05000333/LER-1980-089-03, /03L-0:on 801126,reactor Core Isolation Cooling Steam Line Low Pressure Switch 13-PS-87B Found Set Outside Tech Spec Limits.Caused by Instrument Drift.Switch Adjusted & Surveillance Frequency Increased

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/03L-0:on 801126,reactor Core Isolation Cooling Steam Line Low Pressure Switch 13-PS-87B Found Set Outside Tech Spec Limits.Caused by Instrument Drift.Switch Adjusted & Surveillance Frequency Increased
ML19351F083
Person / Time
Site: FitzPatrick 
Issue date: 12/17/1980
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19351F076 List:
References
LER-80-089-03L, LER-80-89-3L, NUDOCS 8012290447
Download: ML19351F083 (1)


LER-1980-089, /03L-0:on 801126,reactor Core Isolation Cooling Steam Line Low Pressure Switch 13-PS-87B Found Set Outside Tech Spec Limits.Caused by Instrument Drift.Switch Adjusted & Surveillance Frequency Increased
Event date:
Report date:
3331980089R03 - NRC Website

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RCIC steam line low pressure switch 13-PS-87B was found set at 44.0 PSIG when l

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