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LER-2011-001, Regarding 1B Reactor Enclosure Recirculation System Charcoal Sample Analysis Results Exceeded TS Limit |
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| Reporting criterion: |
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(viii)(A)
10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(viii)(B)
10 CFR 50.73(a)(2)(iii)
10 CFR 50.73(a)(2)(ix)(A)
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(x)
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(v), Loss of Safety Function |
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| 3522011001R00 - NRC Website |
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text
10CFR50.73 July 7, 2011 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Limerick Generating Station, Unit 1 Facility Operating License No. NPF-39 NRC Docket No. 50-352
Subject:
LER 2011-001-00, 1B Reactor Enclosure Recirculation System This Licensee Event Report (LER) addresses an event that resulted in a condition prohibited by Technical Specifications as a result of a failed charcoal analysis on the 1B Reactor Enclosure Recirculation System.
This LER is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(i)(B).
There are no commitments contained in this letter.
If you have any questions, please contact John Hunter III at (610) 718-3400.
Respectfully, Original signed by William F. Maguire Vice President - Limerick Exelon Generation Company, LLC cc:
Administrator Region I, USNRC USNRC Senior Resident Inspector, LGS
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (10-2010)
LICENSEE EVENT REPORT (LER)
(See reverse for required number of digits/characters for each block)
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013
, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 1. FACILITY NAME Limerick Generating Station, Unit 1
- 2. DOCKET NUMBER 05000352
- 3. PAGE 1 OF 4
- 4. TITLE 1B Reactor Enclosure Recirculation System Charcoal Sample Analysis Results Exceeded TS Limit
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO.
MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 05000 05 09 2011 2011 - 001 - 00 07 07 2011 FACILITY NAME DOCKET NUMBER 05000
- 9. OPERATING MODE 1
- 10. POWER LEVEL 100
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A) 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A) 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)
OTHER 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D)
Specify in Abstract below or in LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET Previous Similar Occurrences There was one previous similar event during the last three years where charcoal sample analysis results rendered the "A" Control Room Emergency Fresh Air Supply (CREFAS) subsystem inoperable. This event was reported in LER 2009-002. The corrective action for this event was to add charcoal bed age and penetration data as inputs to bed performance monitoring and replacement decision making. This corrective action was implemented and resulted in a request by the System Manager on July 13, 2009 to change the 1B RERS charcoal bed based on age. However, it did not prevent recurrence due to unanticipated resource and charcoal replacement equipment issues.
Component data:
System:
Reactor Enclosure Recirculation System Component:
ADS Adsorber Component Number: 1B-F261 Manufacturer:
C780 CVI Corp
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| 05000352/LER-2011-001, Regarding 1B Reactor Enclosure Recirculation System Charcoal Sample Analysis Results Exceeded TS Limit | Regarding 1B Reactor Enclosure Recirculation System Charcoal Sample Analysis Results Exceeded TS Limit | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000353/LER-2011-001, For Limerick, Unit 2 Regarding Condition Prohibited by Technical Specifications Due to Inoperable Remote Shutdown Panel Instrument | For Limerick, Unit 2 Regarding Condition Prohibited by Technical Specifications Due to Inoperable Remote Shutdown Panel Instrument | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000353/LER-2011-002, Regarding Manual Actuation of the Reactor Protection System Due to Stator Cooling Water High Temperature Actuation | Regarding Manual Actuation of the Reactor Protection System Due to Stator Cooling Water High Temperature Actuation | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000352/LER-2011-002, Regarding Automatic Actuation of the Reactor Protection System Due to a Main Turbine Trip | Regarding Automatic Actuation of the Reactor Protection System Due to a Main Turbine Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000352/LER-2011-003, For Limerick, Unit 1, Regarding High Pressure Coolant Injection System Turbine Control Valve Failed to Fully Close During Testing | For Limerick, Unit 1, Regarding High Pressure Coolant Injection System Turbine Control Valve Failed to Fully Close During Testing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000353/LER-2011-003, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Reactor Core Isolation Cooling System | Regarding Condition Prohibited by Technical Specifications Due to Inoperable Reactor Core Isolation Cooling System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000353/LER-2011-004, For Limerick, Unit 2, Regarding Automatic Actuation of the Reactor Protection System Due to Actuation of Turbine Control Valve Closure Logic | For Limerick, Unit 2, Regarding Automatic Actuation of the Reactor Protection System Due to Actuation of Turbine Control Valve Closure Logic | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000353/LER-2011-005, Regarding Manual Actuation of the Reactor Protection System Due to Both Recirculation Pumps Trip | Regarding Manual Actuation of the Reactor Protection System Due to Both Recirculation Pumps Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) |
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