IR 05000413/2025004

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Catawba Nuclear Station - Integrated Inspection Report 05000413/2025004 and 05000414/2025004
ML26028A165
Person / Time
Site: Catawba  
Issue date: 01/29/2026
From: Robert Williams
NRC/RGN-II/DORS/EB1
To: Huecker J
Duke Energy Carolinas
References
IR 2025004
Download: ML26028A165 (0)


Text

SUBJECT:

CATAWBA NUCLEAR STATION - INTEGRATED INSPECTION REPORT 05000413/2025004 AND 05000414/2025004

Dear Jonathan Huecker:

On December 31, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Catawba Nuclear Station. On January 14, 2026, the NRC inspectors discussed the results of this inspection with Blaine Peters, Plant Manager, and other members of your staff.

The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Catawba Nuclear Station.

January 29, 2026 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Robert E. Williams, Jr., Chief Projects Branch 1 Division of Operating Reactor Safety Docket Nos. 05000413 and 05000414 License Nos. NPF-35 and NPF-52

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000413 and 05000414

License Numbers:

NPF-35 and NPF-52

Report Numbers:

05000413/2025004 and 05000414/2025004

Enterprise Identifier:

I-2025-004-0022

Licensee:

Duke Energy Carolinas, LLC

Facility:

Catawba Nuclear Station

Location:

York, South Carolina

Inspection Dates:

October 1, 2025, to December 31, 2025

Inspectors:

D. Rivard, Senior Resident Inspector

A. Wang, Resident Inspector

M. Kennard, Senior Operations Engineer

Approved By:

Robert E. Williams, Jr., Chief

Projects Branch 1

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Catawba Nuclear Station, in accordance

with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for

overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Correct Through Wall Leak in Letdown Piping at Vent Valve

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

NCV 05000414/2025004-01

Open/Closed

None (NPP)

71111.12

A self-revealed Green finding and associated non-cited violation (NCV) of 10 CFR Part 50,

Appendix B, Criterion XVI, "Corrective Action," was identified when the licensee failed to

correct a condition adverse to quality. Specifically, the licensee failed to implement corrective

actions to address the vibration of letdown line components, including vent and drain valves,

which resulted in pressure boundary through wall leakage at vent valve 2NV-951.

Additional Tracking Items

Type

Issue Number

Title

Report Section

Status

LER 05000414/2025-004-00

LER 2025-004-00 for

Catawba Nuclear Station,

Unit 2, Through Wall Leak in

Letdown Piping

71111.12

Closed

PLANT STATUS

Unit 1 operated at or near RTP for the entire inspection period.

Unit 2 began the inspection period shut down for scheduled refueling outage, C2R27. The unit

was returned to rated thermal power (RTP) on October 9, 2025, and operated at or near RTP

for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix DProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 2515,</br></br>Appendix D" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Nuclear service water system alignment to the nuclear service water pond for 2B

nuclear service water pump testing on October 16, 2025

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated system configurations during a complete walkdown of the

Unit 1 auxiliary feedwater system on November 21 and 25, 2025.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire area:

(1)

Fire area 51, Unit 1 exterior doghouse on November 25, 2025

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

The licensee completed the annual requalification operating examinations and biennial

written examinations required to be administered to all licensed operators in accordance

with Title 10 of the Code of Federal Regulations 55.59(a)(2), "Requalification

Requirements," of the NRC's "Operator's Licenses." The inspector performed an in-office

review of the overall pass/fail results of the individual operating examinations, the crew

simulator operating examinations, and the biennial written examinations in accordance with

IP 71111.11, "Licensed Operator Requalification Program and Licensed Operator

Performance." These results were compared to the thresholds established in Section 3.03,

"Requalification Examination Results," of IP 71111.11.

(1)

The inspectors reviewed and evaluated the licensed operator examination failure

rates for the requalification annual operating exam administered on August 14, 2025,

and the biennial written exam completed on August 16, 2024.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1)

The inspectors observed and evaluated licensed operator performance in the control

room during auxiliary feedwater flow balancing and reactor startup following Unit 2

refueling outage on October 4, 2025.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

The inspectors observed and evaluated crew performance evaluation 2507A

conducted in the plant reference simulator on November 13, 2025.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1)

Nuclear condition report (NCR) 02567300, for base metal flaw and through wall leak

upstream of letdown system vent valve (2NV-951) on October 16 and 17, 2025

(2)

Catawba Units 1 and 2 maintenance rule evaluation as required by

10 CFR 50.65(a)(3) as contained in NCR 02555944 Assignment 05 on

October 24, 2025

(3)

NCR 2530230, loss of 2A offsite power on October 28, 2025

Quality Control (IP Section 03.02) (1 Sample)

The inspectors evaluated the effectiveness of maintenance and quality control activities to

ensure the following SSC remained capable of performing its intended function:

(1)

Emergency diesel generator fuel oil sample failures on acceptance parameter for

lubricity as documented in NCRs 02544121, 02551674, 02554669 and 02556424

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Work order (WO) 20753527 to replace power supply #1 in 2B train solid state

protection system while adhering to the requirements of Selected Licensing

Commitment 16.7-16, "Reactor Trip Breaker and Solid State Protection System

(SSPS) Logic Train Out of Service Commitments"

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

NCR02567313, containment air return fan damper (2ARF-D-4) open delay failed to

meet surveillance requirement acceptance criteria

(2)

NCR 02570871, risk assessment for Mode 3 entry with Unit 2 loss of ability to operate

turbine driven auxiliary feed pump trip throttle valve (2SA-145) from control room

(3)

NCR 02572460, Unit 2 solid state protection system train B power supply #1 failure

(4)

NCR 02573442, power range nuclear instrument 2N43 declared inoperable due to an

axial flux difference alarm

(5)

NCR 02579802, Unit 2 2A auxiliary feed system sump pump and associated check

valve 2WL-838 failure

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1)

EC 424095, 2A hot leg resistance temperature detector replacement - rescale 2A

Thot-average signal

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated refueling outage C2R27 activities from September 3, 2025,

to October 5, 2025.

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system

operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (5 Samples)

(1)

PT/2/A/4200/023 B, "NC PORV and Air Supply Stroke Test," for pressurizer power

operated relief valve (PORV) air supply check valve (2VI-367) leakage repair, on

September 30, 2025

(2)

PT/2/A4250/003 C, "Turbine Driven Auxiliary Feedwater Pump #2 Performance Test,"

following loss of ability to operate turbine driven auxiliary feed pump trip throttle valve

(2SA-145) from control room, on October 4, 2025

(3)

WO 20747276 for 2B letdown orifice outlet vent (2NV-951) valve replacement, on

October 5, 2025

(4)

WO 20067119, Unit 1 letdown pressure control valve (1NV-148) failed to control

letdown system pressure due to a failure of the valve actuator, on December 3, 2025

(5)

WO 20765397 and WO 20765398 for 2A auxiliary feed system sump pump and

associated check valve repair, on December 17, 2025.

Surveillance Testing (IP Section 03.01) (1 Sample)

(1)

PT/2/A/4200/009, "Engineered Safety Features Actuation Periodic Test,"

Enclosure 13.1, "Train A ESF Test," performed on September 7 and 8, 2025

Ice Condenser Testing (IP Section 03.01) (1 Sample)

(1)

MP/0/A/7150/005, "Ice Basket Weight Determination," and inspections performed

under WO 20705059 throughout Unit 2 refueling outage

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)

(1)

Unit 1 (October 1, 2024, through September 30, 2025)

(2)

Unit 2 (October 1, 2024, through September 30, 2025)

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)

(1)

Unit 1 (October 1, 2024, through September 30, 2025)

(2)

Unit 2 (October 1, 2024, through September 30, 2025)

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (2 Samples)

(1)

Unit 1 (October 1, 2024, through September 30, 2025)

(2)

Unit 2 (October 1, 2024, through September 30, 2025)

71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1)

NCR 02302424, 1A emergency diesel generator #3 con-rod bearing found rotated

71153 - Follow-Up of Events and Notices of Enforcement Discretion

Event Report (IP Section 03.02) (1 Sample)

The inspectors evaluated the following licensee event report (LER):

(1)

LER 05000414/2025-004-00, Through Wall Leak in Letdown Piping (ADAMS

Accession No. ML25307A221). The inspection conclusions associated with this LER

are documented in this report under Inspection Results Section 71111.12. This LER

is closed.

INSPECTION RESULTS

Failure to Correct Through Wall Leak in Letdown Piping at Vent Valve

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

NCV 05000414/2025004-01

Open/Closed

None (NPP)

71111.12

A self-revealed Green finding and associated NCV of 10 CFR Part 50, Appendix B,

Criterion XVI, "Corrective Action," was identified when the licensee failed to correct a

condition adverse to quality. Specifically, the licensee failed to implement corrective actions to

address the vibration of letdown line components, including vent and drain valves, which

resulted in pressure boundary through wall leakage at vent valve 2NV-951.

Description: On September 5, 2025, during containment boric acid walkdowns, the licensee

discovered through wall leakage at the weld on the pipe elbow upstream of valve 2NV-951.

Vent valve 2NV-951 is a 1-inch valve that is socket welded to the 3-inch letdown line in a

cantilever configuration. The valve is used for ensuring that the associated piping is vented

for containment penetration leak rate testing.

The inspectors noted that the site had previous challenges associated with fatigue failure of

socket welded components on the Unit 2 letdown line and that there was a general

awareness of industry challenges with fatigue failures of socket welded components.

Specifically, in 2003, the licensee documented a leak caused by fatigue failure of piping at

vent valve 2NV-950 in NCR 01420620. Actions were taken to repair the leak at 2NV-950 by

using a butt weld to replace the failed socket weld. An evaluation of the event considered

eliminating vent and drain valves to reduce the number of socket welded components on the

letdown line, but due to the requirements of containment leak rate testing, the licensee was

unable to do so. The site also generated a corrective action to evaluate vibrational data on

the letdown line, including the associated vent and drain valves. However, several vent and

drain valves were not analyzed due to challenges with accessibility (this included valve

2NV-951). Despite the licensee recognizing vibration-induced fatigue failure in socket welded

piping, with licensee documents referencing industry operating experience including NRC

Information Notice 98-45, Cavitation Erosion of Letdown Line Orifices Resulting In Fatigue

Cracking of Pipe Welds, and EPRI TR-107455, Vibration Fatigue of Small Bore Socket

Weld Joints, the licensee did not generate any additional actions to monitor or correct this

deficiency.

The licensee submitted an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(ii)(A), as well as associated LER 050000414/2025-004-00, "Through Wall Leak in

Letdown Piping," in accordance with 10 CFR 50. 73(a)(2)(ii)(A), for a condition of the nuclear

power plant, including its principal safety barriers, being seriously degraded.

Corrective Actions: The licensee implemented a design change during the repair of the

2NV-951 line. Measures were taken to reduce susceptibility to fatigue failure, which included

reducing the weight of 2NV-951 and utilizing 2:1 tapered welds. The licensee also initiated

actions to evaluate a flow orifice design change to minimize pressure pulsations and

vibration.

Corrective Action Reference: NCR 02567300

Performance Assessment:

Performance Deficiency: The licensee's failure to correct vibration-induced fatigue issues on

the letdown line in accordance with 10 CFR Part 50, Appendix B, Criterion XVI, was a

performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Design Control attribute of the Initiating Events

cornerstone and adversely affected the cornerstone objective to limit the likelihood of events

that upset plant stability and challenge critical safety functions during shutdown as well as

power operations. Specifically, the failure to correct vibration-induced fatigue issues with

letdown line socket welds resulted in pressure boundary leakage at vent valve 2NV-951.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., The Significance Determination Process (SDP) for Findings At-Power. Using

IMC 0609, "Initial Characterization of Findings," and IMC 0609, Appendix A, "The

Significance Determination Process for Findings At-Power," Exhibit 1, "Initiating Events

Screening Questions," the inspectors determined the finding to be of very low safety

significance (Green) because all questions were answered no. Specifically, the leakage from

the 2NV-951 valve line was within the capacity of normal reactor coolant system makeup

sources.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance.

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part,

that measures be established to ensure conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are corrected. Contrary to the above, from 2003, to September 19, 2025,

the licensee failed to establish measures to ensure a condition adverse to quality associated

with letdown line vibration-induced fatigue was corrected. Specifically, the licensee did not

evaluate all socket welded components on the letdown line for vibration-induced fatigue

failure as identified in NCR 01420620, which resulted in pressure boundary leakage at vent

valve 2NV-951.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On January 14, 2026, the inspectors presented the integrated inspection results to

Blaine Peters, Plant Manager, and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed the Nuclear Safety Review Board report that was issued in October 2025.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.15

Corrective Action

Documents

02579624