|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
ACCELERATED DI TRJBUTION DEMONSTRM.TION SYSTEM REGULAT~INFORMATION DISTRIBUTION STEM.(RIDS)
'I ACCESSION NBR:9204080113 DOC.DATE: 92/03/31 NOTARIZED:
NO DOCKET 4 PAREIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH.NAME AUTHOR AFFILIATION FIESzC.L.Washington Public Power Supply System BAKER,J.W.
Washington Public Power Supply System RECIP.NAME
" RECIPIENT AFFILIATlON
SUBJECT:
LER 91-029-01:on 911031,discovered that incorrect Containment Atmospheric Control Recycle Flow Control controllers were installed for both divisions.
Caused by less than adequate design.CAC was revised.W/920331 ltr./DZSTRZBUTZON CODE: ZE22T COPZES RECEZVED:LTR U ENCL r SZZE: 0 TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: RECIPIENT ID CODE/NAME PD5 LA ENG,P.L.1 INTERNAL: ACNW AEOD/DOA AEOD/ROAB/DSP NRR/DLPQ/LHFB10 NRR/DOEA/OEAB NRR/DST/SELB 8D NRR/DST/SPLB8D1 REG F.TL"E~~02 RGN 1L"E-01.J EXTERNAL: EG&G BRYCEzJ.H NRC PDR NSIC POORE,W.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 3 3 1 1 1 1 RECIPIENT ID CODE/NAME PD5 PD ACRS AEOD/DSP/TPAB NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB8H3 NRR/DST/SRXB 8E RES/DSIR/EIB L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 2 2 1'1'1 1 1 1 1 1 1 1~P Pq ly72 3 5 5 O NOTE TO ALL"RIDS" RECIPIENTS PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK.ROOM P 1-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32 t'~
@~i 0 WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~3000 George Washington Way~Richland, Washington 99352 ,March 31, 1992 G02-92-074 Docket No.50-397 Document Control Desk U.S.Nuclear Regulatory Commission Washington, D.C.20555
SUBJECT:
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO.91-029-01 Transmitted herewith is Licensee Event Report No.91-029-01.
This report provides the results of the Supply System initiated Safety System Functional Inspection (SSFI)on the Containment Atmospheric Control (CAC)System.The original LER indicated a supplemental report was to be issued by March 1, 1992.However, the CAC review was not completed on that date as it became more involved than originally perceived.
A preliminary review showed that outside expertise was required and this additional investigation has been underway.'ased on a phone conversation between Mr.Mark Reis of the Supply System and Mr.Phil Johnson of your Region V ofice on February 27, 1992 the date for submittal of LER 91-029-01 was extended to March 31, 1992.This was to allow for completion of the CAC SSFI performed on the Hydrogen Recombiners.
The SSFI and the associated consultants review has now been completed.
This LER revision discusses reportable items that resulted from these efforts.Sincerely,.jW.Baker WNP-2 Plant Manager (Mail Drop 927M)Enclosure CC: r;r Mr.John B.Martin, NRC-Region V Mr.C.Sorensen, NRC Re'sident Inspector (Mail Drop 901A, 2 Copies)INPO Records Center-Atlanta, GA 0 Ms.Dottie Sherman, ANI xylo Mr.D.L.Williams, BPA (Mail Drop 399)gg$Q6S 9204080113 920331 PDR ADOCK 05000397 S'DR AGILITY NAME (1)LICENSEE EVEN EPORT (LER)ashington Nuclear Plant-Unit 2 ITLE (4)DOCKET NUMB R ()PAGE (3)0 5 0 0 0 3 9 7 I PF 10 Inadequate Primary Containment Hydrogen Recombiner Recycle Flow Control EVENT DATE (5 YEAR YEAR HONTH DAY LER NUHBER SEQUENTIAL NUHBER 6)EVI SION NUHBER REPORT DATE 7 MOHTM DAY YEAR FACILITY NAMES DOCKET 5 0 OTHER FACILITIES INVOLVED (8)NUMBERS(S) 00 1 0 3 I P ERAT ING ODE (9)9 1 9 I I 0 2 9 0 I 0 3 3 1 9 2 50 0 0 HIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more of the following)
(11)1 OWER LEVEL (10)0.402(b)0.405 (a)(1)(I)0.405(a)(1)(ii) 0.405(a)(1)(iii) 0.405(a)(1)(iv) 20.405(a)(1)(v) 20.405(C)50.36(c)(l) 50.36(c)(2) 50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x) 77.71(b)73.73(c)THER (Specify in Abstract elow and in Text, NRC ore 366A)HAHE LICENSEE CONTACT FOR THIS LER (12)C.L.Fies, Compliance Engineer TELEPHOHE NUMBER REA CODE 5 0 9 7 7-4 1 4 7 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IH THIS REPORT (13)CAUSE SYSTEH COHPOHEHT MANUFACTURER EPORTABLE 0 HPRDS CAUSE SYSIEH COHPOHEHT MANUFACTURER REPORTABLE TO HPRDS SUPPLEHEHTAL REPORT EXPECTED (14)YES (If yes, complete EXPECTED SUBHISSIOH DATE)HO ABSIRACI (16)EXPECTED SUBHISSIOH MOHIH DAY YEAR ATE (15)On October 31, 1991, a reportability evaluation was completed that concluded that a problem associated with Qow control of the Primary Containment Hydrogen Recombiners was reportable.
A contract engineer, performing a setpoint calculation review, had discovered that incorrect Containment Atmospheric Control (CAC)Recycle Flow Control controllers (CAC-FC-67 A/B)were installed for both divisions in the control room.The plant design and operating procedures required these instruments to be used in the automatic mode of operation to control recombiner recycle Qow.If these incorrect controllers had been used in the automatic mode, they would not have controlled recycle Qow which could have resulted in a reduced recombination rate or possible system shutdown due to excessive recombination.
Immediate corrective action was taken to change plant procedures requiring operation of these instruments in the manual mode.This allowed plant operators to control recycle Qow from the control room by manually positioning the Recycle Flow Control Valve (CAC-FCV-6 A/B).The root cause of this event was a less than adequate design and design change process during plant construction/startup, A second cause was less than adequate testing programs and procedures.
LICENSEE EVENT REPORT (4)TEXT CONTINUATION AGILITY HAHE (1)Washington Nuclear Plant-Unit 2 DOCKET HUHBER (2)0 5 0 0 0 3 9 7 LER HUHBER (8)ear umber ev.Ho.AGE (3)I 29 01 ITLE (4)Inade uate Primar Containment Hydro en Recombiner Rec cle Flow Control 2 F 10 Further corrective action included a review of the design, testing, and operation of the CAC System by the Nuclear Safety Assurance Division.Nine man-months were spent by Supply System and Consultants on the review.Reportable concerns addressed by the SSFI included questions on control of the reaction and the operability of the catalyst.As a lesson learned from this, experience, additional reviews will be performed on similar systems.There was safety significance associated with events discussed in this LER revision since the operability of both divisions of one of the WNP-2 Engineered Safety Features was impacted.However, this safety significance is mitigated by the low probability of needing the CAC system with an inerted primary containment.
The event posed no threat to the health and safety of either the public or plant personnel.
Plan n iti n Power Level-100%PlantMode-1 Even Descri tion At approximately 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> on October 31, 1991, a reportability evaluation was completed that concluded a problem associated with the Containment Atmosphere Control (CAC)System was reportable.
The problem with the Qow instrumentation had been under review since it was discovered on August 7, 1991.A contract engineer identified the issue while evaluating the instrumentation associated with the CAC system as part of the Supply System's setpoint evaluation program.This event was reported under 50.72 at approximately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on October 31, 1991.At WNP-2 the CAC System includes redundant catalytic recombiners provided to combine the hydrogen and oxygen in the Primary Containment during degraded post-LOCA conditions.
The recombiner subsystems (A and B)are located adjacent to the Primar'y Containment in the Reactor Building (Secondary Containment).
Each redundant subsystem consists of a blower, wet scrubber, electric heater, catalyst vessel, after cooler, moisture seperator and associated instrumentation, valves and piping, A constant speed blower is used to draw the atmosphere from the Primary Containment, process it through the equipment and return it back to the Containment.
The amount of recombination is controlled by the amount of recycle Qow that is directed back through the unit.The amount of recycle Qow is controlled by Recycle Flow Control Valve, CAC-FCV-6 A/B.As the amount of recycle flow is increased, the rate of recombination-decreases.
If CAC-FCV-6 A/B is fully closed, the system functions with single pass Qow through the unit resulting in maximum recombination but risking subsystem shutdown due to high recombiner outlet temperature if the recombination rate becomes too high.Part of the instrumentation for the recombiner subsystem is associated with the control of recycle flow.CAC-FCV-6 A/B is controlled by a locally mounted Flow Indicating Controller, CAC-FIC-67 A/B, which receives a flow feedback signal from the Recycle Flow Transmitter CAC-FT-7 A/B.CAC-FIC-67 A/B, in turn, was designed to be controlled by remote Master Controller CAC-FC-67 A/B located in the control room.
LICENSEE EVENT REPORT (0)TEXT CONTINUATION ACILITY NANE (1)Washington Nuclear Plant-Unit 2 OOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUNBER (8)ear Number ev.No.1 029 01 AGE (3)3 F 10 ITLE (4)Inade uate Primar Containment H dro en Recombiner Recycle Flow Control The Remote Master Controller receives input on total fiow from Flow Transmitter CAC-FT-6 A/B.CAC-FC-67 A/B should be, by design, ratio-type setpoint stations providing, in the AUTO mode, the setpoint signal to CAC-FIC-67 A/B.Plant Procedures PPM 2.3.3 A/B, Containment Atmospheric Control, Revision 0, would have been used for post-LOCA operation of the system.These procedures called for CAC-FC-67 A/B to be in automatic on system initiation.
The contract engineer discovered the fact that CAC-FC-67 A/B are proportional-integral controllers rather than ratio type controllers.
These proportional-integral controllers receive total fiow as a process feedback signal.Their output, however, only controls recycle fiow.Hence, they are acting in an open control loop and their output will integrate either up or down until the recycle valves are full open or full closed.If the recycle valve went full open this would limit the containment gas fiow through the scrubber and dilute the hydrogen concentration at the recombiner.
The recombiner would continue to run under this condition but with reduced efiiciency.
If the recycle valve went closed, this could cause a high temperature rise across the recombiner, resulting in automatic system shutdown.The system would then have to be manually restarted.
Immedi te rr iv A i n In August 1991, Plant System Operating Procedures, PPM 2.3.3 A/B, Containment Atmospheric Control, were revised to require operation of CAC with CAC-FC-67 A/B in the manual mode.The recycle fiow (minimum recycle ratio)was to be set to the value given in the procedure.
This ratio was provided as a function of containment pressure.The procedure called for the control room operator (Section 5.3, CAC Operation Following LOCA)to periodically monitor recombiner catalyst temperature and Drywell pressure to maintain minimum recycle ratio (maximum recombination) by adjusting CAC-FC-67 A/B (See discussion under paragraph A.8 below for more recent changes to the CAC Operating Procedures).
Further Ev I i n nd rrective Action A.F her Evalu i n This event is being reported per the requirements of 10CFR50.73 under three different paragraphs.
First, it is reportable under 50.73(a)(2)(i)(B) as a"condition prohibited by the Plant's Tech Specs" since the system did not meet the OPERABLE definition contained therein.Second, 50.73(a)(2)(v) is also applicable as,"Any event or condition that alone could have prevented the fulfillment of the safety function..." in controlling the release of radioactive material and mitigating the consequences of an accident.Finally, 50,73(a)(2)(vii) is impacted since the event caused,"...two independent trains...to become inoperable...." in a single system designed to mitigate the consequences of an accident.
LICENSEE EVENT REPORT ()TEXT CONTINUATION AGILITY NAME (I)Mashington Nuclear Plant-Unit 2 00CKET HUHBER (2)0 5 0 0 0 3 9 1'ER HUHBER (8)ear umber ev.No.I 29 01 AGE (3)4 F 10 ITLE (4)Inade uate Primary Containment H dro en Recombiner Recycle Flow Control 2.Past records indicate that this discrepancy has existed since initial Plant Startup.Startup Problem Report SPR I-1145, dated June 2, 1981, documents the discovery that the Bailey controllers supplied for initial installation were not correct.The Bailey devices installed in the Control Room were Model 701 003ADAE1 proportional-type controllers, 3.Further review showed that Design Change PED 218-I-3923 was issued on February 11, 1982 to respond to this problem.The design change specified a Bailey Model 715 030AAE1 ratio setpoint controller for CAC-FC-67 A/B.Further investigation revealed that this design change alone would not have been sufficient to correct the problem.The Recycle and Total Flow Transmitters (CAC-FT-7 A/B and CAC-FT-6 A/B)were calibrated to different ranges.Further, the feedback signal to the flow controller was a delta-P signal directly from the transmitter since square root converters had not been installed.
Additional signal conditioning equipment would have been required to make the controllers (CAC-FC-67 A/B and CAC-FIC-67 A/B)function together correctly to control the Recycle Flow Control Valve CAC-FCV-6 A/B.4.The correct Bailey ratio-type setpoint stations were never installed.
The root cause investigation determined that a,change in procurement responsibilities at the time the correct setpoint station was identified, led to the failure to procure and install the correct device.The Startup Problem Report was closed out based on the issuance of the corrected design and the recommended System Lineup Test.5.A System Lineup Test was referenced on the Startup Problem report as being a required retest after replacement of the instrument.
This test was performed in April 1983 but it was limited to a functional check of the incorrectly installed Model 701 003ADAE1 proportional-type controller.
6.The Preoperational Test on the system was performed in December 1983.The Test Procedure has a step which states,"Set FC-67 to recycle 55 percent of the gas leaving the phase separator." The procedure did not specifically require placing CAC-FC-67A/B in the auto posi-tion.The preoperational test did not discover the fact that the incorrect device was installed.
7.Various surveillance tests are performed on equipment associated with the CAC system, This includes an 18-month surveillance (4.6.6.1.b.1) which requires"Performing a CHANNEL CALIBRATION of all recombiner operating instrumentation and control circuits." Plant Procedure PPM 7.4.6.6.1.3 C/D, H2 Recombiner 1 A/B Flow Instrumentation Channel Calibration, performs this surveillance test.On November 21, 1991, during a further evaluation associated with this LER, it was discovered that this surveillance had not tested the operation of the Recycle Flow Control Valve, CAC-FCV-6 A/B, from the Remote Master Flow Controller, CAC-FC-67 A/B in the manual mode of operation.
A trouble shooting plan was formulated and implemented that demonstrated movement of the CAC-FCV-6 A/B from the control room.
0 LICENSEE EVENT REPORT (0)TEXT CONTINUATION AGILITY NAHE (I)Washington Nuclear Plant-Unit 2 DOCKET NUHBER (2)0 5 0 0 0 3 9 7 LER NUHBER (B)ear umber I 29 ev.No.AGE (3)5 F 10 ITLE (4)Inade uate Primary Containment Hydro en Recombiner Recycle Flow'Control In early March.1992 additional testing was performed on the Hydrogen Recombiners to collect data on the performance of recycle Qow control and to verify system operability.-
Plant Proce-dure PPM 8.3.248, CAC-HR-1A Recycle Flow Verification from Drywell, was performed on March 11, 1992.'AC-HR-1B Recycle Flow.Verification from Drywell, was performed on March 12, 1992.These procedures established flow through the recombiner unit the way it would be configured during accident conditions; taking suction from the drywell and returning air to the wetwell.Recycle Qow was controlled manually from the control room under a variety of Qow conditions.
8.A review was performed of the 50.59 that implemented the change to PPM 2.3.3 A/B, System Operating Procedures for Containment Atmospheric Control (Division I/II).These procedures are referenced by the Emergency Operating Procedures and were changed previously (see Immediate Corrective Action above)to allow for manual operation of CAC-FC-67 A/B.The review found a Safety Evaluation was not performed on the change and one was completed on November 27, 1991.During the Safety Evaluation the discovery was made that operation of the system at 55 percent recycle flow could have resulted in automatic system shutdown due to high catalyst temperature caused by higher than expected Qows through the system.This could occur since the flow measured by the preoperational test was higher than the Qow assumed in the analysis.The analyzed Qow was 65.7 scfm compared to the measured flow of 86 scfm at atmospheric pressure.Recombiner mass flow would be even higher at elevated containment pressures due to increased density.These high flows resulted in a recommendation for additional changes to PPM 2.3.3 A/B.A deviation to these procedures was approved on November 27, 1991, (Procedure Deviations 91-1126 and 91-1127)that required an additional operator to be stationed at the recombiner panel in the control room as soon as possible, but no later than six hours following a LOCA (the design analysis assumes the recombiners are started six hours post accident).
This dedicated operator would provide added assurance that CAC recycle flow is monitored in a manner that would maximize the hydrogen and oxygen removal rate while preventing a high temperature shutdown.The plant operated with the procedures as described above until February 25, 1992.The SSFI team questioned the manual method being used to control the CAC system.They believed that manual recycle control based on recombiner exit temperature was not acceptable.
The instantaneous reaction rate associated with recombination could lead to high recombiner exit~temperatures resulting in system shutdown at the trip setpoint of 1150'F.This concern was verified by the consultants (Bechtel and United Catalyst).
Due to the transient nature of Post-LOCA operation oxygen or hydrogen fluctuations could come from a)localized pockets of unmixed gases, b)over compensating recycle Qow control by the operator or c)increasing scrubber dehumidification capacity from resetting water Qow.These fluctuations would be espe-cially critical if the recombiners were operated near their upper temperature limits.As a-result of this concern, Plant Procedures were changed to simplify operation of the CAC system.This change was performed with an appropriate 50.59 review and analysis.PPM 2.3.3 A/B, System r LICENSEE EVENT REPORT (L)TEXT CONTINUATION FACILITY NAHE (1)Washington Nuclear Plant-Unit 2 DOCKET NUHBER (2)0 5 0 0 0 3,9 7 LER NUHBER (8)ear umber ev.No.I 0 2 9 0 I AGE (3)6 F 10 ITLE'(4)Inade uate Primary Containment Hydro en Recombiner Rec cle Flow Control Operating Procedures for Containment Atmospheric Control (Division I/II)were changed to require the Plant Operators to place the CAC units on a constant 60 percent recycle flow under post-LOCA conditions.
The EOPs provide for early startup of the CAC System at 0.5 percent hydrogen.This low hydrogen concentration combined with high recycle flow will provide a large margin between the operating point and the high temperature trip.At the same time, this will provide for an adequate hydrogen and oxygen recombination rate.9 The review of the CAC system included a review of the results of the surveillance testing performed by Plant Procedures PPM 7.4.6.6.1.4/5, CAC-HR-1 A/B Functional Test and Visual Examination.
These tests have been performed on each train of CAC seven times since plant startup.These tests are performed as required by Technical Specification 4.6.6.1.b.3 which states that at least once per 18 months a functional test will verify that"....upon introduction of one percent by volume hydrogen in a 140-180 scfm stream containing at least one percent by volume oxygen, that the catalyst bed temperature rises in excess of 120'F within 20 minutes." The review found that for the A train the 1990 test results gave a 114'F temperature rise which did not meet the temperature rise requirement of'120'F.The review of the B train surveillances found the flows in 1988 and 1989 were higher than allowed by the Technical Specifications with values of 217 and 188 scfm (indicated).
The 1991 surveillances for both trains were checked and found to be satisfactory, The SSFI review further questioned the operability of the catalyst.These questions involved potential halogen poisoning during postulated accident conditions and possible water damage due to wetting and flooding during past testing The consultant reviewed past data on halogen testing.and the system design.Since the CAC system is designed with preheaters it operates with the feed temperature at 500'F.At this temperature halogen poisoning is not a concern since these gases are driven from the catalyst bed.The consultant also re-reviewed past test data to determine the condition of the existing catalyst.Heat and mass balances were performed to estimate the amount of conversion in different sections of the catalyst bed for seven years of test data.This analysis showed that the bulk of the reaction was occurring in the top two sections of the catalyst bed as it should for a healthy configuration.
The performance of the units was slightly different but within expected parameters.
The analysis did show that the"A" bed performance was less efficient when compared to the"B".However, variation in the process variables and instrumentation inaccura-cies on the two subsystem would also account for this difference.
On March 11 and March 12, 1992 the normal 18 month surveillance procedures for the catalyst, PPM 7.4.6.6.1.4/5, CAC-HR-1 A/B Functional Test and Visual Examination, were performed as part, of the plant restart effort.During this test the"A" catalyst achieved a 102'F per percent hydrogen temperature rise.Thus, it did not meet the Technical Specification required 120'F per percent hydrogen.
LICENSEE EVENT REPORT (0)TEXT CONTINUATION ACILITY NAME (1)Mashin9ton Nuclear Plant-Unit 2 00CKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUMBER (B)ear umber ev.No.1 029 1 AGE (3)7 F 10 ITLE (4).Inade uate Primary Containment H dro en Recombiner Rec cle Flow Control The test results and associated analysis made it evident that the acceptance criterion of the Technical Specification was very dependent on the analytical methods of calculating the input parameters and measurement of performance indicators; hydrogen concentration, process fiows and temperatures.
Depending on the data, the temperature rise could vary significantly.
The review had led to refinements in input parameter determination.
As a result, during this review the temperature rise acceptance criterion required by the Technical Specifications was identified as suspect.In addition to the analytical methods used to determine the input parameters, other factors such as: heat'removed by the gas Qow;heat capacity of the catalyst bed and the vessel;losses through vessel insulation, supports, and piping;time lag and heat loss caused by tempera-ture sensors and uncertainties in ffow determination during testing, led to a conclusion that the present temperature rise acceptance criterion was not, by itself, an accurate refiection of catalyst operability.
Test results showed variations primarily are a result of the ability to set initial conditions, input parameters, and instrument uncertainty.'he SSFI concluded that sampling of the infiuent and effiuent gases would be a more direct indication of catalyst efficiency.
This was confirmed with the assistance of industry experts in catalyst bed design and operation.
An appropriate acceptance criterion would be the sampling of the effluent gas stream for hydrogen concentration for a defined input volume percent of hydrogen.A sample retaining less than 25 parts per million by volume (ppmV)hydrogen after passing through the catalyst bed would indicate acceptable recombiner operation for a feed of at least one percent hydrogen by volume.In response to this recommendation the normal 18 month surveillance procedures for the catalyst, PPM 7.4.6.6.1.4/5, CAC-HR-1 A/B Functional Test and Visual Examination were modified to require sampling of hydrogen at both the inlet and outlet of the recombiner.
The sampling performed on March 11 and 12 showed 6 ppmV hydrogen concentration in the effluent stream of both recombiner trains with the"A" train showing slightly better performance.
It was these test results that led the Supply System to con-clude that the catalyst efficiency was acceptable and capable of performing in support of plant operation.
B.~Ro)~tglse.The root cause of these events was a less than adequate design and design change implementation.
Design Change PED 218-I-3923 was not driven to completion by the change process during construction and plant startup testing.The second root cause was less than adequate testing that should have identified the catalyst control problems discussed above at an earlier date.C.F rther orrective Action 1.The design change process in place during construction depended on contractors to implement changes that were issued by the Architect-Engineer.
It is concluded, based on the turnover process put in place at the end of construction, that the failure to implement Design Change LICENSEE EVENT REPORT)TEXT CONTINUATION ACILITY NANE (1)Mashington Nuclear Plant-Unit 2 OOCKET NUMBER (2)0 5 0 0 0 3,9 7 LER NUHBER (8)ear umber ev.No.I 0 2 9 0 I AGE (3)8 OF 10 TITLE (4)Inade uate Primary Containment Hydro en Recombiner Recycle Flow Control PED 218-I-3923 is an isolated occurrence.
The construction design change process in place when this event began was completely changed when the plant went into operation.
Therefore, no further corrective action is warranted.
2.3.A Safety System Functional Inspection (SSFI)was performed on the CAC System by the Nuclear Safety Assurance Division.Standard methodology was used which included the establishment of a design basis, and review of system parameters against the design.A more general action being taken in response to the problems associated with the CAC System involves the identification of other systems that may have characteristics similar to those which are believed to have contributed to the CAC situation.
This evaluation considered seven criteria: 1)Late additions to plant design, 2)Not fully testable, 3)Not fully designed by Burns and Roe 4)Not fully designed by General Electric 5)Low work control priority, 6)Importance of the system to Plant Organizations and 7)Current status of system deficiencies.
The results of this evaluation recommended four systems for consideration of additional reviews: Control Room Chillers, Post Accident Sampling, Main Steam~ge Control and Process Radiation Monitors.An engineering evaluation will be performed for each system.This will be followed by a limited team inspection.
It is our goal to have all evaluations and inspections completed by December 31, 1992.4.Plant Procedure PPM 7.4.6.6.1.3.C/D will be revised to incorporate a test of the CAC-FC-67 A/B to CAC-FCV-6 A/B instrument control loop.5.CAC surveillance procedures will be validated and verified to assure all Technical Specification functions are being performed.
6.CAC operating procedures were validated and verified.7.A Technical Specification amendment has been requested to surveillance requirement 4.6.6.1.b,3.
The requirement will read: "Verifying during a recombiner system functional test that, upon introduction of at least one percent by volume hydrogen into the catalyst bed preheated to a temperature not to exceed 300'F, the efHuent stream has a hydrogen concentration.
of less than 25 ppm by volume."~fi lfi We believe this event has safety significance since the operability of both divisions of one of the WNP-2 Engineered Safety Features was impacted.However, the actual safety significance is mitigated by the very low probability of the need for the system given the inerted primary containment.
LICENSEE EVENT REPORT (0)TEXT CONTINUATION FACILITY NAHE (1)Mashin9ton Nuclear Plant-Unit 2 DOCKET NUMBER (2)0 5 0 0 0 3 9 7 ear LER NUHBER (8)umber ev.No.1 029 01 AGE (3)9 F 10 ITLE (4)Inade uate Primary Containment H dro en Recombiner Rec cle Flow Control In the design basis analysis, the probability of hydrogen production following a large LOCA event has been assessed by the Supply System PRA effort.A large LOCA can be due to pipe break or due to failure of suffi-cient SRV's to open when needed.On the basis of generic failure rate for pipes and plant-specific failure rate for SRV's, the probability of a large LOCA has been determined.
A large LOCA event can be mitigated as long as any one of the ECCS systems operate.Plant-specific system unavailabilities have also been determined.
The hydrogen production (or a LOCA without coolant injection) probability can be assessed by multiplying the LOCA probability by the product of the ECCS System unavailabilities.
This number is approximately 1E-7/year.NRC's safety goal is 1E-4/year for core damage and 1E-6/year for containment failure.Although hydrogen production does not mean there is a subsequent burn or containment failure, hydrogen production probability already meets the safety goal for containment failure.Severe accident studies done in support of Individual Plant Evaluation (IPE)work has shown that the amount of oxygen generated and surviving as a gas in a'egraded core scenario is very small.With an inerted containment the oxygen concentration is not likely to exceed acceptable limits precluding the need for the hydrogen recombiners.
In addition, the initial work being done on the WNP-2 IPE concludes that CAC is a negligible contributor toward accident mitigation.
For core melt accidents, the exothermic metal water reaction, once started, generates large quantities of hydrogen.Since there is a limited amount of oxygen that can be reacted it is of marginal value.Hydrogen combustion is" not a possible containment failure mechanism for an inerted containment (
Reference:
FAI/91-110, Defiagration and Detonation of Hydrogen, July 1991).Similar Events The events related to CAC as discussed in this LER and recent related LERs on CAC are unique.The condition of the system and the number of problems found are not comparable to any other events reported at WNP-2.LER 92-003 reported the event where incorrect drawing information regarding overloads led to both divisions of CAC being inoperable during power operation.
Corrective action is underway for this event.LER 92-007 reported the problems associated with the CAC drain line that resulted in a plant shutdown in late February 1992.These problems have been corrected by piping modifications and verified by system testing.
LICENSEE EVENT REPORT ()TEXT CONTINUATION
'GILITY NAHE (I)Mashington Nuclear Plant-Unit 2 OOCKET NUHBER (2)0 5 0 0 0 3 9 7 LER NUHBER (8)ear umber ev.No.I 29 1 AGE (3)10 F 10 ITLE (4)Inade uate Primar Containment H'dro en Recombiner Rec cle Flow Control II Infrm i n Tex Referen Primary Containment Hydrogen Recombiner Containment Atmosphere Control (CAC)System CAC Recycle Flow Controller (CAC-FC-67 A/B)CAC Recycle Flow Control Valve (CAC-FCV-6 A/B)CAC Recycle Flow Transmitter (CAC-FT-7 A/B)CAC Local Recycle Flow Indicating Controller (CAC-FIC-67 A/B)CAC Total Flow Transmitter (CAC-FT-6 A/B)Containment Monitoring Control Panels (CMS-CP-1301/1401)
Containment Monitoring System Hydrogen Recorders (CMS-H2R-1/2)
CAC Recombiner Fan (CAC-FN-1 A/B)BB BB FC BB FCV BB BB BB FIC'T IK IK BB R FN E~l!f$gg~m Q~m~nen BB RCB