05000321/LER-1980-057-03, /03L-0:on 800525,while Performing Procedure HNP-1-1114,RHR Shutdown Cooling Mode,Shutdown Cooling Suction Valve Failed to Open.Caused by Faulty Auxiliary Contact Block.Contact Block Replaced

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/03L-0:on 800525,while Performing Procedure HNP-1-1114,RHR Shutdown Cooling Mode,Shutdown Cooling Suction Valve Failed to Open.Caused by Faulty Auxiliary Contact Block.Contact Block Replaced
ML19324A087
Person / Time
Site: Hatch 
Issue date: 06/13/1980
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19324A084 List:
References
LER-80-057-03L, LER-80-57-3L, NUDOCS 8006200461
Download: ML19324A087 (2)


LER-1980-057, /03L-0:on 800525,while Performing Procedure HNP-1-1114,RHR Shutdown Cooling Mode,Shutdown Cooling Suction Valve Failed to Open.Caused by Faulty Auxiliary Contact Block.Contact Block Replaced
Event date:
Report date:
3211980057R03 - NRC Website

text

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8 60 61 DOCKET NUMBER Gi 63 EVENT DATE 14

~15 HEPORT DATE SO EVENT DESCRIPTION AND PRODABLE CONSEQUENCES h

[ OE l With the reactor in the shutdown mode. while nerforming Procedure liNP-1 0131 l l-1114. RilR Shutdown Cooling Mode, on the

'B' division, the Shutdown Cool-l o 4 l

ing Suction Valve, I E l l-F006B_, for the

'B' RilR pump failed to open. The l

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'B' RilR pump was declared inoperable.

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[TITl l for maintenance, both pumps in the

'B' division were required to be operable i

10 l 7 l l per Tech Spec 3. 5.B. I.b.

This event was not repetitive and there were 1

0 s l no effects to public health and safety.

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The f ailure of the lEll-F006B valve to open was due to a faulty auxiliarv l

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cantact block. The ncrually cloacd contact, which is in the open circuit, i

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replaced and the valve returned to service. The

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NARRATIVE

REPORT.

Georgia Power _ Company Plant E.1. Hatch

.Bax1cy,' Georgia 31513-Reportabic-Occurrence Report No. 50-321/1980-057.

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aOn May 25,1980, with the reactor in the shutdown mode, while performing procedure HNP-1-lll4,.RHR Shutdown Cooling Mode, on the

'B' division, the Shutdown Cooling Valve, IEll-F006B, for the

'B' RHR pump failed to open.

The 'B' 'RHR' pump was declared inoperabic. The

'B' pump was required to be operabic per Tech. Spec 3.5.B. I.b due to the ' A' division of the RHR system being out for maintenance.

Upon investigation of the failure, personnel discovered that a normally-closed auxiliary contact in the open circuit was stuck open. The auxiliary contact block, located on the motor control center starter, was replaced and the valve returned to service. The

'B' RHR pump was then placed back in_ operation.

This was not a repetitive event nor were there any effects to public health and safety.

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