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LER-1980-076, /01T-0:on 800701,while Reactor Was at Hot Standby for Hpci/Reactor Core Isolation Cooling Testing,Site Notified by Ae That Listed RHR Supports Would Not Adequately Support All Design Based Loads |
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| 3211980076R01 - NRC Website |
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F ORM 366 L77)
LICENSEE EVENT REPORT NTROL BLOCK:
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l 8 9 LICENSEE CODE 14 15 LICENSE NUMUEH 25 26 LICENSE TYPE JO bl CAI $8 [ON'T
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8 50 61 DOCKET NUMBER 63 63 EVENT DATE 74 75 REPOHT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h
,o 121 lWhile the Un it 1 Reactor was at hot standby for HPCI/RCIC testing, the I
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that RilR supports 1 E 11 -RH R11-19 6, 313, 262, l
l site was notified by the AE
,g,3, l,o,,,gend 274 would not adequately support all of their design based loads.
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This is a repetitive occurrence for inadequate RHR supports, see LER # _j lo,3, g
l 50-321/1979-089.
There were no effects upon public health and safety duq 01611 o l 7 [ lto this event.
The RHR system was available and operable during the l
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- event, O la l l 80 DE CODE S BC E COMPONENT CODE SUBCOdE S
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10 11 12 83 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION
_ EVENT YEAR R EPORT NO.
CODE TYPE NO.
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22 23 24 26 27 28 29 30 31 32 AK N A O PL NT ME HOURS SB IT D FOR1 B.
SUPPL 1 MAN FAC URER
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3b 36 31 40 41 42 43 44 47 33 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l The problem with hangers 1E11-RHRH-196 and 313 was due to the use of in-1
,,,, gcorrect valve weights during the original design, and the problem with l hangers 1E11-RHRH-262 and 274 was due to welds being inadvertently leftl gg installation.
DCR # 80-222 and MR's 1-80-3532, 3526, and l
l g off during 3527'were implemented to correct the support problems.
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% POWER OTHER STATUS IS O RY DISCOVERY DESCHIPTION l
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lDl@l A/E Notification i s 80 17 8 re to 12 11 44 45 46 LOCATION OF RELE ASE AMOUNT OF ACTIVITY l
AELEASE@D OF RELE ASE@l NA l
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- 7' 8 9 10 11 44 45 PERSONNEL f MPOSURES NUMBEH TYPE DE SCH1PTION l
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8 9 11 12 LOSS OF OH DAMAGE TO FACillTY l
TYPE DE SCRIPitON [Z_j@l NA i 9 80 7
8 9 to NRC USE ONLY PuntlCITY DESCH6 piton 'r 800721037/
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LER-1:.-50-321/1980-076 Licensee:
Georgia' Power Company
' Facility:Name:
.Edwin I.
Hatch Docket #:
50-321
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Narrative
Report for LER 50-321/1980-076
, With' the Unit 'l reactor _at hot' standby for HPCI/RCIC testing andt adjustment the. site was notified that the. axial supports
'.(RHRH-196 -and - RHRH-313) _ f or the 2D"-suction lines between the lEll-F006A-D. valves were inadequate.
Later that day, the site
~
- - notified _ that two.other RHR supports were. inadequate.
was Both a r'e on.4 inch lines; RHRH-262 is -around the IEll-F090 check ' valve ~ and RHRH-274 is-around the-lEll-F026B valve.
While reviewing the as-builts submitted for the I.E.
Bulletin 79-14 program.the Architect Engineer. discovered ' that hangers lEll-RHRH-196, lEll-RHRH-313, IEll-RHRH-262, and IEll-RHRH-274 Twould not. adequately support all.of their design based loads.
^This' situation constituted a-degradation of part of the Unit 1 RHR sys tem. pip.ing,
but the LPCI piping remained adequately supported ~through out-the event.
This is a
repetitive occurrence for inadequate RHR supports, reference R.O.
Number 50-321/1979-089.-
There were no effects upon public health and
-. safety due to-this - event.
The RHR system was not inoperable
. during this event _and the- ' core -spray,
- ADS, LPCI, and RCIC systems. were.also~ available and operable.
The apparent cause of -the event as
'it
- - relates to hangers lE11-RHRH-196 and
.lEll-RHRH-313 was a. design. deficiency in which incorrect valve
- weights were_ use'd in-the original. analysis.
The problems relating to' hanger lEll-RHRH-262 and lEll-RHRH-274 were caused
- by~ improper- -field installation, some ' welds were left off.
Design Change Request. number 80-222 and Maintenance Request numbers 1-80-3532', :1-80-3526, and 1-80-3527 were written and implemented';to correct the -problems mentioned.-above.
The review - of I. E '.Bulletin no. 79-14 as builts for the similar-supports
. are now- 'in - full compliance with the design specifications so, no further reporting is r e q u'i r e d.
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| 05000321/LER-1980-001-01, /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | | | 05000366/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000366/LER-1980-001-03, /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | | | 05000321/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000321/LER-1980-002-03, /03L-0:on 800112,while Performing HNP-1-3655,fan lT46-C001B Would Not Meet Flow Requirements Per Tech Specs. Ten Days Later,While Venting Drywell Per HNP-1-1500,flow Did Not Meet Tech Specs.Equipment Recalibr | /03L-0:on 800112,while Performing HNP-1-3655,fan lT46-C001B Would Not Meet Flow Requirements Per Tech Specs. Ten Days Later,While Venting Drywell Per HNP-1-1500,flow Did Not Meet Tech Specs.Equipment Recalibr | | | 05000321/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000366/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000366/LER-1980-002-01, /01T-0:on 800128,during Cold Shutdown,Ae Notified Util That Single Mode Failure Existed for Torus Gravity Fill Isolation Valve 2G51-F013.Caused by Design Deficiency. Standing Order Issued | /01T-0:on 800128,during Cold Shutdown,Ae Notified Util That Single Mode Failure Existed for Torus Gravity Fill Isolation Valve 2G51-F013.Caused by Design Deficiency. Standing Order Issued | | | 05000366/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000366/LER-1980-003-03, /03L-0:on 800117,while Applying Equalizing Charge to 125/250-volt Dc Station Svc Batteries,Hpci Automatic Flow Control Power Inverter Tripped.Caused by Instrument Drift. Instrument Recalibr Satisfactorily | /03L-0:on 800117,while Applying Equalizing Charge to 125/250-volt Dc Station Svc Batteries,Hpci Automatic Flow Control Power Inverter Tripped.Caused by Instrument Drift. Instrument Recalibr Satisfactorily | | | 05000321/LER-1980-003-03, While Performing RHR Valve Operability Procedure,Outboard Shutdown Cooling Isolation Valve F008 Opened in 25.8-S.Caused by Normal Wear & Human Reaction Time.Valve Operator Adjusted | While Performing RHR Valve Operability Procedure,Outboard Shutdown Cooling Isolation Valve F008 Opened in 25.8-S.Caused by Normal Wear & Human Reaction Time.Valve Operator Adjusted | | | 05000321/LER-1980-003, Forwards Revised LER 80-003/03X-1 | Forwards Revised LER 80-003/03X-1 | | | 05000321/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000321/LER-1980-004-03, /03L-0:on 800106,during Startup Mode,Main Steam Line Inboard Isolation Drain Valve Failed in mid-position. Caused by Failure of Valve Motor Winding.Motor Replaced & Valve Returned to Operable Status | /03L-0:on 800106,during Startup Mode,Main Steam Line Inboard Isolation Drain Valve Failed in mid-position. Caused by Failure of Valve Motor Winding.Motor Replaced & Valve Returned to Operable Status | | | 05000366/LER-1980-004-03, /03L-0:on 800118,during Steady State Power Operation Hydrogen Recombiner Inlet Valve 2T49-F003A Did Not Open.Caused by a Failed Torque Switch.Sys Returned to Operation After Switch Was Replaced | /03L-0:on 800118,during Steady State Power Operation Hydrogen Recombiner Inlet Valve 2T49-F003A Did Not Open.Caused by a Failed Torque Switch.Sys Returned to Operation After Switch Was Replaced | | | 05000366/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000321/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000321/LER-1980-005-03, /03L-0:on 800109,w/reactor Mode Switch in Run Mode,Discovered That Surveillance Procedure HNP-1-3007, Turbine Control Valve Fast Closure,Was Not Performed in Grace Period.Caused by Personnel Error | /03L-0:on 800109,w/reactor Mode Switch in Run Mode,Discovered That Surveillance Procedure HNP-1-3007, Turbine Control Valve Fast Closure,Was Not Performed in Grace Period.Caused by Personnel Error | | | 05000366/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000366/LER-1980-005-03, /03L-0:on 800119,during Power Operation,Tech Specs 4.8.1.1.1.a & 4.8.1.1.2a4 for Electrical Power Sources Were Not Performed within 1-h.Caused by Personnel Misinterpretation of Tech Spec Requirements | /03L-0:on 800119,during Power Operation,Tech Specs 4.8.1.1.1.a & 4.8.1.1.2a4 for Electrical Power Sources Were Not Performed within 1-h.Caused by Personnel Misinterpretation of Tech Spec Requirements | | | 05000321/LER-1980-006-03, /03L-0:on 800113,one Standby Gas Treatment Sys Rendered Inoperable W/Both Units in Power Operation.Unit Not Proven Operable within Required 4-h.Caused by Inability to Prove Filter Train Operable within 4-h | /03L-0:on 800113,one Standby Gas Treatment Sys Rendered Inoperable W/Both Units in Power Operation.Unit Not Proven Operable within Required 4-h.Caused by Inability to Prove Filter Train Operable within 4-h | | | 05000321/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000321/LER-1980-007-03, /03L-0:on 800114,while Testing Standby Svc Water Pump,Pump Would Not Meet Criteria.Caused by Disengagement of Pump First Stage Impeller Lock Collet.Lock Collet Replaced & Pump Reinstalled | /03L-0:on 800114,while Testing Standby Svc Water Pump,Pump Would Not Meet Criteria.Caused by Disengagement of Pump First Stage Impeller Lock Collet.Lock Collet Replaced & Pump Reinstalled | | | 05000321/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000366/LER-1980-007-01, /01T-0:on 800130,while Performing High Drywell Pressure Instrument (Reactor Protection Sys) Functional Test & Calibr,Instruments 2C71-N002A,B & D Exceeded Tech Specs.Caused by Instrument Drift | /01T-0:on 800130,while Performing High Drywell Pressure Instrument (Reactor Protection Sys) Functional Test & Calibr,Instruments 2C71-N002A,B & D Exceeded Tech Specs.Caused by Instrument Drift | | | 05000366/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000366/LER-1980-008-03, While Increasing Reactor Power by Rod Withdrawal,Operator Noticed Rod Select Matrix Backlighted & Rod Sequence Control Sys Not Initiating Rod Blocks Properly.Caused by Design Change | While Increasing Reactor Power by Rod Withdrawal,Operator Noticed Rod Select Matrix Backlighted & Rod Sequence Control Sys Not Initiating Rod Blocks Properly.Caused by Design Change | | | 05000366/LER-1980-008, Forwards LER 80-008/03L-1 | Forwards LER 80-008/03L-1 | | | 05000321/LER-1980-008-03, /03L-0:on 800115,during Steady State Power Operation,Secondary Containment Integrity Violated When Personnel Opened 164-ft Elevation Reactor Bldg & Turbine Bldg Airlock Doors Simultaneously.Procedure Revised | /03L-0:on 800115,during Steady State Power Operation,Secondary Containment Integrity Violated When Personnel Opened 164-ft Elevation Reactor Bldg & Turbine Bldg Airlock Doors Simultaneously.Procedure Revised | | | 05000321/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000366/LER-1980-009-03, /03L-0:on 800130,while Performing Procedure HNP-2-33-3,HPCI Min Flow Valve 2E41-F012 Failed to Close. Caused by Sticking Switch Contacts on Flow Switch 2E41-N006. Switch Contacts Cleaned & Procedure HNP-2-3303 Performed | /03L-0:on 800130,while Performing Procedure HNP-2-33-3,HPCI Min Flow Valve 2E41-F012 Failed to Close. Caused by Sticking Switch Contacts on Flow Switch 2E41-N006. Switch Contacts Cleaned & Procedure HNP-2-3303 Performed | | | 05000321/LER-1980-009-03, /03L-0:on 800118,during Normal Operation,Drywell/ Torus Temp Recorder 1T47-R611 Found Stamping Erratically, Making Drywall & Torus Air Temps & Water Temp Difficult to Ascertain.Caused by Failure of Microswitch.Switch Replace | /03L-0:on 800118,during Normal Operation,Drywell/ Torus Temp Recorder 1T47-R611 Found Stamping Erratically, Making Drywall & Torus Air Temps & Water Temp Difficult to Ascertain.Caused by Failure of Microswitch.Switch Replaced | | | 05000366/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000321/LER-1980-010-03, /03L-0:on 800118,during Normal Operation While Performing Standby Liquid Control Pump Operability Test & Relief Valve Test,Pump a Discharge Relief Valve 1C41-F029A Operated at 1,225 Psig.Caused by Setpoint Drift.Valve Reset | /03L-0:on 800118,during Normal Operation While Performing Standby Liquid Control Pump Operability Test & Relief Valve Test,Pump a Discharge Relief Valve 1C41-F029A Operated at 1,225 Psig.Caused by Setpoint Drift.Valve Reset | | | 05000321/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000366/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000366/LER-1980-010-03, /03L-0:on 800131,during Reactor Startup,At 58% Power,Max Total Peaking Factor Was Calculated at 3.0 Compared to Design Value of 2.38.Caused by Lower than Normal Xenon Distribution During Startup | /03L-0:on 800131,during Reactor Startup,At 58% Power,Max Total Peaking Factor Was Calculated at 3.0 Compared to Design Value of 2.38.Caused by Lower than Normal Xenon Distribution During Startup | | | 05000321/LER-1980-011-03, /03L-0:on 800120,while at Steady State Power, torus-to-drywell Differential Pressure recorder,LT48-R631B Had Low Reading.Cause Not Stated | /03L-0:on 800120,while at Steady State Power, torus-to-drywell Differential Pressure recorder,LT48-R631B Had Low Reading.Cause Not Stated | | | 05000366/LER-1980-011-03, /03L-0:on 800202,while Performing Reactor Core Isolation Cooling Shutdown Flow Test,Power Inverter for Remote Flow Control Loop Found to Be Tripped.Caused by Defective Input Filter Capacitors | /03L-0:on 800202,while Performing Reactor Core Isolation Cooling Shutdown Flow Test,Power Inverter for Remote Flow Control Loop Found to Be Tripped.Caused by Defective Input Filter Capacitors | | | 05000321/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000366/LER-1980-012-03, /03L-0:on 800214,while at Full Power,Rhr & Plant Svc Water Min Flow Line Found to Be Inadequately Supported. Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | /03L-0:on 800214,while at Full Power,Rhr & Plant Svc Water Min Flow Line Found to Be Inadequately Supported. Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | | | 05000321/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000366/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000321/LER-1980-012-03, /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | | | 05000321/LER-1980-013, Forwards Updated LER 80-013/03X-1 | Forwards Updated LER 80-013/03X-1 | | | 05000321/LER-1980-013-03, Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | | | 05000366/LER-1980-013-03, /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | | | 05000366/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000366/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000366/LER-1980-014-03, /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | |
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