05000335/LER-1979-035-03, /03L-0:on 791126,during Surveillance Test,One Channel of Refueling Water Tank Level Had Setpoint Out of Tolerance.Caused by Setpoint Drift in Channel Circuit. Setpoint Readjusted

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/03L-0:on 791126,during Surveillance Test,One Channel of Refueling Water Tank Level Had Setpoint Out of Tolerance.Caused by Setpoint Drift in Channel Circuit. Setpoint Readjusted
ML17266A123
Person / Time
Site: Saint Lucie 
Issue date: 12/26/1979
From: Shoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17207A729 List:
References
LER-79-035-03L, LER-79-35-3L, NUDOCS 8001110653
Download: ML17266A123 (1)


LER-1979-035, /03L-0:on 791126,during Surveillance Test,One Channel of Refueling Water Tank Level Had Setpoint Out of Tolerance.Caused by Setpoint Drift in Channel Circuit. Setpoint Readjusted
Event date:
Report date:
3351979035R03 - NRC Website

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AEtOATOATS SO EVENT OESCAIPTION ANO PAOBAELE CONSEQUENCES Qlo Durin a surveillance test one of four channels (Channel C) of Refueling Water. Tank Level in the Engineered Safeguards Actuation System was found with a setpoint slightly out of tolerance.

The other three re'dundant

~08 were within s ecification.

Also; by procedure, the channels are set conservativel b

about 1 inch and would have actua ed a

RAS signal prior to reaching the actual setpoin't.

This is the fourth occur-rence of this t e

See LERs 335-77-32 77-48 and 78-1 1

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~09 Water Tank level circuit.

Immediate corrective action was to readjust SYSTEM C*VSE

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The cause a 'ars to have been set oint drift of Channel C

Refuelin the Chan e

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