ltr8 May 1998
05000423/LER-1998-021, Forwards LER 98-021-00,documenting Condition Determined Reportable at Millstone,Unit 3,on 980318.Commitments Made by Util,Encl17 April 1998
05000423/LER-1998-020, Forwards LER 98-020-00,documenting Condition Determined Reportable at Millstone,Unit 3,on 980320.Commitments Made by Util,Encl13 April 1998
05000423/LER-1998-019, Forwards LER 98-019-00,documenting Condition Determined Reportable at Unit 3 on 980313.Util Commitments in Response to Event Contained within Attachment 1 to Ltr13 April 1998
05000423/LER-1998-018, Forwards LER 98-018-00,documenting Condition That Was Determined Reportable on 980302.Attachment 1 Contains Commitments in Response to Event1 April 1998
05000423/LER-1998-017, Forwards LER 98-017-00,re Condition That Occurred at Millstone Unit 3 on 980227.Commitments Made in Rept,Encl27 March 1998
05000423/LER-1998-016, Forwards LER 98-016-01,determined Reportable at Millstone Unit 3 on 980223,per 10CFR50.73(a)(2)(vii).Commitments Made within Ltr,Encl18 May 1998
05000423/LER-1998-015, Forwards LER 98-015-00,documenting Condition Determined Reportable at Unit 3 on 980221.Util Commitments in Response to Event Contained within Attachment 1 to Ltr19 March 1998
05000423/LER-1998-014, Forwards LER 98-014-00,failure to Provide Weepholes in Conduits & Junction Boxes Per 10CFR50.73(a)(2)(ii)(B). Attachment 1 Contains Commitments in Response to Event23 March 1998
05000423/LER-1998-013, Forwards LER 98-013-00,documenting Condition Determined Reportable at Millstone,Unit 3,on 980219 Re TS Required Sampling During Mode 5 Not Being Completed for SG Drain Down.Util Commitments in Response to Event Also Encl20 March 1998
05000423/LER-1998-012, Forwards LER 98-012-01,documenting Addl Info Pertaining to Condition That Was Determined Reportable on 980218. Attachment 1 Contains Commitments in Response to Event31 August 1998
05000423/LER-1998-011, Forwards LER 98-011-00,re Failure to Adequately Test Driven AFW Pump at Fixed Speed & Test Position Indication of Two Valves Per Section XI of ASME Code.Commitments,Encl14 March 1998
05000423/LER-1998-010, Forwards LER 98-010-00,documenting Condition That Was Determined at Millstone,Unit 3 on 980214.Util Commitments Provided in Ltr,Encl13 March 1998