05000333/LER-1980-069-03, /03L-0:on 800807,during Normal Shutdown,While Conducting Surveillance Test F-ST-22A,auto Depressurization Sys Timer Found Set Below Limit.Caused by Setpoint Drift. Timer Adjusted & Returned to Svc

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/03L-0:on 800807,during Normal Shutdown,While Conducting Surveillance Test F-ST-22A,auto Depressurization Sys Timer Found Set Below Limit.Caused by Setpoint Drift. Timer Adjusted & Returned to Svc
ML19331D417
Person / Time
Site: FitzPatrick 
Issue date: 08/29/1980
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19331D414 List:
References
LER-80-069-03L, LER-80-69-3L, NUDOCS 8009020422
Download: ML19331D417 (1)


LER-1980-069, /03L-0:on 800807,during Normal Shutdown,While Conducting Surveillance Test F-ST-22A,auto Depressurization Sys Timer Found Set Below Limit.Caused by Setpoint Drift. Timer Adjusted & Returned to Svc
Event date:
Report date:
3331980069R03 - NRC Website

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60 61 DOCKET NUMBER 63 69 EVENT DATE 74 75 REPORT DATE 80 EVENT OESCRIPTION AND PROB ABLE CONSEQUENCES h I

10121l During normal shutdown while conducting Survnillnnca Tn e F " ??A

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o l3l l was found set at 112 seconds when TS Table 3.2-2 required a setpoint of 115 to 125 l

cause n sicm 4 P enn e l 1 o l.i l l seconds. Operation of the timer 3.,

( seconds early would not l o 151 l change in Che operation of the system.

The system was not reauired to be ocarnblo I

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