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 Start dateReporting criterionEvent description
05000296/LER-2017-00229 December 201710 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

On November 1, 2017, at approximately 1425 Central Daylight Time, during an extent of condition review, a 4kV Shutdown Boards (SD BD) do not selectively coordinate with upstream 0.5 amp primary fuses for fault currents greater than 30 amps on the 120 V secondary. Cable fire damage could cause an affected SD BD to spuriously disconnect from off-site power, and could cause a spurious, maintained under-voltage trip signal. The under-voltage trip signal would prevent motor load operation on the board whether on off-site 4kV SD BDs could be affected. In fire area 21, 4kV SD BDs 3EA and 3EB could be affected.

This condition was determined to be a legacy issue dating to the original design of the plant. The most likely cause is lack of rigorous oversight of the vendor during the preparation and subsequent issuance of the fuse evaluation for the four Unit 3 4kV SD BDs. The required coordination studies have since been performed and a vendor oversight process has been added to TVA procedures. Compensatory measures (hourly fire watches) have been put in place for affected fire areas. Additional corrective actions include issuing an Engineering Change Package to replace the Unit 3 4kV SD BDs primary 0.5 amp PT fuses with 1 amp fuses of the same type.

05000296/LER-2017-0011 September 2017
31 October 2017

On September 1, 2017, at approximately 1006 Central Daylight Time (CDT), Browns Ferry Nuclear Plant (BFN) Unit 3 3A Residual Heat Removal (RHR) system pump failed to start during performance of Surveillance 3-SR-3.5.1.6 (RHR I), Quarterly RHR System Rated Flow Test Loop I. The apparent cause was the Electrical Preventive Maintenance Instruction for 4kV Wyle/Siemens Horizontal Vacuum Circuit Breaker (Type-3AF) and Compartment Maintenance was revised to include steps to secure the breaker's mounting hardware which caused internal binding of the indication flag. Binding of the indication flag prevented the closing spring of the breaker from charging and the breaker from closing on demand. As a result, automatic start of the 3A RHR pump was prevented. On September 1, 2017, at approximately 1633 CDT, the 3A RHR Pump was declared operable following lubrication and testing of the breaker's indication flag mounting bolt.

A Past Operability Evaluation concluded that the 3A RHR Pump was inoperable from July 26, 2017 to September 1, 2017, which exceeded the Technical Specification allowed outage time. During this time, the 3B, 3C, and 3D RHR pumps would have started automatically upon receipt of an Emergency Core Cooling System (ECCS) initiation signal or from an Operator manual start demand from the Control Room. Based on results from the Probability Risk Assessment and Engineering inspections, there was no significant risk to the health and safety of the public or plant personnel for this event. The Corrective Action to reduce the probability of similar events occurring in the future will be addressed by revising the Electrical Preventive Maintenance Instruction for 4kV Wyle/Siemens breakers to ensure freedom of movement of the indication flag is present during the breaker inspection.

05000296/LER-2016-0068 June 2016
5 August 2016

During a surveillance test on June 8, 2016, the BFN, Unit 3, High Pressure Coolant Injection (HPCI) Turbine Stop Valve Mechanical Trip Valve behaved erratically upon turbine start. Troubleshooting and maintenance on the valve led to discovery of a condition that could have resulted in the HPCI system being unable to perform its required safety function in a Mode where HPCI Operability was required.

The inoperability was caused by the HPCI Turbine Stop Valve Mechanical Trip Valve's Reset Spring, which was deformed and weakened from years of continuous compression. The spring was replaced and the system was returned to service on June 10, 2016.

Corrective actions to prevent recurrence include revising preventive maintenance procedures to specify replacement of the Trip Tappet, Piston, and Reset Spring on a defined periodicity. Additionally, procedures will be revised to require testing the as-left breakaway force a minimum of three times to ensure repeatability.

Preventative maintenance procedures will also be revised to clarify that lift force checks after spring compression adjustments shall be conducted with the auxiliary oil pump running.

05000296/LER-2016-00518 April 2016
17 June 2016

On April 18, 2016, during a scheduled surveillance, the power to the Main Steam Line (MSL) B Relief Valve failed to transfer to its alternate feeder breaker when the normal feeder breaker was opened. The Automatic Depressurization System (ADS) function of the MSL B Relief Valve was declared inoperable. It was determined that the ADS valve was inoperable from March 26, 2016 to April 19, 2016. The valve's ability to open under normal power was not affected. Five of the six ADS valves remained operable. Only four ADS valves are required to meet the ADS function in the Loss of Coolant Analysis described in the Final Safety Accident Report.

The unavailability of the ADS alternate power source was directly caused by a bus stab on the back of the Molded Case Circuit (MCC) breaker not fully engaging with the bus. This was apparently caused by improper performance of previous post-maintenance testing. The stab was adjusted, the MCC breaker was returned to service, and the MSL B Relief Valve's ADS function was declared operable upon verification of its alternate power supply.

Corrective actions were to determine which load-feeding MCC breakers have a normal and alternate power source, and revise their preventative maintenance procedures to verify that post-maintenance testing includes power source isolation prior to closing the breaker under load. Breaker bus stabs will be replaced.

05000296/LER-2016-0046 April 2016
6 June 2016

On April 6, 2016, the Tennessee Valley Authority was presented with as-found testing results indicating that three of the thirteen Main Steam Relief Valves (MSRVs) from Browns Ferry Nuclear, Unit 3, exceeded the +1- 3 percent setpoint required for their operability. Troubleshooting determined that the MSRV discs failed by corrosion bonding to their valve seats. The valve discs were previously platinum coated to prevent this, but the valve seat's rough Stellite surface caused the coating to flake off.

It was determined that the MSRVs were inoperable from March 19, 2014 to February 20, 2016. The affected valves remained capable of maintaining reactor pressure within American Society of Mechanical Engineers code limits. Additionally, the valves' ability to open under remote-manual operation, or activation through the Automatic Depressurization System or MSRV Automatic Actuation Logics was not affected. The valves remained capable of performing their required safety function.

Corrective Actions were to replace all Unit 3 MSRVs, to analyze the pilot valves of the inoperable MSRVs, and to revise procedures to verify the pilot disc finish meets its requirements prior to valve assembly.

05000296/LER-2016-00323 February 2016
25 April 2016
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On February 23, 2016, at approximately 0405 Central Standard Time, during performance of Primary Containment Local Leak Rate Testing (LLRT) of the Main Steam lines, the 3B Outboard Main Steam Isolation Valve (MSIV) failed its as-found LLRT. Because the MSIV failed to meet the leak rate limit, Browns Ferry Nuclear Plant, Unit 3, operated longer than allowed by Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3. In addition, TS LCO 3.0.4 was not met for each applicable Mode change since the last recorded as-found MSIV leak rate test on March 16, 2014, when the leak rates were below the leak rate limit.

The cause of the event was wear on the seating surface of the pilot poppet seat. Corrective action included replacing the valve stem containing a new pilot poppet, resurfacing the seat and restoration of the valve actuator.

The safety significance of this condition was minimal since the 3B Inboard MSIV was available to perform the safety function.

05000296/LER-2016-00222 February 2016
22 April 2016

On February 22, 2016, during routine maintenance of the Browns Ferry Nuclear, Unit 3 Core Spray (CS) system, relays on the 3ED 4kV Shutdown Board were found de-energized. This resulted in loss of the automatic start function of the 3B and 3D CS Pumps, the 3D Residual Heat Removal (RHR) pump, and the D1 Residual Heat Removal Service Water (RHRSW) pump, with normal power to the 3ED 4kV Shutdown Board.

Troubleshooting determined the relay was de-energized due to a failure of the 6-6C contacts on the MJ(52STA) switch associated with the 3ED 4kV Shutdown Board, and a binding of the 52STA Cam Linkage. This was caused by a misalignment of the switch to linkage interface, due to improper installation. The switch was subsequently replaced. Alignment verification instructions will be added to switch replacement procedures.

The duration of inoperability the 3B and 3D CS pumps, 3D RHR pump, and D1 RHRSW pump, was determined was placed in Mode 4. Manual start of these pumps remained available. Automatic start capability of the other Unit 3 CS, RHR, and RHRSW pumps was unaffected by this condition, and the required safety functions of the impacted systems continued to be met.

05000296/LER-2016-00119 January 2016
21 March 2016
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

On January 19, 2016, at approximately 1100 Central Standard Time (CST), during troubleshooting of the Main Control Room (MCR) green light indication on the 3A Residual Heat Removal (RHR) Pump Motor Breaker Transfer Switch (MBTS), it was discovered that the 3A RHR Pump MBTS had malfunctioned, potentially preventing the pump from starting from the MCR. The 3A RHR Pump was declared inoperable.

On January 20, 2016, at approximately 0030 CST, the 3A RHR Pump was declared operable following replacement of the 3A RHR Pump MBTS.

A Past Operability Evaluation concluded that the 3A RHR Pump was inoperable from January 9 to January 20, 2016, exceeding the Technical Specification allowed outage time. During this time, the 3B and 3D RHR Pumps were also inoperable on January 14, 2016, from 0127 to 0215 CST, resulting in a Safety System Function Failure. A Probabilistic Risk Assessment determined there was a negligible increase in risk.

The cause of this event was failure of the transfer switch to fully latch due to binding resulting from the MBTS being installed greater than its twenty-one year service life with no Preventative Maintenance (PM) performed. Corrective actions include verifying similar transfer switches are latched in the NORMAL positon on BFN, Units 1, 2, and 3, and creating a PM activity with a replacement schedule for these switches.

05000296/LER-2015-00520 August 201510 CFR 50.73(a)(2)(iv)(A), System Actuation

On August 20, 2015, at 1032 Central Daylight Time (CDT), while installing test equipment on the 3ED 4kV Shutdown Board (SD BD), for an online dynamic motor test of the 3D Residual Heat Removal pump motor, the Unit 3 Control Room received degraded voltage alarms and under voltage alarms for the 3ED SD BD. The 3ED 4kV SD BD normal feeder breaker opened, and the 3D Emergency Diesel Generator (DG) fast started and tied onto the board.

Troubleshooting was performed on the 3ED SD BD and on the 3D DG. The failure mode for this event was the clearing of primary and secondary 3ED SD BD metering fuses. The normal feeder breaker was closed, and offsite power to the SD BD was declared operable on August 21, 2015, at 1945 CDT.

A definitive cause could not be identified for the clearing of the fuses. However, corrective actions will be implemented that will address all of the most probable causes, and will minimize the likelihood of recurrence. These actions include performing inspections on circuits used for online dynamic motor testing of motors, removing the potentially faulty test equipment from service, and removing online dynamic motor testing from 4kV motor preventative maintenance.

05000296/LER-2015-0037 January 2015

On January 7, 2015, Browns Ferry Nuclear Plant (BFN), Unit 3, 3D and 3E Traversing Incore Probes (TIPs) stopped responding to automatic controls. The TIPs were left outside of their in-shield positions to decay for 24 hours, and the 3D and 3E TIP Primary Containment Isolation ball valves were left open. On January 8, 2015, the 3D and 3E TIPs were returned to their in-shield positions and their ball valves were closed.

On April 2, 2015, it was determined that, with the identified condition the 3D and 3E TIPs were incapable of automatically retracting in the event of an accident. The impact to the Primary Containment Isolation Valves (PCIVs) function was not recognized on January 7, 2015, and the required PCIV actions were not taken. Therefore, BFN, Unit 3, operated with two inoperable PCIVs, in violation of Technical Specifications (TS).

The apparent cause of this event was operations procedure 3-OI-94, Traversing Incore Probe System, lacked the appropriate guidance and relevant information to address TIP problems and associated TS applicability. Corrective actions include revising the procedure to provide additional guidance on responding to TIP probe malfunctions, and conducting briefings with operations.

05000296/LER-2015-00218 February 2015

On January 22, 2015, the Browns Ferry Nuclear Plant (BFN), Unit 3, the 3D Core Spray Pump normal power relay (3-RLY-075-14A-K31B) was found de-energized when it should have been energized during performance of a surveillance. Troubleshooting determined the cause of the relay being de-energized was failure of the MJ(52STA) switch in the associated breaker. The relay is an emergency start permissive for the 3B and 3D Core Spray pumps, the 3D Residual Heat Removal pump, and the D1 Residual Heat Removal Service Water pump. This condition prevented those systems from automatically performing their safety functions under normal power, rendering them inoperable for longer than allowed by Technical Specifications. However, these systems were available and the affected pumps could be manually started to perform their safety functions in the event of an accident. The failed switch only serviced the normal power feed, and automatic starting function was unaffected under emergency power. On February 18, 2015, an engineering evaluation determined the switch had apparently failed on September 17, 2014. On January 24, 2015, the relay and switch were replaced, and the automatic startup function was restored.

Apparent causes of the event are failure to implement all appropriate preventive maintenance or pre-emptive replacement allowing MJ(52STA) switches to fail, and the BFN Breaker Program excluding the associated switchgear components allowing support components to be overlooked with respect to reliability.

Corrective actions include replacing MJ switches in non-spare breakers and revising associated preventive maintenance, and revising the Breaker Program to include essential switchgear components.

05000296/LER-2015-001, High Pressure Coolant Injection and Reactor Core Isolation Cooling Inoperable Due To No Suction Source Aligned11 February 201510 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

On February 11, 2015, at 0820 Central Standard Time, Brown's Ferry Nuclear Plant (BFN), Unit 3, declared the High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems inoperable due to no suction source aligned. During surveillance testing, the Condensate Storage Tank (CST) emergency discharge isolation valve energized and closed when the breaker was closed, isolating both systems from their suction source. It was subsequently determined that maintenance task. Operations personnel re-opened the isolation valve using the hand switch in the Control Room, restoring operability to the HPCI and RCIC systems.

The apparent cause of this event was inadequate design review of a 2010 plant modification which allowed latent design vulnerabilities to be introduced into the plant.

The corrective actions to reduce the probability of a similar event occurring in the future were to remove thermal overload heaters from the affected breakers, preventing valve closure when these breakers are closed; to review a sample of recent engineering change packages for quality of Design Review; to repair a faulty hand switch; and to implement a design change for the CST isolation valves for all three BFN units to prevent spurious operation of the isolation valve when the associated breaker is closed.

05000296/LER-2015-00111 February 2015

On February 11, 2015, at 0820 Central Standard Time, Brown's Ferry Nuclear Plant (BFN), Unit 3, declared the High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems inoperable due to no suction source aligned. During surveillance testing, the Condensate Storage Tank (CST) emergency discharge isolation valve energized and closed when the breaker was closed, isolating both systems from their suction source. It was subsequently determined that contacts on the local hand switch were stuck closed following performance of a previous maintenance task. Operations personnel re-opened the isolation valve using the hand switch in the Control Room, restoring operability to the HPCI and RCIC systems.

The apparent cause of this event was inadequate design review of a 2010 plant modification which allowed latent design vulnerabilities to be introduced into the plant.

The corrective actions to reduce the probability of a similar event occurring in the future were to remove thermal overload heaters from the affected breakers, preventing valve closure when these breakers are closed; to review a sample of recent engineering change packages for quality of Design Review; to repair a faulty hand switch; and to implement a design change for the CST isolation valves for all three BFN units to prevent spurious operation of the isolation valve when the associated breaker is closed.

05000296/LER-2014-0032 June 2014

On June 2, 2014, during performance of the Reactor High Pressure Calibration surveillance, the Residual Heat Removal (RHR) Shutdown Cooling (SDC) Inboard Suction Valve Isolation relay failed to energize preventing automatic closure of the RHR SDC Inboard Suction Valve. On three occasions, the inability of this valve to close automatically upon receipt of the Primary Containment Isolation System signal resulted in a violation of the Browns Ferry Nuclear Plant, Unit 3, Technical Specifications. The Shutdown Cooling Mode of the Residual Heat Removal System was unaffected by this condition.

The cause of the event was relay wires had been lifted and incorrectly landed due to a human performance error at an indeterminate time between a successful post maintenance test (PMT) on March 07, 2014, and the time the condition was corrected by re-landing the wires according to plant drawings on June 6, 2014.

The corrective action to reduce likelihood of recurrence is to develop and deliver a case study to the Maintenance, Modifications, and Operations departments based on the details of this event.

05000296/LER-2014-0026 May 201410 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 6, 2014, at approximately 0830 Central Daylight Time (CDT), the Browns Ferry Nuclear Plant (BFN) Unit 3 reactor automatically scrammed as a result of an Anticipated Transient Without Scram/Alternate Rod Insertion (ATWS/ARI) signal generated during functional testing of reactor water level instrumentation. The scram air header was depressurized through the ATWS/ARI valves causing all rods to insert into the core. The ATWS/ARI signal also simultaneously opened the Recirculation Pump Trip (RPT) breakers, tripping both Recirculation pumps. The loss of both pumps along with reduced core flow caused a reactor water level transient that lowered level below the Reactor Protection System (RPS) trip setpoint (+2 inches), resulting in a full reactor scram signal.

Prior to this event, reactor power was 2.1 percent as all control rods were inserted by the ATWS/ARI initiation ten seconds earlier. Following receipt of the ATWS/ARI signal, all plant systems performed as required.

The root cause of the event was that the ATWS low reactor water level Automatic Trip Unit (ATU) cards initiated a voltage transient that actuated the ATWS high reactor pressure trip due to a design anomaly.

The corrective action to prevent recurrence includes installing time delay relays in association with the Unit 3 reactor pressure ATWS circuit.

05000296/LER-2014-00118 March 201410 CFR 50.73(a)(2)(iv)(A), System Actuation

On March 18, 2014, the Browns Ferry Nuclear Plant (BFN) Unit 3 reactor automatically scrammed due to a turbine trip from a high main turbine moisture separator level. Initial indications show the level controller for 3B2 Moisture Separator failed to maintain level in automatic. Additionally, local manual control attempts failed to restore moisture separator level. Following the turbine trip Main Steam Isolation Valves remained open with main turbine bypass valves controlling reactor pressure.

At approximately 2232, Central Daylight Time (CDT) the 3B2 Moisture Separator Level High Alarm was received and an operator was dispatched to investigate. In accordance with the alarm response procedure the 3B2 Moisture Separator Water Level Controller was placed in manual. Attempts to control the Moisture Separator Reservoir 3B2 High Level Dump Valve manually were ineffective. At approximately 2252 CDT, the Unit 3 reactor automatically scrammed due to a turbine trip from a high moisture separator level.

The root cause was a failure to prevent the introduction of foreign material during the manufacturing process of the Moisture Separator Level Controller. The manufacturing defect was a legacy issue dating back to 1971 when the controller body was originally machined. The corrective actions to prevent recurrence requires the removal, cleaning of air passages, replacement of control relays, for similar controllers and upgrading the calibration procedure to include cleaning guidance.

05000296/LER-2013-00325 February 201310 CFR 50.73(a)(2)(iv)(A), System Actuation

On February 25, 2013, at approximately 1313 hours Central Standard Time, the Browns Ferry Nuclear Plant (BFN), Unit 3, reactor automatically scrammed due to an actuation of the Reactor Protection System from a turbine trip. The turbine tripped on low condenser vacuum due to a reactor feedwater piping separation. The Main Steam Isolation Valves were manually closed. There was one Safety Relief Valve that was manually operated to maintain reactor pressure due to the unavailability of the Main Turbine Bypass Valves upon loss of condenser vacuum. All systems responded as expected to the turbine trip. No Emergency Core Cooling System or Reactor Core Isolation Cooling (RCIC) system reactor water level initiation set points were reached. Reactor water level was controlled with the RCIC system and reactor pressure was controlled with the High Pressure Coolant Injection system.

The root cause for this event is that the system design for BFN, Unit 3, Feedwater Long Cycle line does not account for flashing of water to steam due to isolation valve leakage.

The corrective action to prevent recurrence is to redesign Feed Water Long Cycle lines downstream of each Feed Water Long Cycle isolation valve and upstream of the Miscellaneous Drain Header with a valve and piping configuration appropriately designed for the specified application.

05000296/LER-2013-00211 February 201310 CFR 50.73(a)(2)(iv)(A), System Actuation

On February 11, 2013, the Reactor Core Isolation Cooling (RCIC) system was manually started during a planned Browns Ferry Nuclear Plant (BFN), Unit 3, reactor shutdown. A Reactor Feedwater recirculation piping through wall leak resulted in the loss of condenser vacuum and subsequent unavailability of the Main Turbine Bypass Valves. The RCIC system was manually started to control reactor water level in anticipation of loss of Reactor Feedwater Pumps tripping on low vacuum. Safety Relief Valves were manually operated to maintain reactor pressure. No Emergency Core Cooling System or RCIC system reactor water level initiation set points were reached.

The root causes of this condition are the design used for valves 3-FCV-03-0071, -0072, and -0073 in the Feedwater Long Cycle Return Line is incorrect for the specified application, and BFN personnel did not consistently consider risk when making decisions to replace the BFN, Unit 3, Feedwater Long Cycle valves.

Corrective actions to prevent recurrence are to replace valves 1, 2, 3-FCV-03-0071, -0072, and -0073 with valves appropriately designed for the required operating conditions and to establish initial and continuing training for leaders and craft that support their roles and responsibilities.

Also, BFN has implemented a Strategic Performance Management process to reinforce and institutionalize conservative decision making principles.

05000296/LER-2013-0019 January 2013

On January 9, 2013, at 0400 Central Standard Time, an Auxiliary Unit Operator (AUO) performing rounds near the 3D Emergency Diesel Generator (EDG) discovered metal residue around the blower shaft. Inspection by Maintenance determined the blower bearing had failed.

Operations declared the 3D EDG inoperable.

The root causes of this condition are the shielded bearings in the EDG blowers were not adequately assessed on a component level to identify potential failure modes and impacts to EDG operability, and standard vibration data was ineffective in identifying the degradation of the lubrication in the shielded bearings of the BFN, Unit 3, EDG blowers due to the masking effect of generator vibrations.

Immediate corrective actions included the inspection and replacement of all diesel blower bearings that had not been replaced since 2012. The corrective actions to prevent recurrence are to determine appropriate Preventive Maintenance strategies for the population of sealed or shielded bearings associated with EDGs and safety or quality related rotating equipment, and to add an additional vibration monitoring point to the EDG blower fan bearings and relocate two existing monitoring points to the drive end bearing housing.

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05000296/LER-2012-00510 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 29, 2012, at 0331 Central Daylight Time, the Browns Ferry Nuclear Plant (BFN), Unit 3, reactor automatically scrammed due to fast closure of turbine control valves, initiated by a load reject signal on the Main Generator. The cause of the load reject signal was actuation of newly installed main transformer differential relay 387T, which caused the scram. All systems responded as expected to the load reject signal. Main steam isolation valves remained open and reactor pressure was controlled by the main turbine bypass valves. No Emergency Core Cooling System or Reactor Core Isolation Cooling System reactor water level initiation set points were reached. Primary Containment Isolation System isolations from Groups 2, 3, 6, and 8 were received, and reactor water level was controlled by the Feedwater System.

Three root causes were identified: 1) inadequate procedure, instructions, and testing methodology/equipment used for current transformer (CT) bench testing; 2) inadequate acceptance review by Tennessee Valley Authority (TVA) Engineering of a vendor prepared design change; and 3) inadequate management, oversight, and accountability by the BFN Maintenance organization for work performed by the Protective Relay Group.

The corrective actions to prevent recurrence include: 1) revise the CT bench test procedure; 2) revise the human performance procedure to incorporate technical conscience principles, focus technical task risk factors, mitigating strategies, and decision making; and 3) using the Nuclear Operating Model, utilize the TVA's strategic performance management process to ensure management alignment in the ownership and accountability for leadership expectations at BFN.

05000296/LER-2012-00424 May 201210 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 24, 2012, at approximately 0638 Central Daylight Time, Operations personnel inadvertently ranged 3H intermediate range monitor (IRM) down instead of up resulting in a half scram from the 3B reactor protection system (RPS) trip channel. Subsequently, the IRM was properly ranged and Operations personnel responded in accordance with procedures to reset the half scram. Coincident with Operations personnel placing the scram reset switch in the Group 2/3 position, an electrical spike was received on 3A IRM of the 3A RPS trip channel resulting in control rod insertion for the Groups 1 and 4 control rods. Operations personnel identified the unexpected control rod motion and initiated a manual reactor scram in accordance with Browns Ferry Nuclear Plant (BFN) Abnormal Operating Instructions.

The root cause was determined to be high impedance of the BFN, Unit 3, Main Control Room (MCR) common ground to station ground that exposed the 3A IRM to noise feedback.

The corrective action to prevent recurrence is to verify that BFN, Unit 3, MCR common ground connections to station ground are as shown in the applicable system drawings. If any ground connections are identified that require repair, work orders will be initiated and repairs performed.

Following repairs, the high impedance connection of BFN, Unit 3, MCR common ground to station ground will be confirmed to have been resolved by documenting the results of validation testing.

05000296/LER-2012-00310 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 22, 2012, at 0249 Central Daylight Time, the BFN, Unit 3, reactor was automatica ly scrammed due to de-energization of the Reactor Protection System from actuation of the 3A Unit Station Service Transformer (USST) differential relay 387SA, which resulted in a loss of 500 kilovolt (kV) power to BFN, Unit 3. All safety systems responded as expected to the loss of 500kV power. No Emergency Core Cooling System or Reactor Core Isolation Cooling (RCIC) System reactor water level initiation set points were reached. The RCIC System was manually started to control reactor water level. Primary Containment Isolation System initiation signals for groups 1, 2, 3, 6 and 8 were received as expected due to loss of power.

The immediate cause of this event was the 3A USST differential relay was installed with incorrect design calculation settings which resulted in the BFN, Unit 3, scram.

The root cause of this condition was inadequate procedural guidance within NEDP-5, Design Document Reviews, for the types of review required by engineering.

The corrective action to prevent recurrence is to revise NEDP-5, Design Document Reviews, to establish the definition and requirements for each type of review.

05000296/LER-2010-00426 December 201010 CFR 50.73(a)(2)(iv)(A), System Actuation

On December 26, 2010, at 1615 hours Central Standard Time, an alarm for Main Turbine Vibration High 3-VA-47-15 was received in the Unit 3 control room on annunciator panel 3-XA-55-7B Window 32.

Control room operators responded using Unit 3 Alarm Response Procedure (ARP) 3-ARP-9-7B. Exciter rotor inboard journal bearing vibration level indicated 8.0 mils and rising, and the outboard journal bearing indicated 5.5 mils and rising. At 1617 hours, an Upper Power Runback was initiated per the ARP. It was noted that vibration levels initially lowered then continued rising. At 1620 hours, control room operators initiated a manual reactor scram.

The direct cause of this event was an exciter rotor-deflector rub resulting from a combination of high differential air exit temperatures and existing decreased clearances on the rotor. The root cause was inadequate procedural guidance for monitoring the exciter air cooling system and prescribing mitigation actions to be taken based on differential temperature limits.

The rub was corrected during the forced outage. Corrective actions include installation of cooler vents for use in minimizing air binding, establishment of a cooler venting process, increased controls and documentation of manual "balancing" valve manipulation, increased system monitoring process rigor and oversight, and performance of a training analysis for inclusion of relevant aspects of this root cause into the Operations and Engineering training materials.

05000296/LER-2010-00326 March 201010 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

Unit 3 Cycle 14 operation failed to meet Technical Specifications (TS) Surveillance Requirement (SR) 3.6.1.3.8, which requires verification that a representative sample of reactor instrumentation line EFCVs actuate to the isolation position on a simulated instrument line break signal. With the discovery of multiple failures during unit shutdown for refueling, multiple EFCVs may have been inoperable during Cycle 14 operation.

TS Limiting Condition for Operation 3.6.1.3 requires that each Primary Containment Isolation Valve be operable in reactor Modes 1, 2, and 3, and when the associated instrumentation is required to be operable.

Given the multiple failures of EFCVs, it is likely that Unit 3 did not comply with the applicable Required Actions and associated Completion Times of TS 3.6.1.3 Action C. Accordingly this situation is being reported as any operation or condition prohibited by the plant's Technical Specifications, i.e., 10 CFR 50.73(a)(2)(i)(B).

The failed EFCVs were replaced. In accordance with the implementation of the Maintenance Rule (10 CFR 50.65) the Browns Ferry Nuclear Plant (BFN), Units 1, 2, and 3 EFCVs have been placed in Maintenance Rule a(1) status. The BFN Corrective Action Program has implemented actions to improve reliability of the EFCVs.

05000296/LER-2009-00322 March 200610 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On February 13, 2007, and again on August 26, 2009, during post-scram reviews, Browns Ferry Nuclear Plant personnel identified an unexpected level of instability in the Reactor Core Isolation Cooling (RCIC) system flow and turbine response following reactor scrams that occurred on February 9, 2007, and on August 24, 2009. Following each event, site engineering personnel reviewed the RCIC response and concluded the RCIC system was capable of performing its design function and Operations determined that RCIC was operable. On February 12, 2007, and again on August 26, 2009, Unit 3 entered Mode 2, commencing startup operations. Following the second event on August 24, 2009, Unit 3 was returned to service and remained at power until September 12, 2009, when Unit 3 was removed from service for scheduled maintenance activities.

During the September 2009 outage, the RCIC Electric Governor-Remote (EG-R) was replaced and I successfully tested. On March 25, 2010, in response to questions from the Nuclear Regulatory Commission (NRC), the Tennessee Valley Authority notified the NRC via a conference telephone call I that Unit 3 RCIC was inoperable since March 22, 2006, after the EG-R had been installed and when Unit 3 exceeded 150 psig while in Mode 2. This reflected RCIC inoperability longer than allowed by Technical Specification 3.5.3 and mode changes not allowed by LCO 3.0.4. A failure analysis, conducted by Engine Systems Incorporated, determined the oscillations were caused by a missing buffer piston and springs within the EG-R.

05000296/LER-2008-0022 June 200810 CFR 50.73(a)(2)(i)(B), Prohibited by Technical SpecificationsOn June 2, 2008, TVA determined that 7 of the 13 Main Steam Relief Valves (MSRVs) (SB), removed from Unit 3 following Cycle 13 operation mechanically actuated at pressures greater than 3 percent above their Technical Specifications (TS) setpoint, thus inoperable. One valve exhibited leakage past the seat, and the lift pressure could not be verified. Unit 3 TS limiting condition for operation (LCO) 3.4.3 requires that twelve (12) MSRVs be operable in reactor modes 1, 2, and 3. If less than twelve MSRVS are operable, the unit is to be placed in Mode 3 hot shutdown within 36 hours. As such, it is probable that Unit 3 operated outside the TSs longer than allowed by the TSs. Therefore, TVA is submitting this report in accordance with 10 CFR 50.73(a)(2)(i)(B), as any operation or condition prohibited by the plant's Technical Specifications.
05000296/LER-2008-0015 May 200810 CFR 50.73(a)(2)(iv)(A), System ActuationOn May 5, 2008, at approximately 0332 hours Central Daylight Time (CDT) Emergency Diesel Generators (EDGs) 3EC and 3ED auto-started and tied to their respective shutdown boards due to an under voltage condition. Operations was in the process of returning the Unit 3 4KV Unit Board 3B to the normal supply in accordance with Operating Instruction 0-01-57A, Switchyard and 4160V AC Electrical System, when the board failed to transfer. The loss of power to Unit Board 3B resulted in a loss of power to 4KV Shutdown Boards 3EC and 3ED, 480V Reactor Motor-Operated Valve (RMOV) Board 3B, and Reactor Protection System 3B (RPS) (JC) power supply. Due to the loss of power on the shutdown boards, EDGs 3EC and 3ED started and tied to their respective shutdown boards. Unit 3 also received Primary Containment Isolation System (PCIS) Groups 3 and 6 isolations and actuations. A coincidental upscale trip of the 3A intermediate range monitor (IRM), which resulted in RPS Channel 3A half scram, in combination with the de-energizing of the RPS Channel 3B resulted in an unexpected full reactor scram. The Standby Gas Treatment (SGT) and Control Room Emergency Ventilation (CREV) systems initiated as expected. By 0352 hours CDT the reactor scram and PCIS logic was reset, the SGT and CREV Systems were returned to standby readiness. By 0944 hours CDT power was restored to 4KV Shutdown Boards 3EC and 3ED; likewise, EDGs 3EC and 3ED were secured. TVA is submitting this report in accordance with 10 CFR 50.73(a)(2)(iv)(A) as any event of condition that resulted in manual or automatic actuation of any system listed in paragraph 10 CFR 50.73 (a)(2)(iv)(B).
05000296/LER-2007-00531 December 200710 CFR 50.73(a)(2)(iv)(A), System Actuation

On December 31, 2007, at 2140 hours Central Standard Time (CST), Unit 3 reactor received an automatic scram signal following a main generator load reject. The reactor scram from the generator load reject was expected. All systems responded to the scram as expected. All control rods inserted. During the initial pressure transient, which peaked at 1141 psig, six of the main steam system relief valves opened. The reactor pressure was subsequently controlled with the main steam system bypass valves. The reactor water level was controlled by the Feedwater system, the normal heat removal path through the main condenser was maintained during the event. The reactor scram was reset December 31, 2007, by 2146 hours CST.

TVA is submitting this report according to 10 CFR 50.73(a)(2)(iv)(A), as an event that resulted in a manual or automatic actuation of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B) (i.e., reactor protection system including reactor scram of trip, and general containment isolation signals affecting containment isolation valves in more than one system.)

05000296/LER-2007-00430 November 200710 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

On November 30, 2007, at approximately 1052 hours Central Standard Time (CST), during the process of shutting down for a planned maintenance outage, Operations isolated the Unit 3 High Pressure Coolant Injection (HPCI) steam supply, with the reactor at 950 psig. Operations verified by administrative means that the Reactor Core Isolation Cooling system and two Control Rod Drive system pumps were available as a high pressure injection water source, and entered Technical Specification Limiting Condition for Operation (LCO) 3.5.1.C. A previously identified steam leak on the packing of the HPCI steam line condensate inboard drain valve had increased. This leak was identified prior to entering the maintenance outage and plans were in place to remove HPCI from service and repair the leak. However, because the volume of the leak increased, operations removed HPCI from service earlier than planned. LCO 3.5.1.0 was exited at 1435 hours CST when the reactor pressure was less than 150 psig.

TVA is submitting this report in accordance with 10 CFR 50.73(a)(2)(v)(B) and 10 CFR 50.73(a)(2)(v)(D) as "any event or condition that could have prevented the fulfillment of a safety function of structures of systems that are needed to: Remove residual heat or mitigate the consequences of an accident.

05000296/LER-2007-00310 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

On September 22, 2007, at approximately 1000 hours Central Daylight Time (CDT), with BFN Unit 3 in Mode 3, an entry into the primary containment (drywell) identified an American Society of Mechanical Engineers (ASME) Class I reactor pressure boundary leak that could not be isolated. During the drywell entry, WA identified a one inch test line associated with a Residual Heat Removal (RHR) system testable check valve had a through wall leak in a welded connection. At 1245 hours CDT, following confirmation that the leak was part of the ASME Class I pressure boundary; operations placed the reactor in Mode 4 per the Technical Specifications.

This report is submitted in accordance with 10 CFR 50.73(a)(2)(ii)(A) as an event or condition that resulted in the nuclear power plant, including principal safety barriers, being seriously degraded.

05000296/LER-2007-00224 July 200710 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v), Loss of Safety Function

On July 24, 2007, at 1645 hours central daylight time (CDT) the Unit 3, Division II Emergency Core Cooling Systems (ECCS) Analog Trip Unit (ATU) Inverter failed due to a cleared fuse during a 250 VDC Reactor Motor Operated Valve (RMOV) board power supply transfer. The inverter provides power to the High Pressure Coolant Injection (HPCI) pump discharge flow controller. WA declared HPCI inoperable and entered a fourteen day Technical Specification (TS) Limiting Condition for Operation (LCO). Following fuse replacement at 2318 hours, Unit 3 HPCI was declared operable and the fourteen day LCO was exited. The fuse cleared due to an overcurrent condition during the power supply transfer. The transfer was performed with the inverter in service. The probable cause for the fuse clearing was a voltage transient on the ECCS inverter during the 250 VDC RMOV Board power supply transfer that resulted in a higher than normal inrush current across the input fuse. WA will revise the operating instructions to require the affected ECCS ATU Inverters de-energized prior to a scheduled transfer of the input voltage source.

Because HPCI was inoperable during the timeframe the inverter was out of service, WA is submitting this report in accordance with 10 CFR 50.73(a)(2)(v)(B) and (D) as; any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: remove residual heat; and to mitigate the consequences of an accident.

05000296/LER-2007-0019 February 200710 CFR 50.73(a)(2)(iv)(A), System ActuationAt 1208 Central Standard Time, on February 9, 2007, Unit 3 received an automatic reactor scram on low water level following the loss of condensate flow. Just prior to the scram, operations attempted to establish manual operation of the condensate and demineralizer system. Personnel were in the process of modifying the control logic for the condensate and demineralized water system backwash controller. With the primary controller in run mode and the secondary controller in the program mode, personnel were loading new software into the secondary controller. The personnel involved were experiencing difficulties loading the software onto the secondary controller, so they attempted to load software onto the primary controller. They placed primary controller, which was previously in the run mode, into the program mode. However, the secondary controller was not returned to the run mode. With neither controller the run mode the condensate and demineralizer water system demineralizers isolated. This resulted in a decrease in reactor water level and an automatic reactor scram. The root cause of this event was the individuals involved in the planning and implementation of the work order did not fully understand manual operation of the system. Additionally, there is inadequate guidance or limitations on the use of in-field decision making. TVA is revising the operating instructions for the condensate demineralizer system. WA is revising trouble shooting guidance to eliminate trouble shooting under the direction of the system engineer or other individuals except under tightly controlled circumstances.
05000296/LER-2006-00329 August 200610 CFR 50.73(a)(2)(iv)(A), System Actuation

On August 29, 2006, while in steady state operation at 100% power, control room annunciation was received at 2210 hours CDT of a low level in the main turbine electro-hydraulic control (EHC) fluid reservoir. Local inspection of the tank confirmed an actual low level and also that the tank level was continuing to drop. At 2223 hours, reactor power was reduced to approximately 78% via reactor recirculation pump speed reduction, and, at 2225 hours, a manual scram was initiated in accordance with plant procedures. All control rods fully inserted and expected system responses were received. Actuation of primary containment isolation system groups 2, 3, 6, and 8 occurred due to the expected temporary lowering of reactor water level below the actuation setpoint. Valve realignment as part of the main turbine trip which followed the scram isolated the location of the EHC fluid leak from the rest of the system. The normal heat rejection path (from the reactor to the main condenser via the main steam lines with reactor water make-up provided by the condensate/feedwater systems) remained in service.

Reactor water level was recovered to the normal operating range by the normal reactor water level control system. Neither the high pressure coolant injection nor reactor core isolation cooling systems were used during this event.

The root cause of the EHC fluid leak was determined to be inadequate 0-ring compression on a solenoid valve mounting due to the use of device mounting bolts which were too long. The bolts and the valve were supplied as a kit by the vendor. Plant procedures will be revised to verify bolt length and mounting hole depth in future activities involving EHC components.

05000296/LER-2006-00219 August 200610 CFR 50.73(a)(2)(iv)(A), System Actuation

On August 19, 2006, at 1105 hours central daylight time, Unit 3 was manually scrammed following a loss of both the 3A and 3B Reactor Recirculation pumps. Just prior to the event, the Unit 3 Unit Operator (UO) received alarms indicating low reactor water level, reactor feedwater level control system failure, and failure of the input/output modules for both the 3A and 3B Reactor Recirculation pumps. The UO also reported that main generator load was approximately 730 megawatts electrical (approximately 64 percent of full power output) and lowering. Based on these indications, the UO scrammed the reactor.

The immediate cause of the manual scram was the loss of both the 3A and 3B Reactor Recirculation pumps. The manual scram was required by the conditions presented to the Unit 3 operator following the loss of recirculation flow. The initial investigation into the trip found the Variable Frequency Drive (VFD) microprocessors non-responsive. The root cause of the event was the VFD controls malfunctioned due to excessive traffic on the connected plant Integrated Control System (ICS) network. Corrective actions include developing a network firewall device that limits the connections and traffic to any potentially susceptible devices on the plant ICS network and installing a network firewall device on each Unit's VFD controller.

05000296/LER-2006-0013 May 200610 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

Following testing of main steam relief valves (MSRV) removed from Unit 3, it was discovered that 2 of the 13 Technical Specifications Limiting Condition for Operation (LCO) 3.4.3 requires that 12 MSRVs be operable in reactor modes 1, 2, and 3. If less than 12 MSRVs are operable, then the unit is to be placed into Mode 3 within 12 hours and Mode 4 within 36 hours. Since each BFN unit has 13 installed MSRVs, the inoperability of more than 1 MSRV would require the above actions to occur. While the setpoint-drift condition was not identified until after the valves' removal from the plant, MSRV pilot valve disc-seat corrosion bonding in boiling water reactor applications is a known phenomenon, and the condition is deemed to have developed while the valves were in service during Unit 3 Cycle 12 operation.

The root cause of this condition was MSRV pilot valve disc-seat corrosion bonding which can develop during normal reactor operations. The affected valves will be refurbished and their lift-setpoints re-established prior to reinstallation in the plant. There were no actual safety consequences associated with this event.

05000296/LER-2005-00331 October 200510 CFR 50.73(a)(2)(iv)(A), System Actuation

On October 31, 2005, while Unit 3 was in steady state operation at 100% power, a main turbine trip and resultant reactor scram occurred. At the time, operators were in the process of returning 500-kV switchyard Bus-2, Section 2 to service using a switching order. When the Power Circuit Breaker (PCB) to the 500-kV Trinity 2 transmission line was closed, the PCB immediately tripped back open. The post-scram investigation subsequently determined that this was due to a closed ground switch at an offsite substation on this transmission line. The PCB properly tripped open to clear the Trinity 2 line ground; however, the electrical power transient resulting from the ground and its clearing caused speed perturbations on the Unit 3 main turbine. The rate of speed change seen on the turbine was slightly greater than the maximum rate anticipated by the turbine control system logic and, therefore, the turbine speed feedback signals were designated as invalid by the turbine control logic. With all turbine speed feedback signals designated as invalid, a main turbine trip on loss of speed feedback occurred in accordance with the system design and a reactor scram occurred due to the turbine trip.

This event was an uncomplicated plant scram with major plant safety systems responding as expected and in accordance with the plant design. The event cause was that actual turbine speed change exceeded that anticipated as possible by the turbine control logic, causing valid speed signals to be designated as invalid.

Additionally, the switching order was deficient in that instructions to open the closed ground switch were in a separate switching order and were not performed. Corrective actions include modifying the Unit 3 turbine control logic and strengthening the process used by the transmission system organization for switching activities.

05000296/LER-2005-00217 September 200510 CFR 50.73(a)(2)(iv)(A), System Actuation

On 9/17/05 Unit 3 was in steady state operation at approximately 73% power. A maintenance activity was in progress to repair a level control valve on a high pressure feedwater heater. During the work on the valve, an air in-leakage pathway to the main condenser was created, and due to an unanticipated mechanical failure of the valve internals, the valve could not be readily reassembled to isolate the in-leakage path. Over a period of approximately 10 minutes, the main condenser vacuum decreased to the low vacuum trip setpoint for the main turbine, and a main turbine trip and subsequent reactor scram occurred at 1129 hours CDT. All expected system responses occurred. Actuation of primary containment isolation system Groups 2, 3, 6, and 8 occurred due to the expected temporary lowering of reactor water level below the actuation setpoint. This logic isolates shutdown cooling (if in service), isolates the reactor water cleanup system, isolates the normal reactor building ventilation, initiates the standby gas treatment system, initiates the control room emergency ventilation system, and retracts traversing incore probes (if inserted). The normal heat rejection path (from the reactor to the main condenser via the steam lines with reactor water make-up provided by the condensate/feedwater systems remained in service.

Neither the high pressure coolant injection nor reactor core isolation cooling systems were used during this event.

No safety-relief valve (SRV) operation occurred during the trip transient, and post-trip review confirmed that peak reactor pressures remained below the nominal SRV lift setpoints.

The event was caused by the unanticipated failure mode of the valve's internals, and the work control process was not effectively managed to assess all possible failure modes. Corrective actions include revisions to operating procedures and the provision of training to managers/supervisors on effective operational decision making.

05000296/LER-2005-00111 February 200510 CFR 50.73(a)(2)(iv)(A), System Actuation

At 1629 hours Central Standard Time on February 11, 2005, the Unit 3 reactor scrammed from 100% power. The scram was caused by a simultaneous false trip signal generated to the main generator circuit breaker 234, switchyard circuit breakers 5264 and 5268, and a main generator trip. This signal was generated when a PK block (disconnect device 26W), which had been pulled as part of a clearance for breaker 5264, was re-inserted as part of a switching order from the Load Dispatcher for returning the breaker to service. When the PK block 26W was inserted (out of sequence of the switching order), the associated current transformer (CT) circuit was momentarily grounded resulting in a false differential. The correct sequence of the switching order was to actuate the trip cutout switches for the differential trip functions prior to inserting any of the PK blocks.

The generator trip resulted in a turbine trip and opening of the output breakers caused a power-load unbalance trip. The control valve (CV) fast closure caused the reactor to SCRAM.

All rods inserted. Reactor water level lowered, as expected, and was recovered by normal feed water flow. All expected Primary Containment Isolation System (PCIS) isolations were received along with the auto start of Control Room Emergency Ventilation (CREV), and the three Standby Gas Treatment (SGT) trains.

The root cause of this event was determined to be personnel error, in that the Operator (Utility Licensed) failed to follow the task sequence identified in the switching order.

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05000296/LER-2004-00317 June 200410 CFR 50.73(a)(2)(i)(B), Prohibited by Technical SpecificationsTesting of main steam relief valves (MSRV) removed from Unit 3 following the operating cycles 10 and 11 respectively, revealed that in each set of valves tested, multiple valves mechanically actuated at pressures greater than 3% above their nominal setpoint. The Unit 3 Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.4.3 requires that 12 MSRVs be operable in reactor Mode 1 (power operation), Mode 2 (startup), and Mode 3 (hot shutdown). If less than 12 MSRVs are operable, the unit is to be placed into Mode 3 within 12 hours and Mode 4 (cold shutdown) within 36 hours. Since each BFN unit has 13 installed MSRVs, any concurrent MSRV inoperability would require the above actions to be taken. While the setpoint-drift condition was not identified until after the valves' removal from the plant, MSRV pilot valve disc-seat corrosion bonding in boiling water reactor applications is a known phenomenon, and the condition is deemed to have developed and existed while the valves were in service during operation in cycles 10 and 11. Similar MSRV performance prior to calendar year 2001 was reported by TVA to NRC via LER. However, TVA did not report the failure to meet TS following the Unit 3 operating cycles 10 and 11 in 2002 and 2004. The failure to report the occurrences have been addressed by the WA Corrective Action Program. LER 296/2006-01 was submitted for Unit 3 Cycle 12 operation. This LER, 296/2004-003-00, addresses the past conditions (i.e., 2002 and 2004) which had not been previously reported. The root cause of this condition was MSRV pilot valve disc-seat corrosion bonding which can develop during normal reactor operations. The affected valves were refurbished and their lift-setpoints re-established prior to their re-installation in the plant. There was no actual safety consequences associated with this condition.
05000296/LER-2004-00223 November 200410 CFR 50.73(a)(2)(iv)(A), System Actuation

On November 23, 2004, while Unit 3 was in steady state operation at 100% power, a main turbine trip and subsequent reactor scram occurred. All expected system responses occurred. A lightning strike occurred on the TVA 500-kV system approximately 40 miles distant from Browns Ferry. This strike resulted in a phase-to-ground fault on all three phases of the transmission line, and the electrical power transient caused speed perturbations on both the Unit 2 and Unit 3 main turbines. The rate of speed change seen on Unit 3 was slightly greater than the maximum rate anticipated by the turbine control system logic, and therefore the turbine speed feedback signals, while valid, were designated as invalid by the logic. With all turbine speed feedback signals designated as invalid, a main turbine trip on loss of speed feedback occurred in accordance with the system design, and a reactor scram occurred due to the turbine trip.

The event cause was that actual turbine speed changes exceeded those anticipated as possible by the turbine control logic, causing valid speed signals to be designated as invalid. Corrective actions included the adjustment of the affected logic settings, evaluation of the turbine speed response, and consideration of modifying the speed control and turbine trip logic.

05000296/LER-1985-014, Corrected Ltr Forwarding LER 85-014-00 Re Containment Isolation Initiation24 May 1985
05000296/LER-1984-004, Followup LER 84-004-01:on 840228,RHR Outboard Loop II Isolation Valve CFV-74-67 Stem Found Broken Upon Disassembly.Caused by Overloading.Valve Stem Replaced W/Stronger & More Durable Matl15 June 1984
05000296/LER-1983-026, Supplemental LER 83-026/03X-4:on 830411,while Attempting to Establish EECW Flow Rate to Emergency Diesel Generator 3 Coolers,Head on HX Found Cracked.Caused by Mfg Defect.Cast Iron Head Replaced25 November 1983
05000296/LER-1983-024, Forwards LER 83-024/01T-03 May 1983
05000296/LER-1983-023, Forwards LER 83-023/03L-026 April 1983
05000296/LER-1983-022, Forwards LER 83-022/03L-020 April 1983
05000296/LER-1983-019, Forwards LER 83-019/03L-08 April 1983
05000296/LER-1983-018, Forwards LER 83-018/03L-028 March 1983
05000296/LER-1983-016, Forwards LER 83-016/03L-029 March 1983
05000296/LER-1983-015, Forwards LER 83-015/03L-025 March 1983