05000335/LER-1981-049-03, /03L-0:on 811012,during Refueling Outage & Retest for Plant Mod,Channel D Refueling Water Tank Bistable Would Not Trip Actuation Module.Cause Undetermined.Bistable Replaced & Tested Satisfactorily

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/03L-0:on 811012,during Refueling Outage & Retest for Plant Mod,Channel D Refueling Water Tank Bistable Would Not Trip Actuation Module.Cause Undetermined.Bistable Replaced & Tested Satisfactorily
ML17342A097
Person / Time
Site: Saint Lucie 
Issue date: 11/12/1981
From: Pace P
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17342A096 List:
References
LER-81-049-03L, LER-81-49-3L, NUDOCS 8111200841
Download: ML17342A097 (2)


LER-1981-049, /03L-0:on 811012,during Refueling Outage & Retest for Plant Mod,Channel D Refueling Water Tank Bistable Would Not Trip Actuation Module.Cause Undetermined.Bistable Replaced & Tested Satisfactorily
Event date:
Report date:
3351981049R03 - NRC Website

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