05000416/FIN-2014005-01
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Finding | |
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Title | Failure to Assure Quality Installation on RCIC Steam Line |
Description | The inspectors reviewed a self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for failure to assure quality installation of the steam line tubing of the reactor core isolation cooling (RCIC) system. Specifically, the licensee failed to assure that rated performance limits of the ferrule connection, installed at the tee between the steam line and the pressure transmitter tube line, were met during initial installation. This failure resulted in an unplanned inoperability of the RCIC system. The licensee entered this issue into the corrective action program as Condition Report CR-GGN-2014-06792. As an immediate corrective action, the licensee replaced the tubing, the failed transmitter, and recalibrated the instruments. Furthermore, the licensee revised their system operation procedure for the RCIC system. This revision requires all steam isolation valves to be closed during this test, and that system recovery starts by opening Valve 1E51F076 (warming bypass valve around the 1E51F063) to allow adequate warming of the steam lines after isolation. The inspectors determined that the failure to assure quality installation of the ferrule connection on the steam line flow Transmitter 1E31N083B was a performance deficiency. The performance deficiency is more than minor and therefore a finding because it is associated with the design control attribute of the Mitigating Systems Cornerstone. Specifically, failure to assure steam lines in the RCIC system meet rated performance limits, may result in the unavailability and unreliability of a system that is relied upon to respond to initiating events to prevent undesirable consequences. Using NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings at Power, dated June 19, 2012, the inspectors determined that the issue required a detailed risk evaluation by the regional senior reactor analyst. This was because the finding represented an actual loss of a safety function due to the RCIC system being a single train system that was out of service for approximately 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> for repairs. The senior reactor analyst determined the change to the core damage frequency was 8.7E-8/year, and since the change to core damage frequency was less than E-7, no evaluation of external events or the large early release frequency was required. The finding was of very low safety significance (Green). The inspectors did not identify a cross-cutting aspect, as the performance deficiency is not reflective of current plant performance. |
Site: | Grand Gulf |
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Report | IR 05000416/2014005 Section 1R15 |
Date counted | Dec 31, 2014 (2014Q4) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71111.15 |
Inspectors (proximate) | C Alldredge G Guerra G Pick J Groom L Carson M Williams N Day P Nizov R Smith T Farina B Parks |
Violation of: | 10 CFR 50 Appendix B Criterion III, Design Control |
INPO aspect | |
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Finding - Grand Gulf - IR 05000416/2014005 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Grand Gulf) @ 2014Q4
Self-Identified List (Grand Gulf)
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