05000335/LER-1979-023-03, /03L-0 on 790702:control Element Assembly 33 Would Not Withdraw Due to Presence of Fullout Position Indication.Caused by Faulty Upper Electric Limit Reed Switch

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/03L-0 on 790702:control Element Assembly 33 Would Not Withdraw Due to Presence of Fullout Position Indication.Caused by Faulty Upper Electric Limit Reed Switch
ML17266A089
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 08/01/1979
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17206A963 List:
References
LER-79-023-03L-01, LER-79-23-3L-1, NUDOCS 7908140726
Download: ML17266A089 (2)


LER-1979-023, /03L-0 on 790702:control Element Assembly 33 Would Not Withdraw Due to Presence of Fullout Position Indication.Caused by Faulty Upper Electric Limit Reed Switch
Event date:
Report date:
3351979023R03 - NRC Website

text

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