ML17279B011

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LER 88-008-00:on 880318 & 24,plant Tech Spec Fire Penetration Seals Discovered Impaired/Unsealed During Ongoing 100% Insp.Cause Under Investigation.Penetrations Placed on Hourly Fire tour.W/880422 Ltr
ML17279B011
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 04/22/1988
From: ARBUCKLE J D, POWERS C M
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
LER-88-008, LER-88-8, NUDOCS 8805030155
Download: ML17279B011 (7)


Text

ee ,4C CEISRA7ZD DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8805030155 DOC.DATE: 88/04/22 NOTARIZED:

NO FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe AUTH.NAME AUTHOR AFFILIATION ARBUCKLE,J.D.

Washington Public Power Supply System POWERS,C.M.

Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000397

SUBJECT:

LER 88-008-00:on 880318,plant Tech Spec fire penetration seals discovered impaired/unsealed during ongoing 1004 insp.W/8 ltr.DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR A ENCL W SIZE: C TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.NOTES: RECIPIENT ID CODE/NAME PD5 LA SAMWORTH, R INTERNAL: ACRS MICHELSON AEOD/DOA AEOD/DSP/ROAB ARM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 NRR7DRQN/SIB 9A G~~02 RES7DE/EIB RGN5 FILE 01 EXTERNAL: EGS(G GROH,M H ST LOBBY WARD NRC PDR NSIC MAYS,G COPIES LTTR ENCL 1 1 1 1 1 1 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 4 4 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD5 PD ACRS MOELLER AEOD/DSP/NAS AEOD/DS P/T PAB DEDRO NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR/DREP/RPB 10 NRR/PMAS/ILRB12 RES TELFORD,J RES/DRPS DIR FORD BLDG HOY,A LPDR NSIC HARRIS,J COPIES LTTR ENCL 1 1 2 2 1.1 1'1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1.1 1 1 1 1 1 1 j A TOTAL'UMBER OF COPIES REQUIRED: LTTR 45 ENCL 44 j A D P gpgg5P(~" D NRC Form 368 (8.83)LICENSEE EVENT REPORT ILER)V.S.NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.3160-0104 EXPIRES: 8/31/88 FACILITY NAME (11 Washin ton Nuclear Plant-Unit 2 DOCKET NUMBER (21 PAGE (3/0 5 0 0 03 9 7 1 OF 0/5 Plant Technical Specification Fire Penetration Seals Discovered Impaired/Unsealed Durin On oin 100%Ins ection-Cause Unknown EVENT DATE (5)LER NUMBER id)REPORT DATE (7)OTHER FACILITIES INVOLVED (8)MONTH DAY YE'AR YEAR SCOUCNT/AL NUMBER Rdvrd/ON yw7 NUMBER MONTH DAY YEAR FACILITY NAMES DOCKET NUMBER(SI 0 5 0 0 0 3 1 8 8 8 008 0 0 0 4 228 8 0 5 0 0 0 OPERATING MODE (8)1 POWE R LEVEL (101 NAME 20.402(6)20.406(~I (1 I ii)20.406(~)(11(ii)20.406(~)(I l(riil 20A05 I~l(1)(Iv)20.406(~)(1)(v)20.405(cl 50.35(cl(ll 50.3d (c)l2)59.73(~l(2)(i)60.73(~I I2)lit)60.73(el(2) liii)LICENSEE CONTACT FOR THIS LEA (121 50.73(~l(21(iv)50,73(~l(21(vl 50,73(e)l2)(xiii 50 73(~I(2)(vri/1(AI 50.73 (e I (2)(viii)I 81 60.73(~I(2)(e)AREA CODE THIS REPORT IS SUBMITTED PURSUANT T 0 THE REOUIREMENTS OF 10 CFR (): (Cnec/r one or more OI tne Iollowinp/(ll 73.71(o)73.71(cl OTHER ISpecily rn Aottrett oelow end in Text, NRC Po" 366A/TELFPHONE NUMBER D Ar 1 Com liance En ineer COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)0 9 3 7 7-1 CAUSE SYSTEM COMPONENT 6'IANUFAC TURER REPORTABLE TO NPADS Av%664~gv p/4>ghppklpN

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po)tr~v.c..i/+6 SUPPLEMENTAL REPORT EXPECTED (14)YFS III ywcomplete EXPECTEO SUSMISSION OATEI ivO ABSTRACT ILimit to/400/peter, l,e., epproximetely IIINen rlnple rpsCe tyPewritNn linn/(181 EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR On March 23, 1988 and March 25, 1988 it was determined that problems documented (on March 18, 1988 and March 24, 1988)with regard to ll Plant Technical Specification fire penetrations were reportable under 10CFR50.73 (a)(2)(i).

The penetrations were impaired such that they would not qualify as a three-hour fire barrier.The penetrations are located in the Diesel Generator and Reactor Buildings.

The problems were identified during the performance of ongoing physical walkdowns of all accessible Technical Specification walls and penet'rations as further corrective action committed to in LER 87-030.As required by the Plant Technical Specifications, the penetrations were placed on an hourly fire tour.Further corrective actions include 1)preparing Maintenance Work Requests (MWRs)to repair/seal the penetrations, and 2)completing the 100K review of documentation and physical walkdowns of all accessible Technical Specification walls and penetrations.

At the completion of the review and walkdowns, a supplemental report describing any further deficiencies discovered will be submitted.

The cause of this event is currently under investigation.

It was determined that this event did not affect the health and safety of either the public or Plant personnel due to the fire protection design of the fire areas involved.8805030155 SS0422 PDR ADOCK 05000397 S DCD NRC Form 3dd (9 83)

OO OO NRC Forro 358A ((S83 I LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION APPROVED OMS NO.3150WI04 EXPIRES: 8/3(/88 FACILITY NAME ((I OOCKET NUMSER (2l LER NUMSER (SI PM 5EQVENTIAL

~ra?45VI5ION NVM554 I'2 NVM554 PAGE (3l Washington Nuclear Plant-Unit 2 TEXT///more spoce is/tr/Item.ose~/5'orre/HRC Form 3//SA'5/(ITI Pl ant Condi ti ons 0 S 0 O 0 0 0 0 0 02oF 0-5 a)Power Level-100%b)Plant Mode-1 (Power Operation)

Event Descri tion On March 23, 1988 and March 25, 1988 the following problems which were documented with regard to Plant Technical Specification fire penetration seals were determined to be reportable under 10CFR50.73 (a)(2)(i).

a)On March 18, 1988 it was documented on a Plant Nonconformance Report that: Fire seal penetrations D101-3002-and D101-3003 (Diesel Generator Building 441 Elevation) each had a non-approved fire configuration type~lug installed (holes had been drilled through the center and filled with'All Thread").b)NRC FORM 3554 (983 I~Fire seal penetrations D102-3002 and D102-3003 (Diesel Generator Building 441.Elevation) each had a non-approved fire configuration type (non-ferralloy) plug installed, and the penetrations were not'listed in'he Plant Seal Tracking'System (PSTS)data base.~Fire seal penetration D104-3063 (Diesel Generator Building,-441 Elevation) was impaired in that the seal depth was less than required.~Fire seal penetration D113-2012 (Diesel Generator Building-441 Elevation) was impaired in that it appears that a cable had been pulled through and the penetration not re-sealed.

On March 24, 1988 it was documented on a Plant Nonconformance Report that: Fire seal penetration R116-3003.9 (Reactor Building-422 Elevation) was impaired in that it appears that a cable had been pulled through and the penetration not re-sealed.

t Fire seal penetration R116-3003.10 (Reactor Building-422.Elevation) was impaired in that the plug had a drilled hole through its center, and the penetration was not listed in the PSTS data base.Fire seal penetration R116-3011.4 (Reactor Building-444 Elevation) was impaired in that the seal depth was less than required.Fire seal penetration R116-3011.6 (Reactor Building-444 Elevation) was impaired in that the plug had a drilled hole through its center, and the penetration was'not listed in the PSTS data base.Fire seal penetration R410-4004.7 (Reactor Building-522 Elevation) was impaired in that it appears that a cable had been pulled through and the penetration not re-sealed.

4 U.S.GPO (98$0.824 538/455 NRC Form 358A IS'83 I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION V.S.NUCLEAR REGULATORY COMMISSION APPROVEO OMS NO.3150WIOO EXPIRES: 8/3I/88 FACILITY NAME III OOCKET NVMSER ITI LER NVMSER ISI YEAR~r'y SEOVENTIAL NUMOEII Vi IIEVISION Ri+i NUMef A PAGE I3I Washington Nuclear Plant-Unit 2 TEXT I//more epoo>>/I pppppnrL Pop o/8/Or'M//VRC forIII38SAS/(IT/

o 5 o o o 39 788 0 0 8 00 03 OF 0 5 The problems were identified during the performance of ongoing activities associated with further corrective actions committed to in a previous LER (87-030,"Upgraded Plant Technical Specification Fire Wall not Constructed to gualify as a Three-Hour Fire Barrier and Wall Penetration not Sealed").Specifically, the Supply System committed to perform a 10(C review of documentation, and physical walkdowns of all accessible Technical Specification walls and penetrations, to determine the adequacy of PSTS.The problems noted in this LER (88-008)were discovered during the ongoing physical walkdowns.

The cause of this LER is currently under investigation.

Immediate Corrective Action As required by the Plant Technical Specifications, the penetrations were placed on an hourly fire tour.Further Discussion and Corrective Action a)Further Discussion

~Fire seal penetrations D101-3002, D101-3003, D102-3002 and D102-3003 are located in Fire Area DG-V (1B Diesel Oil Tank Pump Room).o Fire seal penetration D104-3063 is located in Fire Area DG-I (HPCS Diesel Generator).

~Fire seal penetration D113-2012 is located in Fire Area DG-III (1B Diesel Generator).

o Fire seal penetrations R116-3003.9, R116-3003.10, R116-3011.4 and R116-3011.6 are located in Fire Area R-IV (RHR Pump Room Rl, Pipe Chase and RHR Heat Exchanger"B" Equipment Room).~Fire seal penetration R410-4004.7 is located in Fire Area R-VIII (MCC Room Division 2).I b)Further Corrective Action~Maintenance Work Requests (MWRs)were written to repair/seal the penetrations.

~The penetrations which were not previously included in the PSTS data base were added to the data base.~At the completion of the 100%review-of documentation, and physical walkdowns of all accessible Technical Specification walls and penetrations, a supplemental report describing any further deficiencies discovered will be submitted.

NRC FORM 3OOA I983)o U.S GPO:1988 0 824 538/455 OO~t NRC Form 388A$431 LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUCLEAR REGULATORY COMMISSION APPROVEO OM8 NO, 3150M(04 EXPIRES: 8/31188 FACILITY NAME (I)Washington Nuclear Plant-Unit 2 TExT RY naacp<<>>cp<<(ppund, 1>>p<<ApFp44(HRc Ann 388AYI (Ill DOCKET NUMSER (Tl 0 S 0 0 0 LER NUMSER Iel Y f AR a ff QVE NTIAL (3Q 4(V>>KI>NVMsf 4 i NVMsf 4 00 00 PAGE I31 4 OF Safety Si ni f i c ance Although there were no fires during the event period, the following is a description of the consequences had a Design Basis Fire had occurred in the areas described in this LER.a)Fire Areas DG-I, DG-III and DG-V Smoke from a fire would activate one or more smoke detectors, which would alarm in the Control Room.The fire brigade would be dispatched and take appropriate action in accordance with the pre-fire plans and emergency response procedures.

Manual hoses are available.

The thermal detection system would sense a high heat condition and activate the pre-action sprinkler system.Automatic spray heads would fuse and control the fire.b)Fire Areas R-IV and R-VIII Smoke from a fire would activate an ionization detector, which would alarm in the Control Room.The fire brigade would be dispatched and take appropriate action in'ccordance with the pre-fire plans and emergency response procedures.

Manual hoses are available.

In addition, Fire Area R-IV has a low fire loading and, as a result, the probability of a fire spreading is considered remote.Accordingly, this event did not affect the health and safety of either the public or Plant personnel.

Similar Events LERs85-028, 87-004-00, 87-004-01 and 87-030.EIIS Information NRC FORM 3584 (883 I Text Reference Fire Penetration Seals D101-3002 D101-3003 D102-3002 D102-3003 D104-3063 D113-2012 R116-3003.9 R116-3003.10 EIIS Reference System Component KP Pen*U.s opo:lose o 83f essMss NAC form 344A IS4)3)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION APPAOVEO OMS NO.3)50&)04 EXPIRES: 8/31/88 PACILITY NAME)1)OOCKET NUMSEA l2)LEA NUMSER (4)PAGE 13)Washington Nuclear Plant-Unit 2 TEXT//f more Secre ir reerr)wS eee rr/R/Or'on/I HRC for//I 3//fASI Ill)o s o o o YEAR 8 8 my&.440USNTIAL m'iEr NUM 4 O YeWA 0 0 II 4 VISION NVMSSII 0 0 0 5 OF 0 5 R116-3011.4 R116-3011.6 R410-4004.7 Diesel Generator Bldg Reactor Bldg 1B Diesel Oil Tank Pump Room HPCS Diesel Generator 1B Diesel Generator RHR Pump Room Rl RHR Meat Exchanger NBN Equipment Room IRCC Room, Division 2 NB NG ME EK NB nIE I1E I1E Bldg Bl dg Room Room Room Room Room Room NIIC PO/IM 344A 1883)oU 8GPO;ISSS-O

$24$38/4$$

ai WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~3000 George Washington Way~Richland, Washington 99352 Docket No.50-397 April 22, 1988 Document Control Desk UPS.Nuclear Regulatory Commission Washington, D,C.20555

Subject:

NUCLEAR PLANT NO.2 LICENSEE EVENT REPORT NO.88-008

Dear Sir:

Transmitted herewith is Licensee Event Report No.88-008 for the WNP-2 Plant.This report is s'ubmitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.

Very truly yours,'..Powers (M/D 927M)WNP-2 Plant Manager CMP: lg

Enclosure:

-Licensee Event Report No.88-008 cc: Mr.John B.Martin, NRC-Region V Mr.C.J.Bosted, NRC Site (M/D 901A)INPO Records Center-Atlanta, GA Ms.Dottie Sherman, ANI Mr.D.L.Williams, BPA (M/D 399)p 7g 5 05'r'f